ENS 43179
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ENS Event | |
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00:15 Feb 22, 2007 | |
Title | |
Event Description | At 1915 on February 21, 2007, Crystal River Unit 3 was at reduced power (71%) for planned maintenance on one of four condenser waterboxes when the Integrated Control System (ICS) for Main Feedwater became erratic causing a feedwater transient that underfed the once thru steam generators. The reactor protection system (RPS) actuated on high Reactor Coolant System pressure causing a reactor trip. CR3 also received an Emergency Feedwater Actuation (EFIC) on low steam generator levels. This event is reportable as a 4-Hour Non-Emergency Notification per 10CFR50.72 (b)(2)(iv)(B) for Reactor Protection System Actuation and as an 8-Hour Non-Emergency Notification per 10CFR50.72 (b)(3)(iv)(A) for Emergency Feedwater Actuation and for Reactor Protection System actuation. All systems responded as designed and the plant remains stable with Emergency Feedwater in MODE 3.
The licensee informed the NRC Resident Inspector. |
Where | |
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Crystal River Florida (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000302/LER-2007-002 |
Time - Person (Reporting Time:+-2.07 h-0.0863 days <br />-0.0123 weeks <br />-0.00284 months <br />) | |
Opened: | Ricky E. Rawls 22:11 Feb 21, 2007 |
NRC Officer: | Steve Sandin |
Last Updated: | Feb 21, 2007 |
43179 - NRC Website
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Unit 3 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (71 %) |
After | Hot Standby (0 %) |
Crystal River with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 490862013-06-02T01:29:0002 June 2013 01:29:00
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