ENS 47514
From kanterella
Jump to navigation
Jump to search
ENS Event | |
---|---|
15:46 Dec 9, 2011 | |
Title | Unidentified Rcs Leakage Greater than 2 Gpm Increase within 24 Hours |
Event Description | At 0908 [EST] Nine Mile Point Unit 2 received alert alarms for containment monitoring particulate channels. These alarms were accompanied by a rise in drywell floor drain leakage and drywell pressure.
At 0915 [EST] Nine Mile Point Unit 2 entered technical specification action statement (TS 3.4.5 B) due to unidentified leakage rise of greater than 2 gpm within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. At 1046 [EST] the control room commenced power reduction for shutdown of the plant. Peak drywell pressure was approximately 0.16 psig and is lowering since the commencement of plant shutdown. Peak drywell floor drain leakage was approximately 3.7 gpm and is also lowering since the commencement of the plant shutdown. The cause of the rise in unidentified drywell leakage is unknown at this time. The licensee has notified the NRC Resident Inspector and the state. |
Where | |
---|---|
Nine Mile Point New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-2.02 h-0.0842 days <br />-0.012 weeks <br />-0.00277 months <br />) | |
Opened: | Greg Elkins 13:45 Dec 9, 2011 |
NRC Officer: | John Knoke |
Last Updated: | Dec 9, 2011 |
47514 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 47514\u003C/a\u003E - \u003Ca href=\"/Nine_Mile_Point\" title=\"Nine Mile Point\"\u003ENine Mile Point\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EUnidentified Rcs Leakage Greater than 2 Gpm Increase within 24 Hours\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 47514 - Nine Mile Point\n","link":"","lat":43.52021388888889,"lon":-76.40656388888888,"icon":"/w/images/b/be/Constellation_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (50 %) |
WEEKMONTHYEARENS 496772013-12-26T18:01:00026 December 2013 18:01:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Blown Fuse ENS 485902012-12-13T21:30:00013 December 2012 21:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Primary Containment System Declared Inoperable ENS 475142011-12-09T15:46:0009 December 2011 15:46:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unidentified Rcs Leakage Greater than 2 Gpm Increase within 24 Hours ENS 471292011-08-06T07:22:0006 August 2011 07:22:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unusual Event and Plant Shutdown Due to Drywell Unidentified Leakage Greater than 10 Gpm ENS 461442010-08-03T18:52:0003 August 2010 18:52:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 1 Entered a Tech Spec Required Shutdown After Declaring Edg 102 Inoperable ENS 446352008-11-07T01:27:0007 November 2008 01:27:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Required Due to Failed Surveillance Test ENS 432232007-03-08T19:50:0008 March 2007 19:50:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to a Degraded Seal in the "a" Reactor Recirculation Pump ENS 426302006-06-11T05:26:00011 June 2006 05:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to High Rcs Drywell Leakage ENS 409192004-08-03T23:30:0003 August 2004 23:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Initiated Due to Inoperable Emergency Ups Inverter ENS 407192004-05-02T06:17:0002 May 2004 06:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Manual Scram Due to Rising Torus Temperature Due to Stuck Open Erv ENS 405882004-03-15T15:30:00015 March 2004 15:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shutdown Required by Technical Specifications Due to Inoperable Isolation Instrumentation ENS 404362004-01-10T18:00:00010 January 2004 18:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Ts Required Shutdown at Nmp1 Due to Inoperable Msiv ENS 402322003-10-08T14:30:0008 October 2003 14:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Primary Coolant Boundary Leakage 2013-12-26T18:01:00 | |
Retrieved from "https://kanterella.com/w/index.php?title=ENS_47514&oldid=424187"