3F1286-11, Monthly Operating Rept for Nov 1986
| ML20211Q201 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 11/30/1986 |
| From: | Graham D, Eric Simpson FLORIDA POWER CORP. |
| To: | Taylor J NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| 3F1286-11, NUDOCS 8703030036 | |
| Download: ML20211Q201 (5) | |
Text
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I OPERATING DATA REPORT
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DOCKETNO.80-301 DAtt CDNPLSTED SY m
TELEPHONE 3802 OPERATING 5TATUS 4
- 1. Unit Neme:
Crystal River Unit 3 Notes
- 2. Reporting Portad.
11/1/s8 - 11/so/ss
- 3. Llosaaed Tlunnel Power (MWt):
2544
- 4. Neswpiste Rating (Crom MWe):
890
- f. Design Electrieel Rating (Net MWe):
825
- 6. Maximum Dependeble Cepecity (Csese MWe):
860
- 7. Mealmen Dependable Capacity (Not MWe):
821
- 8. If Changes Occur in Cepeelty Ratings (1: ems Nanber 3 Threagh 7) Since Last Repo'et. Give Renese NA
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- 9. Power Level Te Which Restricted. lf Any (Net MWe):
NA
- 10. Reasons For Restrictions. If Amy: NA This Meath Yr..to.Dete Cusselstive
- 11. Hoare la Reporting Period 720 8018 85200
- 12. Number Of Neurs Reester Wee Critieel 27p.2 3522.1 53523.1
- 13. Roseter Reserve Sheedown Houre 0
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0 1280.3
- 14. Heers Cemeester on Line 275.5 3497.7
_ 52588.5
- 18. UsH Ressree $heodown News
-- 0 0
___ 0
- 16. Gsees Thermal Basesy Generated (MWN) 5 7981931
-- 118460796 50072
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- 17. Geone Dessrisal taarty Geesseted (MWH) 189342 2750342
_ 40508844
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- 14. Not Electrieel Emergy Cemented (MWM) 178118 2810590
__ 3347017s
- 19. Unit Servise Faesar 38 3 %
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43.8 %
81.7 %
- 20. Unia Avegebery Fesser
_ 3 8.3%
43.8%
81.7 %
- 21. Unit Corneity Feeser (Using MDC Net) 30.1 %
39.7%
54.5 %
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- 22. Unit cepeelty Foster (Ushis DER Net) 30.0%
- 23. Unit Forced Oussee Rate 43.3 %
39.5%
S4.7%
55.1%
13.4 %
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- 24. 36medewee $cheduAnd Over Nest 4 Months (Type. Dese. and Dureeles ef Eachi:
None
- 25. If Shut Down At End Of Report Period. F eteisted Deee of Sertup.12/13/86
- 26. Units la Test Steens iPrior to Commereimi Operation):
Foreest Aehieved i
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III4III INITIAL CRITICALITY INITIAL ELECTRICITY
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COMMERCIAL OPERAT10N
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8703030036 861130 PDR ADOCK 05000302 R
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I uppgy seguyggpques age ym agggtygggg DOCKETNO. - W302 j
UNIT MAISE FLCRP-3 DATE - 32/2/88 RMY80GIEN 33/3s COGNI.ETED gy S. A. Ettmerart l
1ELEre00psE --- (9M)195-3802 l
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'Is f a 't Lksusse kai k
rawee & C esecesse 3*
.a i Evans ay p
c Acei.e s.,
p 38-27 astIM F
8.0 B
,5 NA liti VA LVE,X Plain Feedwater Pusep 2R was taken off-line to chmage the governor.
1 M-28 861111 P
9.9 A
5 NA RB CRDRVE Control rod autonsatically dropped lato core asw! reduced power.
i M-19 Mill!
S 234.1 A
I NA RB CRDRVE Took asalt off-line to replace a control rod stator and perforse additional preventative I
menintenance activities.
84-34 M1122 P
218.4 A
4 NA CJ IITEXCH Prianary coolant leak into the Niacteor Services Cooling Systene via a failiare la the "A" letdown cooler kept the plant Mf-line. Replacing the letdown cooter.
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2
'I F F.w.ed Asamen:
4 Enkhd 5 54emauled A Equipasses Fallmos(FM Estishit G. Inserei-sames B her Test s,,,eae,l f,or Psepasasium esi Desa C Itefestems g.gg,,,,,3 sc, Emers Sheets for Leiamew 3-asete Scram E*ess Recurs ILERIFde eNt'Rt s.
D-Regdae.ny Rewrkseen 4-Conteaued 01686 E eperas.= Teminsag a license Esamanaeine 5-a m ed te.d F-Adswasseessive Geperasaund Ereve(Emplain) 5 i s*Un HOsber(Earlekst Em I.5asme 5=v
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AYEn4cg D AILY UNIT POWER Lgygg ih? -
DOCKET NO, 50-302 UNIT FLCRP-3 DATE _12/3/$6 COMPL3TED BY
_D. Graham TELEPHONg (904) 795-3802 MONTH November 1986 DAY AVERAGE DAILYPOWER LEVEL DAY AYERAGE DAILY POWER LEVEL (MWe Net)
(HWeWet) 808 37 0
2 8II
~~
1g 0
3 805 19 0
4 813 20 0
g 812 21 0
g 765 22 0
(
314 23 0
g 300 24 0
i.
454 25 0
10 808 26 0
802 27 0
12 133 28 0
13 0
3 0
14 0
30 0
IS 0
38 0
16 0
INSTRUCTIONS On this format,1 se the average daily unit power levet in MWe Net for each day in the repumns the nearest whole mepwatt.
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MONTALY OPERATIONAL $UMMARY STATDGQfT ili.
DOCl3T NO. 50-302 UNIT FLCRP-3 DAfg 12/2/86 CONFLRTED BY 5. A. Stewart TELEPHONg (904) 795-3802 NONTE November.1986
SUMMARY
STATEMENT:
Crystal River Unit 3 was taken off-line on November 11,1986 to replace a defective control rod drive (CRD) stator. The plant remained off-line to replace both of the letdown coolers.
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DOCKET COPY w.g,,...;
0 0 A P Q m a t i c as December 10, 1986 3F1286-11 l
Mr. James M. Taylor, Of ractor Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Attn:
Document Contro1 Desk
~ ~ '" ~ Wa~s hi ng ton, DC 20555
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Subject:
Crystal Rfver Unf t 3 Docket No. 50-302 Operating License No. OPR-72 Monthly Operating Report
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Dear Str:
Attached are twelve (12) copies of the Crystal River Unit 3 November 1986 Monthly Operating Report.
Thase reports are submitted in accordance with Technical Specification 6.9.1.6 Sincerely, E. C. Simpson Director, Nuclear Operations Engineering and Licensing AEF/feb Attachments cert M xc:
Dr. J. Nelson Grace Regional Administrator, Region II office of Inspection & Enforcement U.S. Nuclear Regulatory Consnission 101 Marietta Street N.W., Sui te 2900
$p/'
I Atlanta, GA 30323 f
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CENERAL OFFICE: 32ci Thiny-founn street souin -
8.o. som 14o42
- St. PetersDurg, flonda 33733 ! _.(313) 884 5151 A MoMa Progreen Comuny
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