ENS 51368
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ENS Event | |
|---|---|
23:01 Sep 3, 2015 | |
| Title | High Pressure Coolant Injection (Hpci) Declared Inoperable |
| Event Description | At 1901 EDT on 9/3/2015, the Unit 2 HPCI system inboard steam supply valve isolated due to a high steam flow instrument failure. The inboard steam supply valve closed and isolated as expected. There were no indications of a steam leak. Drywell parameters and affected Reactor Enclosure rooms and piping areas were inspected with no indications of a steam leak. In addition, the steam leak detection system did not indicate any rising temperatures for any of the affected areas. The issue has caused Unit 2 HPCI to be declared inoperable and unavailable. Unit 2 has entered into a 14 day [Technical Specification] Limited Condition of Operation per T.S. 3.5.1.
The licensee notified the NRC Resident Inspector. |
| Where | |
|---|---|
| Limerick Pennsylvania (NRC Region 1) | |
| Reporting | |
| 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
| Time - Person (Reporting Time:+-0.95 h-0.0396 days <br />-0.00565 weeks <br />-0.0013 months <br />) | |
| Opened: | Mark Arnosky 22:04 Sep 3, 2015 |
| NRC Officer: | Jeff Rotton |
| Last Updated: | Sep 3, 2015 |
| 51368 - NRC Website
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Unit 2 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (100 %) |
| After | Power Operation (100 %) |
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