IR 05000454/1989017

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Safety Insp Repts 50-454/89-17 & 50-455/89-19 on 890820- 0930.Violation Noted.Major Areas Inspected:Licensee Action on Previous Insp Findings,Operational Safety,Onsite Event Followup,Plant Matl Condition & LER Followup
ML19327B471
Person / Time
Site: Byron  Constellation icon.png
Issue date: 10/19/1989
From: Hinds J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19327B466 List:
References
50-454-89-17, 50-455-89-19, NUDOCS 8910310249
Download: ML19327B471 (13)


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U.S. NUCLEAR REGULATORY COMMISSION

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REGION III

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,o Report'Nos.50-454/S9017(DRP);50-iS0/89019(DRP)

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Docket Nos.'50-454;.50-455 Licenses Nos. NPF-37; NPF-66

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9l Licensee: 'Commhnwealth'EdisonCompany

' Post Office Box 76/

Chicago, IL 60690 Fadility Name: Byron Station,' Units I and 2 Inspection At:. Byron Station, Byron, Illinois Inspection Conducted: August 20 through September 30, 1989 l

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Inspectors:

W.'d. Kropp

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'R.'S.'Sutphin d

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,3 R. B. Holtzman

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D. R. Calhoun

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' Approved By:b'.'flinds, h

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ief to 19.M

. Reactor Projects Section IA Date I

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Inspection Summa g Inspection from August 20 throu h.leptember 30,1989 (Reports

.Nos. 50-454/83017(DRP); SO R 9019(DRPJ)

Arers Inspe::ted:. Routine, unannounced safety inspection by the resident

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, inspectors of Ticensee action on previous inspection findings; operational

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safety;; onsite event follow-up; plant mater 4al condition; fitness' for duty

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program; maintenance / surveillance activities; backlog; LER Follow-up; evaluation of licensee quality ' assurance program; radiological environmental

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i monito'r.in0 program; onsite-review; discrepancy records; and meetings.

Results: Of the 12 areas inspected, no violations or deviations were identified

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E ll areas; one violation was identified in the following area; radiological a

4\\l anvironmental monitoring program, Paragraph 6.

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DETAILS

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1.

Persons Cnnta:ted Commonwealth Edison Compa,ny

    • R. Pleniewicz, Station Manager s
  1. G. Schwartz, Production Superintendei t

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.# R. Ward, Technical Superintendent

  1. J. Kudalis, Service Director D. Brir 'le, Operating Engineer, Administration T. Didier, Operating Engineer Unit 0 T. Gierich, Operating Engineer, Unit 2 T. Higgins, Ass'stant Superintendent, Operating e
  1. J. Schrock, Operating Engineer, Unit 1 D. St. Clair, Assistent Superiatendent, Work Planning
  1. T. Tulon, Assistant Saperintendent, Maintenance
  1. D. Winchester, Quality Assurance Superintendent
  1. D. Wozniak, ENC Project Manager

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    • E. Zittle, Reguistory Assurance Staff The inspector also contacted and interviewed other licensee and, contractor pe*sonnel during the course of this inspectinn.
  1. Denotes those present during the exit inte~ view on September 29, 1989.

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  • Denotes those present during a telephone discussion on September 1,1989 with R. B. Holtzman, NRC regional inspector.

2.

Action on Previous Inspection Findings (92701 and 92702)

a.

NRC Region III management has reviewed open iters for the Byron Station and determined that the following open items will be closed administratively due to a lack of safety significance, age of the item, and other priority work. Tha licensee is reminded that commitments directly related to these open items are the sole res,tonsibility of the licensee and must be met as specified. NRC Region III will review licensee actions by periodically conducting L statistical sample of administratively closed items.

Unit 1 Open Item 454/89004-03 Unresolved lue,m 454/89004-01

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. Bulletins 454/87001-BB 454/88005-1B 454/87002-BB 454/88008-BB 454/87002-2B 454/88008-1B

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454/08002-BB 454/88010-BB 454/88004-BB 454/88011-BB-Generic Letters 454/88003-HH 454/88017-HH 454/88014-HH 454/88020-HH Unit 2 Open Items 455/86040 05 455/89007-03

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Bulletins 455/87003-BB 455/88005-1B 455/87002-BB 455/88008-BB 455/07002-1B 455/88008-1B 455/88004-BB 455/88010-BB 455/83011-BB Generic Letters

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455/38003-HH 455/88017-HH 455/88314-HH 455/86020-HH 3.

