IR 05000438/1981007

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-438/81-07 & 50-439/81-07 on 810131-0228. Noncompliance Noted:Three Examples of Welding Performance, Violating Drawing Criteria,Identified in Mechanical Heating & Ventilation Sys
ML20003H237
Person / Time
Site: Bellefonte  Tennessee Valley Authority icon.png
Issue date: 03/18/1981
From: Quick D, Wilcox J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML110870763 List:
References
50-438-81-07, 50-438-81-7, 50-439-81-07, 50-439-81-7, NUDOCS 8105050387
Download: ML20003H237 (5)


Text

fmg e

UNITED STATES g

V 8'

NUCLEAR REGULATORY COMMISSION n

E REGION 11

"g

101 MARIETTA ST., N.W., SUITE 3100 ATLANTA, GEORGIA 30303

.....

Report Nos. 50-438/81-07 and 50-439/81-07 Licensee: Tennessee Valley Authority 500A Chestnut Street Chattanooga, TN 37401 Facility Name: Bellefonte Docket Nos. 50-438 and 50-439 License Nos. CPPR-122 and CPPR-123 Inspection at Be)

fonte Site near Scottsboro, Alabama h

S ? f/

Inspector: /

'

'

J( 0.' Wi l c5(, Jr., 4pior Resident Inspector

'Dat'e Signed Approved by:

3 /# //

D. Quii:k, S[ction Chief, Division of Resident Date Signed and Reactor Project Inspection SUMMARY Areas Inspected This routine, announced inspection involved 144 resident inspector-hours on site in the areas of construction surveillance, Quality Control Investigation Report (QCIR) review, nonconforming condition report (NCR) review, QA audits, radiation survey, minimum design wall thickness review, installation of mechanical heating ind ventilation system, and surveillance of pipe runs.

Results Of the eight areas inspected, no violations or deviations were identified in seven areas; one violation was found in one area (Violation - Failure to follow procedures when installing the mechanical heating and ventilation structures.)

h/6 50 S03 8 9

.

.

.

.

Cr DETAILS 1.

Persons Contacted

Licensee Employees

  • W. Dahnke, Project Manager
  • F. Gilbert, Construction Engineer
  • G. Blackburn, General Construction Superintendent
  • D. Freeman, Electrical Engineer. Supervisor
  • L. McCollun, Instrument Engineer Supervisor
  • T. Brothers, Hanger Engineer Supervisor
  • F. Moses, Mechanical Engineer Supervisor
  • J. Olyniec, Civil Engineer Supervisor
  • J. T. Walker, Assistant Construction Engineer L. Jackson, Assistant Construction Engineer
  • J. Barnes, QA Supervisor Other licensee employees contacted included 18 construction craftsmen, 6 technicians, 8 mechanics, 2 security force members and 12 office personnel.
  • Attended exit interview.

2.

Exit Interview The inspection scope and findings were summarized on February 27, 1981 with those persons indicated in Paragraph I above.

3.

Licensee Action on Previous Inspection Findings Not inspected.

4.

Unresolved Items Unresolved items are matters about which more information is required to determine whether they are acceptable or may involve noncompliance or deviations. New unresolved items identified during this inspection are discussed in paragraphs 8,10 and 11.

5.

Independent Inspection Effort - Construction Surve111an~ce The inspector spent most of his time in direct surveillance of hardware in the field which included the following areas:

(Unit 1 Reactor Building)

Witnessed portions of installing decay heat removal, feedwater, reactor building spray, main steam, component cooling water, spent fuel cooling, core flooding, and waste disposal piping; installing steam generator snubbers and bumpers; installing main steam and feedwater pipe whip restraints; performing surge line weld prep and fit-up; installing reactor coolant whip restraint caps and installing exposed conduit and supports.

-

-

.

.

-

- - -

- -

-_

- -.

-

.

.-

-

.

.-

-

-

.

.

e

.

(Unit 2 Reactor Building) Witnessed portions of installing and welding stainless steel sloped ceilings in sumps

'A' and 'B'; welding reactor cooling system piping; installing and welding stainless steel liner in refueling canal; installation of core flooding, de:ay heat removal, reactor building spray, waste disposal, component cooling water, and spent fuel cooling piping; installing steam generator snubbers and bumpers; installing reactor coolant pump case supports; installing cable trays and associated supports; installing exposed conduit and associated supports; and installing control rod drive cooling piping.

(Auxiliary Building) Witnessed portions of installing chemical additions and baron recovery, startup and recirculation, component cooling, feedwater, main steam, waste disposal, auxiliary steam, makeup and purification, spent fuel handling and reactor building spray piping; installing spent fuel cooling and decay heat removal hangers, piping and valves, installing the third and 4elghth spent fuel storage racks in Unit 2 spent fuel pool; installing cable trays and associated supports; installing exposed conduit and supports, installing control and essential air piping; and oullup and terminating cables.

(General)

Witnessed portions of sandblasting and applying protective coatings; installing fire protection piping system.

6.

Quality Control Investigation Reports (QCIR) Review The resident inspector reviewed the description, and recommended disposition of the following QCIR's:

QCIR No.

