ENS 50221
ENS Event | |
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16:07 Jun 23, 2014 | |
Title | Emergency Diesel Generator Auto Start Due to Degraded Bus Voltage Signal |
Event Description | At 1107 [CDT] on 6/23/14, Safeguards Bus 15 received a degraded voltage signal that resulted in the bus load shed and the automatic start of the D1 Emergency Diesel Generator (EDG). Bus 15 re-energized to normal voltage after the source breaker from D1 [EDG] automatically closed. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) for valid actuation of the D1 EDG.
The initiating condition appears to be a failure of the automatic voltage tap changer on the 10-Bank transformer which affected voltage to the normal offsite power supply to the 1R transformer and Safeguards Bus 15. Currently Bus 15 is powered from offsite via the CT-11 transformer and D1 [EDG] has been shutdown. When Bus 15 power supply was transferred from D1 [EDG] to CT-11 transformer, a lockout was received on D1 [EDG] due to reverse power. Unit 1 is in TS [Technical Specification] 3.8.1 Condition D for one path inoperable and one EDG inoperable. At no time during the event were the health and safety of the public challenged. The redundant AC power supply train (Bus 16 and D2 EDG) remained operable and Bus 16 remained powered from offsite power. The Senior Resident Inspector has been notified. TS 3.8.1 Condition D requires that the one inoperable offsite power path or the D1 EDG be returned to operable status by 2334 CDT or be in Mode 3 in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Unit 2 is not affected by this issue. |
Where | |
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Prairie Island ![]() Minnesota (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+0.92 h0.0383 days <br />0.00548 weeks <br />0.00126 months <br />) | |
Opened: | Brain Johnson 17:02 Jun 23, 2014 |
NRC Officer: | Jeff Rotton |
Last Updated: | Jun 23, 2014 |
50221 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 570032024-03-03T17:42:0003 March 2024 17:42:00
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