Plant Operations

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Unit 1 operated at power levels up;to 100% for the entire report period.

Unit 2 operated at power icvcis up to 96% for the entire report period, a.

Ogerational Safety (71707)

The inspectors observed control room operation, reviev:3d applicable logs and conducted discussions with control room operators.

During these discussions and observations, the inspectors ascertained that the operators were alert, cognizant of plant conditions, attentive to changes in these conditions, and took prompt action when appropriate.

The inspectors verified the operability vf selected emergency systems, reviewed tagout reccrds and verified proper return to service of affected components. Tours of the auxiliary and turbine buildings were conducted to observe plant equipnent

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conditions, including potential fire hazards, fluid leaks and

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cxcessive vibration and to verify that maintenance requests had been inftiated for equipment in need of maintenance.

The inspectors verified by observation and direct interviews that the physical security plan was implemented in accordance with the station security plan.

The inspectors observed plant housekeeping / cleanliness conditions and verified implementation of radiation protection controls. The inspectors ~ considered housekreping above average except in the

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following two areas, the Unit 2 auxiliary electric rooms and the electrical maintenance shops. The housekeeping in these two areas were considered poor; however, the inspectors noted an imprnvement

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during subsequent walkdowns of the Unit 2 auxiliary electric rooms later in the inspection period. With regards to the electrical maintenance shops, additional management attention is needed.

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During the inspection period, the inspectors walked down the accessible portions of the Unit I and 2 auxiliary feedwater (AFW)

systems and Unit I rod control system to verify operability.

These reviews and observations were conducted to verify that facility operations were in accordance with the requirements establishert under Technical Specifications, 10 CFR and administrative procedures.

One concern was identified that pertained to the auxiliary feedwater (AFW) pump suction pressure transmitter setpoint. On August 29 and 30, 1989, the AFW pump suction pressure transmitters were recalibrated by the licensee to accommodate a revised suction pressure setpoint reference. The previous reference point was

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the location of the pressure transmitter. The new reference point was identified as the location of the instrement tap en the AFW suction piping. A letter, dated September 5,1989, to the Byron-Project Manager from Sargent and Lundy, stated that relative to the initial reference setting, the allowable value of inches Hg vacuum specified in Technical Specification.3.3-4 was exceedcd for three of the four AFW pump suction pressure transmitters (2-Unit 1, 1-Unit 2). Additionally, new information concerning another change of the setpoint reference has been introduced and discussed with the licensee. This item is considered unresolved (454/89017-01(DRP);

456/89019-01(DRP)) pending fu.ther evaluation of data by the licensee and NRC staff review upon receipt of the applicable LER.

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Onsite Event follow-up (93702)

The inspectors reviewed an even', that involved the accidental discharge of the hilon fire suppression system to che Unit I upper j

cable spreading room (UCSR) on August 31, 1989. A technician

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inadvertently grounded a set of contacts in the halon release system during the performance of surveillance, IDHS FP-18. The entire

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p contents of seven halon bottler were discharged into the UCSR, and.

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t. fire alarm signal was generated. The station fire brigade and security forces responded. There was no fire and no personnel injuries. This event occurred just prior to the Labor Day weekend, so the replacement of halon and complete retesting of the system was slightly delayed. Fire watches were posted for the entire time that the halon system was considered out-of-service.

Efforts were initiated inr:ediately to investigate the cause and provide corrective

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measures to prevent recurrence.

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CurrentMaterialCondition(71707)

l The inspectors performed general plant as well as selected system

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and component walkdowns to assess the general and specific material condition of the plant, to verify that Nuclear Work Requests (NWRs)

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had-been initiated for identified equipment' problems, and to

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evaluate. housekeeping.

Walkdowns included an assessment of the buildings, com)onents, and

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systems for proper identification and tagging, accessiaility, fire and security door integrity, scaffolding, radiological controls, and any unusual conditions.

Unusual conditions included but werc not limited to water, oil, or other liquids on the floor or equipment; indications of leakage through ceiling, walls or floors; loose insulation; corrosion; excessive noise; unusual temperatures; and abr.ormal ventilation and lighting.

