ENS 54239
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ENS Event | |
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16:02 Aug 25, 2019 | |
Title | Automatic Scram Due to Main Generator Ground Fault Relay |
Event Description | On August 25, 2019, at 1102 [CDT], Quad Cities Unit 1 experienced an automatic scram from 100 percent power. All rods fully inserted and there were no complications. The trip was initiated from a main generator ground fault relay. Troubleshooting of the fault is in progress. All systems responded as designed. There were no systems inoperable and no TS [Technical Specification] action statements were in progress prior to the Reactor Scram. Reactor water level dropped below the Group 2 and Group 3 Reactor Water Level Isolation set-points as expected, and recovered via the Feedwater system. Standby Gas Treatment System auto started and Reactor Building Ventilation Isolation occurred as expected. Unit 1 remains in Mode 3.
Decay heat is being removed using the steam bypass valves to the condenser and the safety relief valves did not lift as a result of the trip. This report is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. Unit 2 was not affected. |
Where | |
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Quad Cities Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.18 h-0.0075 days <br />-0.00107 weeks <br />-2.46564e-4 months <br />) | |
Opened: | Clifford Steiner 15:51 Aug 25, 2019 |
NRC Officer: | Ossy Font |
Last Updated: | Aug 25, 2019 |
54239 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Shutdown (0 %) |
Quad Cities with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 571412024-05-23T16:46:00023 May 2024 16:46:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Turbine Trip Signal ENS 570582024-03-28T01:46:00028 March 2024 01:46:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Reactor Protection System ENS 566762023-08-11T08:29:00011 August 2023 08:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 562102022-11-04T19:00:0004 November 2022 19:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Scram Due to Rising Water Level ENS 559752022-07-04T06:04:0004 July 2022 06:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Manual Scram Due to Lowering Reactor Water Level ENS 551462021-03-20T01:30:00020 March 2021 01:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Unit 1 Emergency Diesel Generator ENS 542392019-08-25T16:02:00025 August 2019 16:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Main Generator Ground Fault Relay ENS 536932018-10-24T05:00:00024 October 2018 05:00:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(iv)(A), System Actuation 1/2 Edg Auto Started and Lpci/Core Spray Inoperable Due to Loss of Safety Bus ENS 536262018-09-26T05:00:00026 September 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Generator Output Breaker Trip ENS 509492015-04-03T02:33:0003 April 2015 02:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Steam Leak ENS 499882014-04-02T18:40:0002 April 2014 18:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Alert Declared Due to Fire in Unit 2 Turbine Building ENS 478472012-04-18T20:11:00018 April 2012 20:11:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Two Automatic Reactor Scram on High Reactor Pressure ENS 469512011-06-13T10:10:00013 June 2011 10:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Steam Leak in Turbine Building ENS 461842010-08-17T19:14:00017 August 2010 19:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Initiated Due to Recirculation Pump Trip ENS 461692010-08-12T08:58:00012 August 2010 08:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Reactor Automatic Scram Due to Turbine Trip ENS 431982007-02-28T07:20:00028 February 2007 07:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Reactor Manually Scrammed Due to Decreasing Condenser Vacuum ENS 425742006-05-14T14:57:00014 May 2006 14:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Automatic Start ENS 423562006-02-22T07:22:00022 February 2006 07:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Valid Main Turbine Load Reject Signal ENS 417822005-06-17T16:20:00017 June 2005 16:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Ehc Malfunction ENS 406252004-03-30T13:40:00030 March 2004 13:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram During Turbine Thrust Bearing Wear Detector Testing 2024-05-23T16:46:00 | |
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