ENS 44402
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ENS Event | |
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07:04 Aug 9, 2008 | |
Title | Manual Reactor Scram Due to Failure of Reheat Stop Valve to Open During Turbine Valve Testing |
Event Description | While performing main turbine reheat stop valve surveillance testing, Reheat Stop Valve 1RV 1A failed to reopen simultaneously with a Moisture Separator C high level alarm. Plant alarm response procedures require a reactor scram in this situation. Operating crew inserted a manual scram at 0204 CDT. Immediately after the scram, RPV level responded as expected and dropped below the Group 2 containment isolation setpoint. All rods inserted fully. RPV level is being controlled with RFP A and the startup valves. RPV pressure is being controlled on the bypass valves. The Group 2 isolation was complete with no anomalies.
This report is being submitted pursuant to 50.72(b)(2) for RPS actuation (4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> report) and 50.72(b)(3) for a valid Group 2 isolation (8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> report). The scram was characterized as uncomplicated. The lowest reactor vessel water level reached was - 20 inches. No safeties lifted during the transient and all systems functioned as required. The cause of the reheat stop valve failure to reopen is under investigation. The NRC Resident Inspector has been notified. |
Where | |
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Cooper Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000298/LER-2008-001 |
Time - Person (Reporting Time:+-1.67 h-0.0696 days <br />-0.00994 weeks <br />-0.00229 months <br />) | |
Opened: | Roy Giles 05:24 Aug 9, 2008 |
NRC Officer: | Bill Huffman |
Last Updated: | Aug 9, 2008 |
44402 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (69 %) |
After | Hot Shutdown (0 %) |
Cooper with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 562782022-12-17T05:51:00017 December 2022 05:51:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram ENS 562202022-11-13T04:19:00013 November 2022 04:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 561742022-10-22T17:58:00022 October 2022 17:58:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge ECCS Injection While Shutdown ENS 549762020-11-01T10:34:0001 November 2020 10:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to an Un-Isolable Leak on the Turbine High Pressure Fluid System ENS 522612016-09-25T06:03:00025 September 2016 06:03:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuation of Group 1 Isolation Signal ENS 454892009-11-11T23:43:00011 November 2009 23:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram After a Turbine Hydraulic Fluid Leak ENS 454822009-11-07T01:30:0007 November 2009 01:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to an Unisolable Leak on the Turbine High Pressure Fluid System ENS 444022008-08-09T07:04:0009 August 2008 07:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Failure of Reheat Stop Valve to Open During Turbine Valve Testing ENS 433752007-05-19T07:12:00019 May 2007 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Control Rod Hcu Valve Bonnet Leak Into Reactor Building ENS 425942006-05-22T12:01:00022 May 2006 12:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram as a Mitigating Action Due to Lowering Service Air Pressure ENS 423752006-02-26T08:50:00026 February 2006 08:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Msr High Level ENS 420102005-09-23T05:40:00023 September 2005 05:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Degrading Main Condenser Vacuum ENS 416012005-04-15T09:36:00015 April 2005 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram and Specified System Actuations ENS 403622003-11-29T04:02:00029 November 2003 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to Low Reactor Water Level 2022-12-17T05:51:00 | |
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