ENS 54014
ENS Event | |
---|---|
15:30 Feb 22, 2019 | |
Title | Invalid Actuation of a Unit 1 Containment Isolation Logic Due to a Blown Fuse |
Event Description | This 60-Day telephone notification is being made per the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of Limerick Generating Station Unit 1 containment isolation logic.
On February 22, 2019, while performing work on the 1C Main Seam Line Rad Monitor a partial containment isolation occurred due to a blown fuse. The blown fuse caused a single channel 'C' isolation signal for the Refueling Area Ventilation Exhaust High Radiation and the Reactor Enclosure Ventilation Exhaust-High Radiation logic. The following systems had components that actuated due to the partial isolation: - Plant Process Radiation Monitoring System - Nuclear Boiler System - Control Rod Drive Hydraulic System - Containment Atmospheric Control System - Primary Containment Instrument Gas System This event resulted in partial Group VIC and partial Group VIIIB isolations. All the components that would actuate on a single 'C' isolation signal responded as designed. The licensee notified the NRC Resident Inspector. |
Where | |
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Limerick Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1386.27 h57.761 days <br />8.252 weeks <br />1.899 months <br />) | |
Opened: | Richard Wagner 08:46 Apr 21, 2019 |
NRC Officer: | Jeffrey Whited |
Last Updated: | Apr 21, 2019 |
54014 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 564642023-02-16T12:05:00016 February 2023 12:05:00
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