ENS 40612
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ENS Event | |
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04:30 Mar 27, 2004 | |
Title | Unanalyzed Condition Regarding Hhsi Flush Line Isolation Valve Leakage - |
Event Description | While performing a High Head Safety Injection (HHSI) Train-B inservice test, a Plant Operator noted leakage coming through HHSI Flush Line Isolation Valve #SI-0120B. This valve is located on a flush line coming from the discharge of the HHSI pump and directs water to the Safety Injection Pump room sump located within the Fuel Handling Building. The operator investigated and determined that the leakage was due to the valve not being fully seated. The Licensee has come to the conclusion that the estimated leakage through the valve exceeded the allowable value to remain in compliance with 10 CFR 50, Appendix A, GDC 19 limits for Control Room Envelope during the post LOCA Containment recirc phase of a large break LOCA. This condition resulted in an unanalyzed condition that significantly degraded plant safety requiring a notification to the NRC within eight hours per 10 CFR 50.72 (b) (3) ii. Subsequently, flush line valve #SI-0120B has been fully seated, and the leakage stopped. The licensee considers this valve to be operable.
The Licensee notified the NRC Resident Inspector. |
Where | |
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South Texas Texas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
Time - Person (Reporting Time:+-2.37 h-0.0988 days <br />-0.0141 weeks <br />-0.00325 months <br />) | |
Opened: | Steven Kaspar 02:08 Mar 27, 2004 |
NRC Officer: | Dick Jolliffe |
Last Updated: | Mar 27, 2004 |
40612 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
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