ENS 54976
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ENS Event | |
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10:34 Nov 1, 2020 | |
Title | Manual Reactor Trip Due to an Un-Isolable Leak on the Turbine High Pressure Fluid System |
Event Description | On November 1, 2020, at 0534 CST the reactor was manually scrammed due to an un-isolable leak on the Turbine High Pressure Fluid System. Initial power level when the leak was identified was 100 percent. Power was lowered commencing at 0525 in accordance with shutdown procedures. The Reactor Operator scrammed the reactor at 0534 from approximately 75 percent power. Following the scram, Reactor vessel water level lowered to approximately -20 inches on the Wide Range Instruments, and was subsequently recovered to normal post scram range (approximately 36 inches) using the Reactor Feedwater system. Group 2 Isolation occurred due to Reactor vessel level reaching the isolation setpoint (3 inches). The plant is stable in MODE 3 and proceeding to cold shutdown. The Main Condenser remained available throughout the evolution and condenser vacuum is currently being maintained by the Mechanical Vacuum Pumps. Pressure is being controlled using the steam line drains to the main condenser.
All control rods fully inserted and there were no complications. All systems responded as designed. The Turbine High Pressure Fluid System has been secured. This event is reportable under 10 CFR 50.72(b)(2)(iv)(B) due to RPS Actuation-Critical and 50.72(b)(3)(iv)(A) Valid Specified System Actuation. The licensee has notified the NRC Resident Inspector. |
Where | |
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Cooper Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1 h-0.0417 days <br />-0.00595 weeks <br />-0.00137 months <br />) | |
Opened: | James Dedic 09:34 Nov 1, 2020 |
NRC Officer: | Jeffrey Whited |
Last Updated: | Nov 1, 2020 |
54976 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (75 %) |
After | Hot Shutdown (0 %) |
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