ENS 54083
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ENS Event | |
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06:49 Apr 18, 2019 | |
Title | Invalid Actuation of a Unit 2 Containment Isolation Logic Due to a Blown Fuse |
Event Description | This 60-Day telephone notification is being made per the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of Limerick Generating Station Unit 2 containment isolation logic.
On April 18, 2019, while performing a relay replacement on the Division 2/4 Main Steam Line logic, a partial containment isolation occurred due to a blown fuse. The following systems had components that actuated due to the partial isolation: Reactor Water Clean-Up System Primary Containment Instrument Gas System Drywell Chilled Water System Reactor Enclosure Cooling Water System Core Spray System The Residual Heat Removal System received an isolation signal; however, the system remained in service because the isolation was defeated in accordance with plant procedures. This event resulted in partial Group 2A, 3, 7A, 8A, and 8B isolations. The systems successfully functioned per the plant design and plant configuration. The licensee notified the NRC Resident Inspector. |
Where | |
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Limerick ![]() Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+867.03 h36.126 days <br />5.161 weeks <br />1.188 months <br />) | |
Opened: | Richard Wagner 09:51 May 24, 2019 |
NRC Officer: | Jeffrey Whited |
Last Updated: | May 24, 2019 |
54083 - NRC Website
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WEEKMONTHYEARENS 564642023-02-16T12:05:00016 February 2023 12:05:00
[Table view]Other Unspec Reqmnt, 10 CFR 50.73(a)(1), Submit an LER 60 Day Notification for an Invalid Actuation of the Emergency Service Water System ENS 562832022-11-02T23:29:0002 November 2022 23:29:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Telephonic Notification - Invalid Specific System Actuation ENS 553452021-05-13T11:00:00013 May 2021 11:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Signal ENS 540832019-04-18T06:49:00018 April 2019 06:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of a Unit 2 Containment Isolation Logic Due to a Blown Fuse ENS 540142019-02-22T15:30:00022 February 2019 15:30:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of a Unit 1 Containment Isolation Logic Due to a Blown Fuse ENS 519522016-03-28T05:50:00028 March 2016 05:50:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Inboard Isolation Logic ENS 485752012-10-13T23:41:00013 October 2012 23:41:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Multiple System Actuations ENS 468832011-04-02T16:18:0002 April 2011 16:18:00 10 CFR 50.73(a)(1), Submit an LER Loss of Rps/Ups Power Supply ENS 459622010-04-03T01:56:0003 April 2010 01:56:00 10 CFR 50.73(a)(1), Submit an LER Overvoltage Condition Causes Reactor Protective System Actuation ENS 455182009-10-19T16:05:00019 October 2009 16:05:00 10 CFR 50.73(a)(1), Submit an LER Automatic Closure of Primary Containment Isolation Valves Due to Invalid Signal ENS 442602008-04-09T08:16:0009 April 2008 08:16:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Notification for Invalid Specified System Actuation ENS 433662007-03-19T06:20:00019 March 2007 06:20:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuations During Testing ENS 428302006-07-09T22:49:0009 July 2006 22:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the B Esw Pump ENS 425722006-03-14T21:40:00014 March 2006 21:40:00 10 CFR 50.73(a)(1), Submit an LER Inadvertant Core Spray Pump Actuation ENS 416672005-03-06T19:07:0006 March 2005 19:07:00 10 CFR 50.73(a)(1), Submit an LER Invalid Safety System Actuation During an Outage ENS 408952004-05-26T20:22:00026 May 2004 20:22:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Invalid Automatic Actuation Report: Containment Isoaltion Valves in More than One System 2023-02-16T12:05:00 | |
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