IR 05000438/2004001

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IR 05000438-04-001, IR 05000439-04-001, on 07/07/2004 - 07/08/2004, Bellefonte Nuclear Plant, Units 1 & 2; Routine Layup Inspection
ML042110356
Person / Time
Site: Bellefonte  
Issue date: 07/29/2004
From: Cahill S
Reactor Projects Region 2 Branch 6
To: Singer K
Tennessee Valley Authority
References
Download: ML042110356 (11)


Text

July 29, 2004

SUBJECT:

BELLEFONTE NUCLEAR PLANT - NRC INSPECTION REPORT NOS.

50-438/04-01 AND 50-439/04-01

Dear Mr. Singer:

On July 8, 2004, the NRC completed an inspection at your Bellefonte Units 1 and 2 reactor facilities. The enclosed report documents the inspection results which were discussed on July 8, 2004, with Mr. M. Phillippe and other members of your staff.

The purpose of the inspection was to determine whether equipment preservation activities authorized by the construction permits were conducted safely and in accordance with NRC requirements. Specific areas examined during the inspection are identified in the report. Within these areas, the inspection consisted of selected examinations of procedures and representative records, interviews with personnel, and observation of layup equipment in operation.

Based on the results of this inspection, no findings of significance were identified.

TVA

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS).

ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Stephen J. Cahill, Chief Reactor Projects Branch 6 Division of Reactor Projects Docket Nos. 50-438, 50-439 License Nos. CPPR-122, CPPR-123

Enclosure:

NRC Inspection Report 50-438/04-01 AND 50-439/04-01 w/Attachment - Supplemental Information

REGION II==

Docket Nos:

50-438 and 50-439 License Nos:

CPPR-122 and CPPR-123 Report No:

50-438/04-01 and 50-439/04-01 Applicant:

Tennessee Valley Authority (TVA)

Facility:

Bellefonte Nuclear Plant, Units 1 & 2 Location:

Bellefonte Road Hollywood, AL 35752 Dates:

July 7 - 8, 2004 Inspectors:

W. C. Bearden, Senior Resident Inspector, Browns Ferry (Unit 1)

R. L. Monk, Resident Inspector, Browns Ferry Approved by:

S. J. Cahill, Chief Reactor Projects Branch 6 Division of Reactor Projects

Enclosure SUMMARY OF FINDINGS IR 05000438/2004-001, IR 05000439/2004-001; 7/-7/8/2004; Bellefonte Nuclear Plant, Units 1 & 2; Routine Layup Inspection.

This annual inspection was to review the layup and maintenance of plant systems and the review of various plant records. This was an announced routine inspection conducted by two visiting Resident Inspectors. Based on the results of this inspection no findings of significance were identified. The inspectors concluded that, overall, the applicants layup and preservation program had been effective.

Enclosure Report Details Summary of Plant Status Bellefonte Nuclear Plant (BLN) Units 1 and 2 remain in a deferred construction status as described in a July 14, 2000, Tennessee Valley Authority (TVA) letter to the NRC regarding confirmation of construction deferral status. The majority of piping systems remain in dry lay-up with the exception of fire protection-related systems, chiller and associated support systems, and those systems required to support operation of the Unit 1 emergency diesel generators which are used as needed to assist in meeting temporary electrical distribution system peak load demand.

1.0 Plant Walkdowns a.

Inspection Scope (92050)

The inspector toured selected portions of the turbine building, auxiliary building, Units 1 and 2 reactor buildings, and Units 1 and 2 diesel generator buildings to evaluate the lay-up and preservation condition of selected safety-related equipment. During these tours, the inspector observed the proper operation of installed dehumidifiers and checked various safety-related components. Proper housekeeping practices and other control measures were verified to be in place. Selected safety-related components were checked by the inspector for external condition and protective covering, where necessary. Electrical motors and generators checked by the inspector were verified to be warm, with either internal heaters or heat tape energized. The following specific components were inspected:

Component cooling 1A and 3A pumps and motors

Unit 1 Diesel generators (Dgs) 1A and 1B

Unit 1 High pressure injection (HPI) 1A, 2A, and 1B pumps and motors

Unit 1 Reactor building spray 1A and 1B pumps and motors

Unit 1 Decay heat removal 1A and 1B pumps and motors

Unit 1 Motor-driven auxiliary feed water (AFW) 1A and 1B pumps and motors

Unit 2 Decay heat removal 2A and 2B pumps and motors

Unit 2 HPI 2A and 1B pumps and motors

Unit 2 Reactor building spray 2A and 2B pumps and motors

Unit 2 Motor-driven AFW 2A and 2B pumps and motors

Unit 2 DGs 2A and 2B

Unit 1 Vital battery rooms b.

Observations and Findings The inspector noted that some battery cells were continuing to show signs of impending failure (cell structure was buckled) on the vital batteries. Most of the cells are approaching 30 years old and are well beyond their design life. Multiple cells had previously been jumpered out and evidence existed of frequent cleaning of the vital battery rooms due to the accumulation of acid-induced corrosion. The inspectors verified that battery condition was monitored daily during operator rounds and ventilation

Enclosure of the battery rooms was maintained. The inspector was informed that the applicant planned to dispose of the aged battery cells during Fiscal Year 2005 and to provide an alternate means of providing 125-VDC control power for switchgear.

Accumulated water was noted on the floor in the Unit 1 HPI Pump 3B room on elevation 590 in the Auxiliary Building. The inspectors notified the applicant who determined that the water had leaked from an air compressor undergoing maintenance on the 610 elevation. Service Request 2531 was issued to remove the water and divert the water coming from above.

