ENS 42574
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ENS Event | |
---|---|
14:57 May 14, 2006 | |
Title | Emergency Diesel Generator Automatic Start |
Event Description | During restoration from a scheduled LCO, the Unit 1 EDG auto started when its control switch was placed in the auto position. The auto start occurred as a result of a 4KV Bus Feed Breaker being open. This breaker was in the open position as part of scheduled maintenance.
This notification is being made in accordance with 10CFR50.72(b)(3)(iv)(A) due to an actuation that was the result of a valid signal. The 4KV Bus was subsequently restored and the EDG was returned to standby. The licensee notified the NRC Resident Inspector. |
Where | |
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Quad Cities Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+1.93 h0.0804 days <br />0.0115 weeks <br />0.00264 months <br />) | |
Opened: | Eric Marks 16:53 May 14, 2006 |
NRC Officer: | Mike Ripley |
Last Updated: | May 14, 2006 |
42574 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (97 %) |
After | Power Operation (97 %) |
WEEKMONTHYEARENS 571412024-05-23T16:46:00023 May 2024 16:46:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Turbine Trip Signal ENS 570582024-03-28T01:46:00028 March 2024 01:46:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Reactor Protection System ENS 566762023-08-11T08:29:00011 August 2023 08:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 551462021-03-20T01:30:00020 March 2021 01:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Unit 1 Emergency Diesel Generator ENS 542392019-08-25T16:02:00025 August 2019 16:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Main Generator Ground Fault Relay ENS 536932018-10-24T05:00:00024 October 2018 05:00:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(iv)(A), System Actuation 1/2 Edg Auto Started and Lpci/Core Spray Inoperable Due to Loss of Safety Bus ENS 536262018-09-26T05:00:00026 September 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Generator Output Breaker Trip ENS 509492015-04-03T02:33:0003 April 2015 02:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Steam Leak ENS 499882014-04-02T18:40:0002 April 2014 18:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Alert Declared Due to Fire in Unit 2 Turbine Building ENS 478472012-04-18T20:11:00018 April 2012 20:11:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Two Automatic Reactor Scram on High Reactor Pressure ENS 469512011-06-13T10:10:00013 June 2011 10:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Steam Leak in Turbine Building ENS 461842010-08-17T19:14:00017 August 2010 19:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Initiated Due to Recirculation Pump Trip ENS 461692010-08-12T08:58:00012 August 2010 08:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Reactor Automatic Scram Due to Turbine Trip ENS 431982007-02-28T07:20:00028 February 2007 07:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Reactor Manually Scrammed Due to Decreasing Condenser Vacuum ENS 425742006-05-14T14:57:00014 May 2006 14:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Automatic Start ENS 423562006-02-22T07:22:00022 February 2006 07:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Valid Main Turbine Load Reject Signal ENS 417822005-06-17T16:20:00017 June 2005 16:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Ehc Malfunction 2024-05-23T16:46:00 | |
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