ENS 56861
ENS Event | |
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21:41 Nov 16, 2023 | |
Title | Essential Chiller Trains Inoperable |
Event Description | The following information was provided by the licensee via phone and email:
11/05/23, 2200 CST: Essential Chiller 'B' train and associated cascading equipment were declared INOPERABLE for planned maintenance. Unit 2 entered the Configuration Risk Management Program as required by Technical Specifications on 11/12/23 at 2200. 11/16/23, 1541: Essential Chiller 'C' train and associated cascading equipment were declared INOPERABLE due to an unexpected material condition causing the Essential Chiller to trip. The most limiting [Limiting Condition of Operability] LCO is 3.7.7, Action c. This condition resulted in the INOPERABILITY of two of the three safety trains required for the accident mitigating function including: High Head Safety Injection, Low Head Safety Injection, Containment Spray, Electrical Auxiliary Building HVAC, Control Room Envelope HVAC, Essential Chilled Water. This is an 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> reportable condition per 10CFR50.72(b)(3)(v)(D) because it could affect the ability to mitigate the consequences of an accident. A risk analysis was performed for the equipment INOPERABILITY and mitigating actions have been taken per site procedures. All 'A' train equipment remains operable. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The 'B' train Emergency Diesel Generator was also inoperable due to planned maintenance and continues to be inoperable. It was considered in the Configuration Risk Management Program and it was determined this condition could be maintained. LCO 3.7.7, Action c requires reactor shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. |
Where | |
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South Texas ![]() Texas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+-0.18 h-0.0075 days <br />-0.00107 weeks <br />-2.46564e-4 months <br />) | |
Opened: | Neil Rocha 21:30 Nov 16, 2023 |
NRC Officer: | Ian Howard |
Last Updated: | Nov 16, 2023 |
56861 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |