ENS 56220
ENS Event | |
---|---|
04:19 Nov 13, 2022 | |
Title | Automatic Reactor Scram |
Event Description | The following information was provided by the licensee email:
On November 12, 2022, at 2319 CST, an actuation of the reactor protection system (RPS) initiated a full scram. The plant was in Mode 2, reactor pressure was 149 pounds. The high pressure coolant injection (HPCI) injection valve, HPCI-MOV-MO19, opened and injected cold water into the reactor vessel while HPCI system testing was in progress. The cause is still under investigation. All control rods inserted. Plant is currently in Mode 3 and stable. All systems operated as designed with no Primary Containment Isolation System group isolations. This event is being reported under two event classifications: 50. 72(b)(2)(iv)(B) -- "Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. 50. 72(b)(3)(iv)(A) -- "Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. The NRC Resident has been informed. |
Where | |
---|---|
Cooper Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000298/LER-2022-003 Actuation of Reactor Protection System Initiates a Full Reactor Scram |
Time - Person (Reporting Time:+-0.3 h-0.0125 days <br />-0.00179 weeks <br />-4.1094e-4 months <br />) | |
Opened: | Scott Johnson 04:01 Nov 13, 2022 |
NRC Officer: | Lloyd Desotell |
Last Updated: | Nov 13, 2022 |
56220 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 56220\u003C/a\u003E - \u003Ca href=\"/Cooper\" title=\"Cooper\"\u003ECooper\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EAutomatic Reactor Scram\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 56220 - Cooper\n","link":"","lat":40.359658333333336,"lon":-95.65465277777778,"icon":"/w/images/7/79/Entergy_icon.png"}],"imageoverlays":null} | |
Cooper with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 562782022-12-17T05:51:00017 December 2022 05:51:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram ENS 562202022-11-13T04:19:00013 November 2022 04:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 561742022-10-22T17:58:00022 October 2022 17:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge ECCS Injection While Shutdown ENS 549762020-11-01T10:34:0001 November 2020 10:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to an Un-Isolable Leak on the Turbine High Pressure Fluid System ENS 522612016-09-25T06:03:00025 September 2016 06:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Group 1 Isolation Signal ENS 454892009-11-11T23:43:00011 November 2009 23:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram After a Turbine Hydraulic Fluid Leak ENS 454822009-11-07T01:30:0007 November 2009 01:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to an Unisolable Leak on the Turbine High Pressure Fluid System ENS 444022008-08-09T07:04:0009 August 2008 07:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Failure of Reheat Stop Valve to Open During Turbine Valve Testing ENS 433752007-05-19T07:12:00019 May 2007 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Control Rod Hcu Valve Bonnet Leak Into Reactor Building ENS 425942006-05-22T12:01:00022 May 2006 12:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram as a Mitigating Action Due to Lowering Service Air Pressure ENS 423752006-02-26T08:50:00026 February 2006 08:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Msr High Level ENS 420102005-09-23T05:40:00023 September 2005 05:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Degrading Main Condenser Vacuum ENS 416012005-04-15T09:36:00015 April 2005 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram and Specified System Actuations ENS 403622003-11-29T04:02:00029 November 2003 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to Low Reactor Water Level 2022-12-17T05:51:00 | |