On 03/01/2008 a pre-planned unit shutdown was in progress to repair a
reactor coolant pump seal. At approximately 20% reactor power, a main
feedwater flow perturbation occurred. This flow perturbation resulted in an Emergency
Feedwater actuation at 0427 [EST]. Both
Emergency Feedwater system trains started automatically on low levels in the Once Through
Steam Generators as designed. Main
feedwater system recovered and continued to supply inventory with levels stabilized at the required low level setpoint. Following plant stabilization, Emergency
Feedwater was secured and the pre-planned unit shutdown was resumed. This event is reportable under the requirements of
10 CFR 50.72 (b)(3)(iv)(A).
The cause of the
feedwater flow perturbation is still under investigation. The licensee notified the NRC Resident Inspector.