Results were as follows:

(1) Overall material condition of the diesel driven fire pump needs improvement.

(F) Scaff ald was noted in Unit 2 6.9 kv switchgear room on September 8, 1989. The scaffold had been up since July 3,1989,

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and the scaffold tag had expired July 29, 1989. This scaffold

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was subsequently removed.later in the inspection period.

i The inspectors did nut identify any significant material deficien-l cies and the material condition of the plant was cor.sidered above

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average for this report period.

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" Fitness for Duty" Program Support (71707)

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i During this inspection period the inspectors observed the

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presentation by the licensee, to the personnel at the By.on Station, l

of the SST Production " Intervention Theatre." This program, presented by professionel actors lasted app.oximately one hour and was presented

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l sev ral times during the month of September for the berefit of the Byron Station' personnel. This presentation was a highly entertaining alternative to the conventional approaches used to con:nunicate and l

educate in the general area of substance abuse. The objective of

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the presentation was to introduce the con:. apt of intervention which takes place when abusers come face-to-face with their problem and are

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offered the means cf initiating a recovery. The overall objective

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was to prompt and motivate those needirg counseling and/or treatment to seek out the appropriate sources of help. The Ceco Byron Employee Assistance Program (EAP) Coordinator was on hand durir.g the presentations to answer any questions and to explain the company s

policies in this general area of fitness for duty.

No violations or deviations were identifind.

4.

Maintf,rjnce/ Surveillance (61726 & 62703)

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Activities Station maintenance and surveillance activities of the safety-related systems and components listed below were observed or reviewed to determine that the activities were conducted in accordance with approved procedures, regulatory guides, and industry codes or standards, and in conformance with Technical t

Specifications.

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Maintenance NWR B 70342 - Limitorque Valve - Change grease to calcium base grease, Exxon Nebula EP0 NWR B 6881A - Rewire wide range temperature recorders or repair.

NWR B 68868 - 111 DC Bus - MCB Alarm NWR B 68969 - Investigate and repair DC ground on Bus 111.

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NWR B 69611 - Install new alarm horn or redirect / rotate existing alarm horn.

NWR B 69615 - Install new alarm horn or redirect / rotate existing alarm horn.

NWR B 69684 - U-Bolt on pipe hanger 1FW 01268R needs repair.

NWR B 69686 - Investigate unexplained trip of AC feed to charger 111.

NWR B 69746 - Investigate and repair high positive ground on DC l

Bus 211.

NWR B 70194 - Rod control urgent failure alarm.

NWP 3 70337 - Replace electro thermal link fire damper

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NWE s 70338 - Replace electro thermal link fire damper

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NWR B 70339 - Replace exhausted halon bottles for upper cable spreading room.

NWR B 70342 - Limitorque Valve - Change grease to calcium base grease Exxon Nebula EPO NWR B 70452 - Found 2 MEG ground on nVS-SX142.

NWR B 70526 - Investigate and repair DC ground on Bas 111.

Surveillance

" 1 BHS FP-18, " Semi-annual test of fire protection detection and suppression wire trouble alarm for cr oss logic zones. 1 PA39J cabinet."

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Surveillance

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  • 1 BOS DC-M1, "(Unit 1) 125V DC ESF battery III monthly

surveillance."

  • 1 BVS 0.5-3. AF.1-2, "ASME surveillance requirements for the diesel driven AFW pump and Train B AFW valves."
  • 1 BVS 1.1.3.b-1, " Moderator temperature coefficient at power -

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1 BOS 3.1.1-21, "(Unit 1) Train B solid state protection

system bi-monthly surveillance (staggered)."

  • 1 BOS 8.1.1.2.a-1, "1A Diesel Generator operability. monthly (staggerad) and semi-annual staggered.

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surveillance.

  • 2 BVS 0.5-3.AF.1-1, "ASME surveillance motor driver AFW Pump

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and train A AFW valves."

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The following items were considered during this review:

the limiting conditions for operation were met while affected components or systems were removed from and restored to seavice; approvals were obtained prior to initiating work or testing; quality control records were maintained; radiological and fire prevention controls

. were accomplished in accordance with approved procedures; test instrumentation was within its calibration interval; functional testi_ng and/or calibrations were performed prior to returning components' or systems to' service; test results. conformed with

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Technical Specifications and procedural requirements and were

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reviewed by personnel other than the individual directing the

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test; any deficiencies identified during the testing were properly documented, reviewed, and resolved by. appropriate management personnel. The following concern was identified:

The. inspectors reviewed the status of the process for verification of proper gr9ase in Limitorque gearcase operators for Motor Operated Valves (MOVs) used in Environmentally Qualified (EQ) applications.

