05000498/FIN-2010002-02
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Finding | |
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| Title | Inadueage Engineering Evaluation Causes an Inoperable Essential Chilled Water Train |
| Description | The inspectors reviewed a self-revealing noncited violation of Technical Specification 3.7.14 because the licensee had one independent loop of essential chilled water inoperable for longer than the allowed outage time of 7 days. Specifically, the licensee performed an inadequate engineering evaluation that failed to determine the effects of changing the operation of the essential cooling water system on the essential chillers and in turn the essential chilled water system. On July 9, 2009, essential chiller 22A tripped due to low oil pressure during the start up sequence. As a result, the corresponding essential chilled water train was declared inoperable. The licensees initial corrective action was to place idle time restrictions on all the essential chillers until corrective maintenance items could be performed. The licensee entered this event into the corrective action program as Condition Report 09-10502. The finding was more than minor because it was associated with the Mitigating Systems Cornerstone attribute of configuration control and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Using the Significance Determination Process Phase 1 worksheets from Inspection Manual Chapter 0609, the finding screened to a Phase 2 analysis because it resulted in the loss of the safety function of a single train for greater than its technical specification allowed outage time. A Region IV senior reactor analyst performed a Phase 2 significance determination and found that the finding was potentially greater than Green. The analyst performed a bounding Phase 3 significance determination and found the finding to be of very low safety significance. The dominant core damage sequences included: 1) steam line break outside of containment with a common cause failure of the other chillers, and 2) steam generator tube rupture with a common cause failure of the steam generator power operated relief valves. Remaining mitigation equipment that helped to limit the significance included the remaining functional chillers and the turbine driven auxiliary feedwater pump. In addition, this finding had human performance crosscutting aspects associated with resources in that the licensee did not ensure that procedures were adequate to maintain long term plant safety by maintaining design margins H.2(a)(Section 4OA3). |
| Site: | South Texas |
|---|---|
| Report | IR 05000498/2010002 Section 4OA3 |
| Date counted | Mar 31, 2010 (2010Q1) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71153 |
| Inspectors (proximate) | L Ricketson J Dixon B Tharakan C Graves D Stearns W Walker |
| CCA | H.6, Design Margins |
| INPO aspect | WP.2 |
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Finding - South Texas - IR 05000498/2010002 | |||||||||||||||||||||||||||||||||||
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Finding List (South Texas) @ 2010Q1
Self-Identified List (South Texas)
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