ENS 52863
ENS Event | |
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21:17 Jul 17, 2017 | |
Title | Unusual Event Declared Due to Loss of Offsite Power |
Event Description | During a rain and lightning storm, plant operators observed arcing from the main transformer bus duct and notified the control room. The decision was made to trip the main generator which resulted in an automatic reactor trip. The plant entered EAL SU.1 as a result of the loss of offsite power for greater than fifteen minutes. Plant safety busses are being supplied by both emergency diesel generators while the licensee inspects the electrical system to determine any damage prior to bringing offsite power back into the facility. Offsite power is available to the facility. No offsite assistance was requested by the licensee.
During the trip, all rods inserted into the core. Decay heat is being removed via the atmospheric dump valves with emergency feedwater supplying the steam generators. The main steam isolation valves were manually closed to protect the main condenser. There were no safeties or relief valves that actuated during the plant transient. There is no known primary-to-secondary leakage. Reactor cooling is via natural circulation. All safety equipment is available for the safe shutdown of the plant. The licensee has notified the NRC Resident Inspector, Louisiana Department of Environmental Quality and the local Parish emergency management agencies. Notified DHS SWO, FEMA, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).
This notification is also made under 10 CFR 50.72(b)(3)(v)(D). This is a non-emergency notification from Waterford 3. On July 17, 2017 at 1606 CDT, the reactor automatically tripped due to a loss of Forced Circulation, which was the result of Loss of Offsite Power (LOOP) to the electrical (safety and non-safety) buses. Both 'A' and 'B' trains of Emergency Diesel Generators (EDGs) started as designed to reenergize the 'A' and 'B' safety buses. The LOOP caused a loss of feedwater pumps, resulting in an automatic actuation of the Emergency Feedwater (EFW) system. Prior to the reactor trip, at 1600 CDT, personnel noticed the isophase bus duct to main transformer 'B' glowing orange due to an unknown reason. Due to this, the main turbine was manually tripped at 1606 CDT. Following the turbine trip, the electrical (safety and non-safety) buses did not transfer to the startup transformers as expected due to an unknown reason. The plant entered the Emergency Operating Procedure for LOOP/Loss of Forced Circulation Recovery. At 1617 CDT, an Unusual Event was declared due to Initiating Condition (IC) SU1 - Loss of all offsite AC power to safety buses [greater than] 15 minutes. All safety systems responded as expected. The plant is currently in mode 3 and stable with the EDGs supplying both safety buses and with EFW feeding and maintaining both steam generators. Offsite power is in the process of being restored. The licensee has notified the NRC Resident Inspector, Louisiana Department of Environmental Quality and the local Parish emergency management agencies.
The licensee terminated the Notification of Unusual Event at 2056 CDT. The basis for terminating was that offsite power was restored to the safety busses. The licensee has notified Louisiana Department of Environmental Quality, St. John and St. Charles Parishes, Louisiana Homeland Security Emergency Preparedness, and will be notifying the NRC Resident Inspector. Notified IRD (Stapleton), NRR (King), R4DO (Hipschman), DHS SWO, FEMA, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).
This update is being reported under 10 CFR 50.72(b)(3)(v)(B). During the event discussed in EN 52863, at 1642 CDT [on July 17, 2017], Condensate Storage Pool (CSP) level lowered to less than 92% resulting in entry to Technical Specification (TS) 3.7.1.3. Level in the CSP was lowered due to feeding from both Steam Generators with EFW. Normal makeup to the CSP was temporarily unavailable due to the LOOP. Filling the CSP commenced at 1815 CDT [on July 17, 2017], and TS 3.7.1.3 was exited on July 18, 2017 at 0039 CDT. The licensee notified the NRC Resident Inspector. Notified R4DO (Hipschman).
Waterford 3 is retracting a follow up notification made on July 19, 2017 for EN 52863, concerning the loss of safety function associated with the Condensate Storage Pool (CSP) per 10 CFR 50.72(b)(3)(v)(B). The Condensate Storage Pool was performing its required safety function by providing inventory to the Emergency Feed Water pumps when the required Tech Spec level (T.S. 3.7.1.3) dropped below 92%. The Technical Specification was entered at 1624 [CDT] on July 17, 2017 and exited after filling at 0039 on July 18, 2017. The total allowed outage time allowed by Tech Spec 3.7.1.3 is 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> to be in Hot Shutdown if not restored. The Condensate Storage Pool level was restored to greater than 92% prior to exceeding the allowed outage time. Based on level being restored and the Condensate Storage Pool performing its required safety function, 10 CFR 50.72(b)(3)(v)(B) does not apply. Prior to the automatic reactor trip, Condensate Storage Pool level was greater than 92%. The NRC Resident Inspector has been notified of the retraction. Notified R4DO (Groom). |
Where | |
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Waterford ![]() Louisiana (NRC Region 4) | |
Reporting | |
Emergency class: | Unusual Event |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor | |
Time - Person (Reporting Time:+-3.67 h-0.153 days <br />-0.0218 weeks <br />-0.00503 months <br />) | |
Opened: | Mickey Folse 17:37 Jul 17, 2017 |
NRC Officer: | Howie Crouch |
Last Updated: | Sep 14, 2017 |
52863 - NRC Website
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Unit 3 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Waterford ![]() | |
WEEKMONTHYEARENS 571752024-06-16T17:33:00016 June 2024 17:33:00
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Shutdown the Reactor, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Loss of Offsite Power ENS 523212016-10-27T05:21:00027 October 2016 05:21:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Loss of Charging and Letdown Systems from the Reactor Coolant System ENS 514472015-10-04T04:07:0004 October 2015 04:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 513482015-08-26T12:40:00026 August 2015 12:40:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Both Emergency Diesel Generators Declared Inoperable ENS 511162015-06-03T22:05:0003 June 2015 22:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Main Feedwater Pump ENS 486872013-01-21T21:51:00021 January 2013 21:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Level ENS 454452009-10-19T14:44:00019 October 2009 14:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following Stuck Open Moisture Separator Heater Relief Valve ENS 444542008-09-01T04:00:0001 September 2008 04:00:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event Due to Hurricane Warning Onsite ENS 426362006-06-12T18:00:00012 June 2006 18:00:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor Manual Actions Determined Untimely for Fire Safe Shutdown ENS 421382005-11-12T02:34:00012 November 2005 02:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After Loss of All Condenser Circulating Water Pumps ENS 419542005-08-28T03:04:00028 August 2005 03:04:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Hurricane Warning ENS 410402004-09-14T21:04:00014 September 2004 21:04:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Hurricane Watch in St. Charles Parish 2024-06-16T17:33:00 | |