In January of 1939 a System Materials Analysis Department (SMAD) report, M-5825-88, dated January 6,1989, reported on the results of tests performed on 25 grease samples submitted for analysis on November 22, 1988.

Of the 25 samples analyzed by SMAD, two had unsatisfactory results. Valve 15188040 was identified with mixed greases.

The ratio of mixed greases was 20:1, calcium based grease to lithium cased grease. NWR B 65783 was issued on March 13, 1989, c

to replace the unsatisfactory mixed grease, with Exxon Nebula

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EPO grease. This was completed in July 1989.

The other unsatisfactory test result involved valve 15I8814. The test results identified that the incorrect grease was in the MOV gearcase.

Instead of a calcium based grease, the gearcase contained a 11thiva based grease.

It does not appear that a Deviation Report (DVR) was generated as a result of these two unsatisfactory test results.

It also appears that the

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SMAD report, M-5825-88 was not distributed to the EQ

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Coordinator for information-or action as appropriate.

L On August 31, 1989, based on a visual inspection of three grease' samples taken from the gearcase on a EQ Limitorque actuator for valve 1 CC 9412 B, it appeared that the grease was not of the type that would be acceptable for use in EQ applications. The three samples were sent to SMAD for analysis

and DVR No. 6-1-89-110 was written.

Samples from eight

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other gearcases were also sent for analysis at the same time.

SMAD report M-4194-89, of September 8, 1989, reported that the eight additional valve grease samples were acceptable ratio; y

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however, the grease in valve actuater 1 CC 9412 B was primarily s

a lithium based grease instead of the required calcium based grease. NWR B70342 was issued to change the grease, to the correct calcium base grease, Exxon Nebula EPO.

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Based on the recent August 31, 1989, SMAD test results the licensee initiated action to test the grease in 100% of the accessible 90 valves used in safety related EQ applications for both units. Also the licensee initiated administrative i

action to ensure involvement of the EQ coordinator with SMAD test results. Approximately 40 of the 90 valves had been sarrpled at the ei.d of tiiis inspection period. This will

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remain an unresolved item pending the rer.ults of the current

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sample program. (454/89017 01(DRP); 455/89019-01(DRp)).

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Backloo

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The inspectors reviewed the licensee's backlog of non-outage corrective NWRs on hold for parts to assess the significance.

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The NWRs were evaluated for safety impact of the deferrals, r

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W NWRs on hold for parts. -The backlog of open corrective non-outage

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NWRs was 411. The inspectors reviewed a computer listing of NWRs

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and selected four for detailed review to assess if there was an

impact on operability of the affected comoonent/ system. The NWRs selected were:

NWR#

Date Problem L

B56238 06/1/88 Damper has bad oil leak B63540 12/21/88 Valve is binding not allowing proper l

stroke.

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B63895 01/9/88 Switch appears to have failed closed not allowing jacket water to flow through jacket.

B65419 03/2/89 Vertical directional vibration reads Hi during surveillance.

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Safety Assessment / Quality Verification (35502, 40500, 40704)

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Licensee Event Report (LER) Follow-up (90712 and 92700)

(Closed) LER (454/89007)): Through direct observation, discussions with licensee personnel, and review uf records, the following LER was reviewed to determine that the reportability requirements were fulfilled, immediate corrective action was accomplished, and corrective action to prevent recurrence had been accomplished in accordance with Technical Specifications.

LER No.

Tith Unit 1

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454/89007 Control. room ventilation alignment due to voltage transient caused by lightning, i

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Evaluation of Licensee Quality Assurance program Implementation (35502)

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The inspectors reviewed the licensee's corrective actions to

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findings identified by an external industry assessment organization i

to determine the effectiveness of the licensee's Quality Assurance

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Program.

h The licensee's corrective actions were timely and adequate in regards~to deficiencies noted in the maintenance departments; in heightening the awarer.ess of first line supervisors on good

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industrial safety practices through additional enhanced training and on monitoring the radiation exposure received while performing j

repetitive and routine jobs for ALARA considerations.

