ENS 50806
ENS Event | |
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18:40 Feb 10, 2015 | |
Title | Unanalyzed Condition in Station Blackout Implementation at Monticello |
Event Description | On February 10, 2015, at 1240 EST, Northern States Power-Minnesota (NSPM) determined that the Station Blackout (SBO) implementation at Monticello Nuclear Generating Plant (MNGP) was not consistent with the NRC Safety Evaluation (SE). Specifically, the High Pressure Coolant Injection (HPCI) system was not being utilized in a manner consistent with the NRC SE for SBO. Current battery calculations do not reflect a full complement of HPCI system equipment running for the duration (coping requirements) of the SBO event. The calculation assumed a manual action to remove the HPCI auxiliary oil pump from operating during an SBO event in order to preserve the station battery.
NSPM is reporting this as an Unanalyzed Condition pursuant to the requirements of 10 CFR 50.72(b)(3)(ii)(B). The health and safety of the public was not affected since no SBO event occurred. All station batteries and the HPCI system remain operable in accordance with the plant Technical Specifications. The NRC Resident Inspector was notified of the event.
An engineering analysis was performed updating the battery calculations for Station Blackout (SBO) implementation demonstrating the ability of the safety related station batteries to provide sufficient capacity and capability to ensure that the core is cooled and appropriate containment integrity is maintained in the event of the SBO for the specified four hours. Therefore, the battery calculation is analyzed and specifically the High Pressure Cooling Injection (HPCI) System is analyzed to run in automatic for the entire duration of the SBO event meeting the site licensing basis for SBO. The SBO procedure has been revised to incorporate HPCI running in automatic for the entire duration of the SBO event. The NRC Resident Inspector has been notified. Notified R3DO (Duncan) |
Where | |
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Monticello Minnesota (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
Time - Person (Reporting Time:+1.98 h0.0825 days <br />0.0118 weeks <br />0.00271 months <br />) | |
Opened: | Kirk Duea 20:39 Feb 10, 2015 |
NRC Officer: | Jeff Herrera |
Last Updated: | Apr 3, 2015 |
50806 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (95 %) |
After | Power Operation (95 %) |