ENS 43280
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ENS Event | |
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14:08 Apr 5, 2007 | |
Title | Automatic Reactor Trip Caused by Spurious Safety Injection During Testing |
Event Description | At 09:08 am on 4/5/2007, during surveillance testing of Unit 2 Train A safeguards logic at power, a spurious Train A safety Injection (SI) actuation occurred resulting in reactor protection system (RPS) actuation. Train A SI was in "Test" at the time and should not have caused the RPS trip. The operating crew manually actuated Train B SI as required by emergency operating procedures. All automatic actions for a reactor trip and safety Injection occurred as required. Reactor Coolant System (RCS) pressure decreased below the shutoff head of the high head Emergency Core Cooling System (ECCS) pumps during the transient, resulting in momentary ECCS discharge to the RCS. SI has been terminated per emergency operating procedures.
Prairie Island Unit 2 has been stabilized in mode 3, at about 2235 psig and 547 degrees average RCS temperature. Decay heat Is currently being removed by auxiliary feedwater and secondary steam dump to the main condenser. The cause of the actuation signal is under investigation. All control rods fully inserted. No primary power operated relief valves or safety valves lifted. No steam generator safeties lifted. Safeguards buses are powered by offsite power. The Unit 2 Emergency Diesel Generators (EDG) started but did not load. Unit 1 Control Rod Drive Mechanism cooling isolated as designed in response to the actuation and has since been restored. Otherwise, Unit 1 was unaffected and remains in mode 1 at 100% power. The licensee notified the NRC Resident Inspector. The licensee will also be notifying the State, local and other Government agencies and will be issuing a press release. |
Where | |
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Prairie Island Minnesota (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-0.12 h-0.005 days <br />-7.142857e-4 weeks <br />-1.64376e-4 months <br />) | |
Opened: | Stephen Seilhymer 14:01 Apr 5, 2007 |
NRC Officer: | John Knoke |
Last Updated: | Apr 5, 2007 |
43280 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Prairie Island with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge | |
WEEKMONTHYEARENS 570032024-03-03T17:42:0003 March 2024 17:42:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Main Feedwater Pump Suction ENS 568032023-10-19T16:10:00019 October 2023 16:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 565432023-05-27T23:34:00027 May 2023 23:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Notification of Unusual Event Due to Multiple Fire Alarms in Containment Not Verified within 15 Minutes ENS 548592020-08-26T18:19:00026 August 2020 18:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Flux Rate ENS 516092015-12-17T19:18:00017 December 2015 19:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Fire Alarm in Containment Not Verified within 15 Minutes ENS 511362015-06-07T12:35:0007 June 2015 12:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Resulting from Turbine Trip on Low Oil Pressure ENS 511072015-06-01T03:20:0001 June 2015 03:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Trip of Condensate and Main Feedwater Pump ENS 509502015-04-03T11:52:0003 April 2015 11:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Main Feedwater Pump ENS 476832012-02-22T05:42:00022 February 2012 05:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Feedwater Heater Hi Hi Alarm ENS 470172011-07-01T20:52:0001 July 2011 20:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manual Trip Due to Electro-Hydraulic Control Fluid Leak on Turbine Stop Valve ENS 468302011-05-09T12:22:0009 May 2011 12:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Upon Turbine Trip Due to Main Generator Lockout ENS 459522010-05-25T08:14:00025 May 2010 08:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 458512010-04-17T03:37:00017 April 2010 03:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Turbine Trip ENS 450772009-05-18T18:05:00018 May 2009 18:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip/Reactor Trip Due to Condenser Vacuum ENS 446152008-10-30T19:17:00030 October 2008 19:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Manually Tripped Due to Failure in Rod Control System ENS 443772008-07-31T13:17:00031 July 2008 13:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip During Testing ENS 432802007-04-05T14:08:0005 April 2007 14:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip Caused by Spurious Safety Injection During Testing ENS 425042006-04-14T19:25:00014 April 2006 19:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Condensate Pump and Feedwater Pump Trip 2024-03-03T17:42:00 | |
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