The inspectors attended a modification status meeting.

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attendance were memters frem Operating, Tech Staff, all three i

Maintenance departments, and QA; and each member actively I

participated. The status of each modification was readily made available; indicating adequate planning, proper interface and good communications between groups. The licensee had a conscientious effort underway to complete all routine activities in anticipation of the large upcoming manpower demand during the outage, i

The inspectors also reviewed LERs issued during the 1989 calendar

year and concluded that root causes were properly determined, adequate corrective actions were implemented, and no significant j

discernible trends wcre identified.

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Evaluation of Licensee Performance (35502)

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A review of site operations from January through August 1989, was

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I conducted to evaluate the performance of the licensee as it-may require adjustment of the NRC inspection plan. The review included operational events and trends indicated by monthly status reports.

No violations or deviations were identified.

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~ Radiological Environmental Monitoring Program (REMP) (IP 84750, IP S0721)

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In a review of the corporate and nuclear plant radiological environmental monitoring programs, the inspector noted several deficiencies in the

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Byron program. Although the Annuel Radiological Environmental Reports from 1985 through 1988 contained summaries of the results of analysis of j

all radiological environmental sam)1es, the reports did not include the actual results, as required by Tec1nical Specification (TS) 6.9.1.6.

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licensee representative agreed to correct this by adding the results to the reports. This failure to include the results is considered a violation of Technical Specifications (454/89017 02(DRSS); 455/89019-02(DRSS)).

The violation was assigned a Severity Level IV due to poor programmatic oversight of TS requirements by corporate and licensee management and

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the related deficiency noted below.

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'A 1988 Corporate QA audit (QAA 20-88-31, October 21-28,1988), identified that contrary to Technical Specification 4.12.3, the Interlaboratory rogram w6s not described in the Offsite Dose Calculation Comparison o

Manual (0DCM). Corporate representatives revised the generic section of the ODCM where it appears to satisfy the TS requirement, especially when combined with the details in the Annual Radiological Environmental Report.

One violation of NRC requirements was identified.

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EngineeringandTechnicalSupport(37700)

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On-Site Reviews The inspectors reviewed five On-Site Review (03R) that pertained to potentially degradable equipment or system configurations different from UFSAR requirements. The OSRs were reviewed for clarity,

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accuracy, and technical content. The five OSRs reviewed were:

89-194 Containment Floor Drain Instrument

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(IFR-RF008)89-203 AFW Battery Capacity 89-206 IB CV Pump Seal Replacement 89-207 RHR Bearing Life analysis89-209 Operation with Charging / Safety Injection mini-flow loop isolated The inspectors identified one concern with OSR 89-206 that pertained to a seal replacement for the 18 CV pump. The OSR stated that a ASME Pump Performance Test was not required as the work performed

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did not affect the pump performance reference values of inlet

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pressure, differential pressure or flow rate.

Since the work involved uncoupling the pump from the motor, the ASME reference

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value for vibration could have been affected.

The OSR did not identify the affect of the work on pump vibration. However, subsequent to the work, the licensee did perform a ASME Pump Performance Test to accurately evaluate future maintenance to be

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performed on the IB CV pump.

The inspectors emphasized, to the licensee, the need for OSRs to be technically accurate and address the salient points.

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Discrepancy Records / Degraded Equip.nent The inspectors reviewed DVR No.89-016, which was issued on August 15, 1989, that identified the AFW "B" battery bank capacity for the Unit I diesel driven AFW pump as 73%, based on the pqrformance of surveillance, IBVS AF-2.

The acceptance criteria in the surveillance procedure was 80%.

The DVR stated that the

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' battery was considered operable based on a letter from the licensee's

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Nuclear Engineering Department (NED). The inspectors reviewed the

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letter and the history of the Nickel Cadium (NiCa) ba+.teries utilized to start the Unit 1 diesel driven AFW pump. There are two banks of NiCa batteries (Bank A and Bank B), each capable of starting the diesel driven AFW pump. A selector switch on the local panel is positioned to either bank,. with Bank "A" selected on the odd months

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and Bank "B" on the even months.

