ENS 50891
ENS Event | |
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17:30 Mar 13, 2015 | |
Title | Low Pressure Coolant Injection Declared Inoperable |
Event Description | This condition is reported in accordance with 10 CFR 50.72(b)(3)(v). On 3/12/15, during surveillance testing on LPCI [Low Pressure Coolant Injection] Loop Select Instrumentation, a degraded component was discovered. At 1230 CDT on 3/13/15, LPCI was declared INOPERABLE in accordance with Technical Specification requirements. All remaining ECCS systems remain available and operable.
The NRC Resident Inspector has been informed.
At 0105 CDT on 3/14/15, the subject component has been replaced and retested with satisfactory results. LPCI INOPERABLE condition was exited at 0105 CDT and the LPCI System is OPERABLE. The licensee informed the NRC Resident Inspector. Notified R3DO (Orth).
The purpose of this notification is to retract a previous report made on 3/13/15 at 1859 EDT. Notification of the event to the NRC was initially made as a result of an event where Low Pressure Coolant Injection (LPCI) was declared inoperable due to the discovery of a degraded LPCI Loop Select timing relay. Subsequent to the initial report, NextEra Energy Duane Arnold (NextEra) has determined that the LPCI Loop Select timing relay was tested in a configuration that affected time delay measurements. This testing configuration was revised in 2012 following a modification to the LPCI Loop Select Logic, STP 3.3.5.1-29. The inadequate testing configuration adversely affected the time delay when the test equipment was installed. A revision to STP 3.3.5.1-29 was completed to resolve the inadequate testing configuration. Subsequent bench testing, performed to mimic plant installed configuration, of the affected relay, was completed. This testing demonstrated that the relay could be tested in a manner that provided acceptable results, and it has been concluded that the relay would have performed its required safety function up to when it was tested on 3/13/15. Therefore, this event is not considered a Safety System Functional Failure and is not reportable to the NRC as a Licensee Event Report (LER) per 10 CFR 50.73. The NRC Resident Inspector has been notified. Notified R3DO (Valos). |
Where | |
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Duane Arnold Iowa (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+1.48 h0.0617 days <br />0.00881 weeks <br />0.00203 months <br />) | |
Opened: | Terry Brandt 18:59 Mar 13, 2015 |
NRC Officer: | Daniel Mills |
Last Updated: | Apr 23, 2015 |
50891 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Duane Arnold with 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
WEEKMONTHYEARENS 528812017-08-01T14:34:0001 August 2017 14:34:00
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