ENS 48730
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ENS Event | |
---|---|
20:30 Feb 7, 2013 | |
Title | Unanalyzed Condition Due to Possible Run-Out of High Pressure Safety Injection Pump |
Event Description | Current design basis calculations indicate the high pressure safety injection (HPSI) pumps could potentially operate in a run-out condition under certain worst case design basis conditions. The calculated flow is beyond the pump curves. The HPSI pumps could operate in a run-out condition for an extended period following a design basis accident. The pump vendor indicates that long term operation in this condition could not be supported due to accelerated wear of pump internal components. This represents a reportable unanalyzed condition.
The NRC Resident Inspector has been notified. |
Where | |
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Fort Calhoun Nebraska (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
LER: | 05000285/LER-2013-003 |
Time - Person (Reporting Time:+-2.15 h-0.0896 days <br />-0.0128 weeks <br />-0.00295 months <br />) | |
Opened: | Tim Schulte 18:21 Feb 7, 2013 |
NRC Officer: | Bill Huffman |
Last Updated: | Feb 7, 2013 |
48730 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 522012016-08-25T20:23:00025 August 2016 20:23:00
[Table view]10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Involving Potential Tornado Missile Damage ENS 519172016-05-10T16:38:00010 May 2016 16:38:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Containment Cooling Water System Inoperable Due to Unanalyzed Condition ENS 514872015-10-21T18:50:00021 October 2015 18:50:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Pressurizer Heater Bank Potential Circuit Failure Vulnerability ENS 508002015-02-09T23:30:0009 February 2015 23:30:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Safety Injection Tank Level Results in an Unanalyzed Condition ENS 494782013-10-28T17:30:00028 October 2013 17:30:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Postulated Event Could Result in a Hot Short That Could Adversely Impact Safe Shutdown Equipment ENS 493782013-09-23T18:40:00023 September 2013 18:40:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition - Epoxy Floor Coatings Do Not Meet Design Basis Requirements in Two Rooms ENS 493242013-09-05T13:31:0005 September 2013 13:31:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Low Pressure Safety Injection Pump Run Out Condition ENS 491192013-06-14T16:00:00014 June 2013 16:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Invalid Conditions Discovered Due to Exclusion of Small Bore Piping from Analysis ENS 491122013-06-13T13:05:00013 June 2013 13:05:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition ENS 490502013-05-17T05:00:00017 May 2013 05:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Embedment Depth for Seismic Anchors Inadequate ENS 488062013-03-04T20:00:0004 March 2013 20:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Mechanical Seal Material Design ENS 487872013-02-27T02:12:00027 February 2013 02:12:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Relay Backing Plate Fasteners Discovered to Be at Less than Specified Torque ENS 487812013-02-24T23:00:00024 February 2013 23:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Inverters Potentially Inoperable During Emergency Diesel Generator Operation ENS 487302013-02-07T20:30:0007 February 2013 20:30:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Possible Run-Out of High Pressure Safety Injection Pump ENS 480942012-07-11T21:03:00011 July 2012 21:03:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Analysis of Internal Containment Support Beam Exceeds Load Combination Limit ENS 479922012-06-04T20:14:0004 June 2012 20:14:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Reactor Coolant System in a Degraded Condition Due to an Instrument Rack Seismic Design Issue ENS 479002012-05-04T15:00:0004 May 2012 15:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Containment Equipment Not Analyzed for Environmental Conditions of Record ENS 478922012-05-02T16:55:0002 May 2012 16:55:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Unanalyzed Condition with Containment Pressure Instruments ENS 478622012-04-25T14:00:00025 April 2012 14:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Conditions Resulting from a Non-Conservative Error in Calculations ENS 478842012-03-02T13:41:0002 March 2012 13:41:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Degradation of Reactor Containment Electrical Penetration Seals ENS 476582012-02-10T06:00:00010 February 2012 06:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition - Guidance Not Adequate to Mitigate a Design Basis Flood ENS 478482011-10-06T18:44:0006 October 2011 18:44:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Waste Disposal System Class One Seismic Support Inoperable ENS 470882011-07-22T13:30:00022 July 2011 13:30:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Fire Supression Pumps Inoperable ENS 469652011-06-16T17:30:00016 June 2011 17:30:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Additional Penetration Identified for Mitigation During Walkdown ENS 462972010-09-30T21:16:00030 September 2010 21:16:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Potential Flooding Via Condensate Drain Lines ENS 458282010-04-08T21:22:0008 April 2010 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Steam Generator Inlet Isolation Valve ENS 454672009-10-26T15:50:00026 October 2009 15:50:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Pressurizer and Feedwater Storage Tank Level Indications Do Not Meet Appendix R Requirements ENS 429432006-10-28T22:09:00028 October 2006 22:09:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition ENS 429022006-10-12T22:30:00012 October 2006 22:30:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Steam Generator Instrumentation Nonconformance ENS 428962006-10-10T20:00:00010 October 2006 20:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Containment Spray Valve Mispositioned 2016-08-25T20:23:00 | |
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