The inspectors were unable to verify motor heat applied to the Unit 2 HPI pump 1A motor. This concern was discussed with the applicant and the associated system engineer verified that motor heat was energized for this component. The inspectors determined that motor heat had been energized prior to the inspection but the presence of metal temperature above ambient levels in the room was difficult to verify.

No findings of significance were identified.

2.0 Preventive Maintenance Program a.

Inspection Scope (92050)

The inspector reviewed the applicants Preventive Maintenance (PM) Program to determine adequacy of the program for maintaining systems in lay-up. Maintenance of the applicants layup and preservation program relies on performance of PMs.

Examples of PMs performed under this program include motor heat verification, shaft rotation, component external inspections, system lay-up valve lineups, and humidity checks. Specific PM requirements were specified in the BLN Maintenance Code Book, Rev. 94. Site personnel have performed approximately 12,000 to 15,000 scheduled PMs on an annual basis, depending on the schedule requirements. The inspector reviewed the results of the applicants program for verification of system dry lay-up by performance of drain valve checks and humidity checks. Verifications involved routinely opening drain valves at designated low points in each system to check for the presence of moisture. Humidity checks involved sampling system flow paths for relative humidity.

The inspector reviewed documentation associated with various PM requirements that were completed by site personnel during the period of July 2003 - June 2004, including a review of applicable portions of the BLN Maintenance Code Book which specified the PM requirements. The inspector also reviewed completed PM records to verify that the PM requirements had been satisfied and that actions had been initiated to address any discrepancies which were identified during performance of the PM. In addition, the inspector reviewed documentation for selected inspection intervals of the PM activities to verify that the frequencies were performed on schedule.

Enclosure The following PM records were reviewed:

Component PM Codes Work Performed 1ND-MPMP/EMOT-002-B, Decay Removal Pump and Motor 243, 533, 115, 160, 202 Rotate pump/motor shaft, lubricate.

Perform visual inspection of external/internal surfaces and clean as necessary. Verify motor heat 1NS-MPMP/EMOT-002-B, Reactor Building Spray Pump and Motor 116, 243, 160, 202 Rotate pump/motor shaft, lubricate.

Perform visual inspection of external/internal surfaces and clean as necessary. Verify motor heat 2NS-EMOT-002-B, Reactor Building Spray Motor 252 Insulation test 1EU-EBC-53-G/01, 125-V DC vital battery charger N/A Visual inspection, clean if required 1EU-EDP-53C/01, 125-V DC Distribution Panel N/A Visual inspection, clean if required 1CA-MPMP-003-Q, Auxiliary Feedwater Pump and Turbine 052 Oil sample 2CA-MPMP-003-Q, Auxiliary Feedwater Pump and Turbine 022 Internal visual inspection 1CA-MPMP/EMOT-002-B, Auxiliary Feedwater Pump and Motor 022, 243, 155, 201, 625, 115 Rotate pump/motor shaft, lubricate.

Perform visual inspection of external/internal surfaces and clean as necessary. Verify motor heat tape applied 1KC01-RHR-4.1.3.1, Component cooling system N/A Perform dry system reverification 1KE-EMOT-007-A, Nuclear Service Water Strainer Motor 1A1 243 Cleanliness inspection

Enclosure 1NB-MPMP/EMOT-007-A, Boric Acid Pump and Motor 1A 052, 014, 156, 243 Cleanliness inspection, lubricate and rotate, oil sample 1RT-MDSL-002-B/1, Emergency Diesel Generator 2B 051 Oil sample 2RG-MRCR-004-B, Unit 2 EDG Start Air Tank 176 Verify nitrogen blanket 5 - 10 psig 1NI-EPEN-027-B, Electrical Containment Penetration 177 Verify nitrogen pressure 15 psig 0WE-GRDWATER-08 N/A Verify temporary ground water control, check caulking, drain not obstructed 2KE-MH-2B1-2B13, ERCW Manholes NA Inspect for presence of water, pump dry if required 1NC-EMOT-008/2, Reactor Coolant Pump 1B2 030, 154 Check oil level and rotate b.

Observations and Findings No findings of significance were identified.

3.0 Exit Meeting Summary The inspectors presented the inspection results to Mr. M. Phillippe, Operations and Maintenance Manager, and other members of staff on July 8, 2004. The inspector asked the applicant whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified. The applicant acknowledged the findings presented.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment Attachment SUPPLEMENTAL INFORMATION PARTIAL LIST OF PERSONS CONTACTED Applicant Staff R. Brown, Nuclear Licensing R. Davis, System Engineer H. Fischer, System Engineer G. Lyle, System Engineer S. Patterson, System Engineer M. Phillippe, Operations and Maintenance Manager ITEMS OPENED AND CLOSED Opened None Closed None

LIST OF DOCUMENTS REVIEWED

TVA Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 13

Generic Letter 87-15, Policy Statement on Deferred Plants

TVA Memorandum dated July 1, 1988, transmitting Draft Quality Assurance Plan for Deferred Plants/Units

TVA Letter dated July 14, 2000, BLN Nuclear Plant Units 1 & 2 and Watts Bar Nuclear Plant Unit 2 - Confirmation of Construction Deferral Status

TVA Letter dated December 13, 1999, BLN Nuclear Plant - PM reductions for manpower leveling

BLN Engineering Requirements Specification Manual

BLN Maintenance Code Book, Revision 94

Site Specific Procedure (SSP) - 9.90, Preventative Maintenance for Long Term Lay-up, Revision 2