ENS 42630
ENS Event | |
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05:26 Jun 11, 2006 | |
Title | Technical Specification Shutdown Due to High Rcs Drywell Leakage |
Event Description | At 01:26 on 6/11/2006 Nine Mile Point Unit 1 experienced a rise in drywell leakage of 2 gallons per minute increase of unidentified leakage in a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period [placing the Unit in an LCO] per Technical Specification 3.2.5.a.2. Present Drywell leakage is 2.33 gpm.
A normal orderly shutdown commenced at 01:26, per Technical Specification 3.2.5.b, [to] place the reactor in cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Drywell leakage has trended up very slowly over the past several weeks. On 6/10/2006 the plant reduced power, deinerted the primary containment, [and] attempted to repair packing leak on VLV-32-194. [This valve is a 1 inch drain valve on recirculation pump #12]. Following attempts to repair [the] valve, [the] plant inerted the primary containment [and] raised power to approximately 45% while main condenser tube cleaning continued. Unidentified drywell leakage began rising at a faster rate beginning on 6/10/2006 at 17:55. Drywell leakage has stabilized at a little over 2 gpm. The TS shutdown is required because of the 2 gpm increase in leak rate over the last 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period. There are no other equipment operability concerns or TS LCOs that present a challenge to a normal safe plant shutdown. The licensee notified the NRC Resident Inspector. |
Where | |
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Nine Mile Point New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-1.58 h-0.0658 days <br />-0.0094 weeks <br />-0.00216 months <br />) | |
Opened: | Eric Kelsey 03:51 Jun 11, 2006 |
NRC Officer: | Bill Huffman |
Last Updated: | Jun 11, 2006 |
42630 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (45 %) |
After | Power Operation (25 %) |
WEEKMONTHYEARENS 496772013-12-26T18:01:00026 December 2013 18:01:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Blown Fuse ENS 485902012-12-13T21:30:00013 December 2012 21:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Primary Containment System Declared Inoperable ENS 475142011-12-09T15:46:0009 December 2011 15:46:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unidentified Rcs Leakage Greater than 2 Gpm Increase within 24 Hours ENS 471292011-08-06T07:22:0006 August 2011 07:22:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unusual Event and Plant Shutdown Due to Drywell Unidentified Leakage Greater than 10 Gpm ENS 461442010-08-03T18:52:0003 August 2010 18:52:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 1 Entered a Tech Spec Required Shutdown After Declaring Edg 102 Inoperable ENS 446352008-11-07T01:27:0007 November 2008 01:27:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Required Due to Failed Surveillance Test ENS 432232007-03-08T19:50:0008 March 2007 19:50:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to a Degraded Seal in the "a" Reactor Recirculation Pump ENS 426302006-06-11T05:26:00011 June 2006 05:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to High Rcs Drywell Leakage ENS 409192004-08-03T23:30:0003 August 2004 23:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Initiated Due to Inoperable Emergency Ups Inverter ENS 407192004-05-02T06:17:0002 May 2004 06:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Manual Scram Due to Rising Torus Temperature Due to Stuck Open Erv ENS 405882004-03-15T15:30:00015 March 2004 15:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shutdown Required by Technical Specifications Due to Inoperable Isolation Instrumentation ENS 404362004-01-10T18:00:00010 January 2004 18:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Ts Required Shutdown at Nmp1 Due to Inoperable Msiv ENS 402322003-10-08T14:30:0008 October 2003 14:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Primary Coolant Boundary Leakage 2013-12-26T18:01:00 | |