DATE TITLE 7552 2/18/81 Hydraulic Snubbers 7001 2/2/81 Fuel Handling Bridge Rails 7588 2/18/81 18 Gauge Shield /14-16 Gauge Terminals 7531 2/19/81 Weld #INB00105 7482 2/16/81 Control Assemply Door No violations or deviations were identified.

7.

Nonconforming Condition Report (NCR) Review The resident inspector reviewed the item description, nonconformance des-cription, recommended disposition and action required to prevent recurrence for the following NCR's:

NCR No.

DATE TITLE 1371 2/12/81 Surface Mounted Plate 1374 2/13/81 Door Latch Handles 1378 2/12/81 Sleeve Penetration X-46

'

No violations or deviations were identified.

l t

-

.

.

.

..

-

--

. =, =

._

- -

-

_-

..

_

-

<

.

.

a

8.

Audits The resident inspector reviewed the following Quality Assurance audits for

.

accuracy and completeness:

f AUDIT No.

TITLE No. OF DEFICIENCIES i

BN-G-81-01 Preparation, Review, and Control of

QC Procedures

BN-G-81-02 Drawing Control

Paragraph 9.c of the Quality Assurance Staff Procedure (QASP) 7.1, Rev. 6

" Auditing Construction Activities" states:

"The lead auditor immediately i

brings a deficiency to the attention of management having responsibility in the area audited to permit maximum time for the comprehension of the deficiency., determination and prompt implementation of corrective action.'

It has not been determined by the resident. inspector how this immediate notification to management has been implemented by the QA organization.

This item is identified as unresolved item 50-438/81-07-01 and 50-439/81-

-07-02 "Immediate notification of management to QA audit deficiencies". The

,

resident inspector has requested the QA organization to notify him how this immediate notification of management to the above audits was performed.

,

9.

Radiation Survey

'

!

The resident inspector performed a radiation survey of the Welding

.

Engineering Unit Non-destructive Examination Building on site and obtained I

readings around a gang box of 1 mR/hr in several areas adjacent to and on top of this box. The gang box contained Radium 192 pills used in gamma radiography. The NRC RII office was immediately notified of this condition.

,

,

i The appropriate State of Alabama health physics personnel were also notified. TVA site personnel immediately moved the contents of the gang. box to Radiography Building (TVA Dwg #40lN127-1 Rev 1) for storage.

No violations or deviations were identified.

i

!

'

10. Minimum Design Wall Thickness

-

The resident inspector reviewed the recommended disposition of NCR's 1131 and 1285. TVA En-Des approved the minimum design calculated wall thickness for an 8" - sch 120 feedwater spoolpiece to be.585" and for 2" - sch 40 reactor building spray piping to be.0248".

Section 3641.1 of ASME 1974 i

Code gives the minimum thickness of pipe wall calculation formulas.

l However, this formula incorporates a coefficient for corrosion and erosion.

l This corrosion and erosion would be introduced to the piping section over

[

the life of the plant. The resident inspector questioned En-Des approval

'

'

for using this minimum design ca.lculated wall thickness for new piping sections which have not been introduced to corrosion and erosion on a plant l

under construction. The resident inspector requested TVA En-Des to explain j

the use of the minimum design calculated wall thickness on new piping

!

I

-,. _.... - - -. -, _,, _ _...., _ _,. _..,. - - - -.. -........ _ _... _ _.... _, _...,,, -, _.., _,

, _. _

-_,_ _

.

-

,

.

,

a w

sections under construction activities. This is identified as unresolved item 50-438/81-07-03 " Design minimum wall thickness for pipe section".

11.

Surveillance of Pipe Runs During the surveillance of the common zone elevation 629 Auxiliary Building, the resident inspector identified a section of chemical addition and baron recovery piping supported by hanger 0NB-0017 which appears to be cold sprung. TVA's General Construction Specification G-43 paragraph 2.6, states in part that cold springing is not permitted unless specified on design drawings. The resident inspector requested TVA to evaluate the above noted condition to determine if the chemical addition and boron recovery piping is cold sprung in this area.

This is identified as unresolved item 50-438/81-07-02, " Cold Springing of Pipe Runs".

12.

Installation of Mechanical Heating and Ventilation System Between February 20-27, 1981, the resident inspector observed work being performed on the structural installation of the mechanical heating and ventilation system to Unit 2.

During this inspection, it was determined that several areas were being erected contrary to TVA approved procedures.

These areas consisted of the following:

a.

Faur welds were made on February 18, 1981, at elevation 686'6" (Detail J55-J55 of TVA 3AWO910-00-55 Rev 11) without any welds specified on the above drawing.

^

'

b.

Several welds were made on the mechanical heating and ventilation structure which did not coincide with the weld symbols identified on TVA drawing 3AWO910-00-55 Rev. 11.

'

c.

The welder was performing the welds without weld cards in the immediate

.

work area and four weld cards did not exist.

Conversation between the welder, foreman and resident inspector confirmed that the foreman had not given the missing four weld cards to the welder when the weld was being accomplished.

This is identified as violation 50-439/81-07-01 " Failure to follow procedures when installing the mechanical heating and ventilation structures".

.

,,.-.

_..,. -., - - - - ~, -..,.

.c..

- _ _

m,,

_..

m-.

- _,, _

,,

,,.m

,.-_ -, - _.., -. _. -,