The inspectors identified the following concerns:

(1) DVR No.89-016 referenced a letter for the basis of determining

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operability for the~"B" NiCa battery bank that was dated July 11, 1989.

fhe letter referenced a calculation, which was performed as a result uf a similar capacity test for the "A" NiCa battery

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bank. The capacity test on the

"A". battery bank was conducted

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in accordance with procedure S?P-89-037 on May 9, 1989.

The l-capacity of Bank "A" was determined to be 61% which was below l

the 80% acceptance criteria defined in SPP-89-037. The l

calculation by the NED, to determine the minimum battery I

capacity, was determined by the inspectors to be inadequate.

l The calculation concluded that the minimum capacity was 49%;

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however, the calculation did not use the correct duty cycle for

the battery. The inspectors determined that the duty cycle I

utilized in the calculation did not meet the duty cycle described in the Updated Final Safety Analysis Report (UFSAR).

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The duty cycle in the UFSAR was four cranks of the diesel with the diesel AFW pump starting on the fifth attempt. The licensee

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performed another calculation on August 29, 1989, with the

correct duty cycle. The revised minimum capacity of 58% did l

not affect the operability status of both banks of the Unit 1 AFW NiCa batteries. However, the licensee has issued NWRs to repir.ce both battery banks within one year. The original apacity test on May 9, 1989, for the "A" Bank was based on a two Sour discharge. Based on vendor recommendations, the L

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L4-l licensee conducted another discharge test of Bank "A" but

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i utilized a five hour discharge method on September 5,.1989.

The' vendor stated that a five hour discharge would be a more o

h representative test of battery capacity. The capacity of f

the "A" Bank was determined to be 72%, based on the five hour discharge test.

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(2) The evaluation of Bank "A" NiCa batteries discharge test results of May 9. 1989 by the station did not address all the salient issues to determine Bank "A" operability. The e

evaluation was conducted by the system engineer and was part

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of the SPP-89-037 package. The evaluation stated that

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operability of the batteries will be verified by' starting

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the diesel driven AFW pump with the NiCa. battery charger off

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during the monthly surveillances. The evaluation did not address if the NiCa batteries would meet the design criteric L'

(duty cycle) of the batteries described in' the UFSAR, which was-the batteries capable of cranking the AFW diesel four q

s times with the diesel starting the fifth time.

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(3) The review of the status of Unit 1 AFW Bank "A" battery after the discharge test on May 9,1989, was considered untimely based on the test being done May 9, 1989; the review of results on June 5,-1989, and the calculations to determine minimum capacity performed July 11, 1989.

In conclusion, the inspectors are concerned with the licensee's process of assessing degraded equipment.

The inspectors have identified where the licensee had performed timely and adequate assessments of degraded equipment such as for the containment flow drain measurement system on August 10, 1989.

However, inconsistencies have been noted by the inspectors that warrant an evaluation of the process used by the licensee. Since degraded or nonconforming equipment directly relates to safe plant operations, the effectiveness of the process for assessing degraded / nonconforming equipment is considered an Open Item (454/89017-03(DRP); 455/89019-03(DRP)).

No violations or deviations were identified.

8.

Unresolved Items I

Unresclved items are matters about which more information is required in order to ascertain whether they are acceptable items, violations, or

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deviations. An Unresolved item has been identified during the inspection

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and is discussed in paragraph 4.a.

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9.

Meetings I

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Management Meetings (30702)

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On September 7, 1989, J. M. Hinds, Chief, Reactor Projects Section l

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1A, and the NRC resident inspectors toured the Byron plant and on September 8,1989, met with licensee management to discuss plant performance and plant material condition.

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b.

Exit Interview (30703)

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The scope and findings of the inspection were reviewed with corporate representatives (Section 1) at the conclusion of the inspection

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en July 14, 1989.

Telephone discussions were held with corporate representative on August 30, 1989, and a licensee representative on

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September 1, 1989.

During the exit interviews, the inspector discussed the likely

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informational content of the inspection report with regard to documents or processes reviewed during the inspection.

Licensee representatives did not identify any such documents or processes as proprietary.

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The inspectors met with the licensee representatives denoted in

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Paragraph I at the conclusion of the inspection on September 29, 1989. The inspectors summarized the purpose and scope of the inspection and the findings. The inspectors also discussed the likely informational content of the inspection report, with regard to documents or processes reviewed by the inspectors during the inspection. The licensee did not identify any such documents or procedures as proprietary.

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