text
-.
l l
I M
=M Log # TXX-90338
)
L File f 10200 g
g Ref. # 50.73(a)(2)(iv) 2 filELECTRIC October 9, 1990 s
% litism J. Cahill, Jr.
farcutove i ur henient U. S. Nuclear Regulatory Commission i
Attn: Document Control Desk Washington, D. C.
20555 SUBJECT: COMANCHE PEAK STEAM ELECTRIC STATION DOCKET NO. 50-445 MANUAL OR AUTOMATIC ACTUATION OF ANY ENGINEERED SAFETY FEATURE t
LICENSEE EVENT REPORT 90-028 00 f
Gentlemen:
Enclosed is Licensee Event Report 90-028 00 for Comanche Peak Steam Electric Station Unit 1, " Automatic Reactor Trip Caused by Lightning Strike."
Sincerel,
j r
t
- fot, William J. Cahill, Jr.
DEN /daj Enclosure c - Mr. R. D. Martin, Region IV ResidentInspectors,CPSES(3)
I k
I t
l L
f s
, f'
(
I 6
F4 North Olive Street L B. 81 Dallas, Texas 75201 i
Enclosure to TXX 90338 N% f OHaf 364 U $ NsGLL AR htOJLATONY COWWi&&lON APPROVED OW8 NO. 3190 0104 E KPIRES. 4/3092 l
CSTlWA1ED BURDEN PE R RESPONSE TO COMPLY W'TH TH2 IWORMAfl0N 00LLEC110N REQUEST: 60.0 HRS. FORWARD COWWENTS REGARDNQ
)
'"" '" * * ' '"' "'C"'""
"E"""''"'N' LICENSEE EVENT REPORT (LER)
GRANCH (P 630), U.S. NUCLE AR REGAATORY COVWS$10N. WASHINGTON.
JC. 20655. AND TO THE PAPERWORK REDUCTION PROJECT (31500104) orFCE OF WANAGEMENT AND BMT. WASHINGTON.DC.P0503.
F.cwy h.no p)
Dock.t %,,te G)
Fati" 43' COMANCHE PEAK. UNIT 1 0151010101414 l 5 1 I or 1016 1.. s, AUTOMATIC RFACTOR TRIP CAUSED BY UGHTNING STRIKE o~,...,
n.#.. g, o...e,..,
vo,.n.,
' *"g"=
75$ l O I O I I
l 6c 'i.
b,.t" Wonin o.,
v.-
W-n.,
v, v,
019 0 18 90 910 01218 010 110 0l9 910 N/A 0151010101 1
I o,
i,..
~,.m,..,..
.,, o m <~.
,o,.
ie
,, i i,
" c'* t* >
1 rs om w.ome L
60nenam n r,(a)
V o** '
20 406(.JO)(ii) 60.30(4 0) 60.73(.HSM 73.7,(4 PC 406(ani)(i)
Y Ql}lg 60.3f44(2) 00.73ta)(htvi)
Oth., (bmo#y., Ah.t,.d b.4mm a,d in T.E,
0' j;-,
RC 406(s)D)(n,)
6an xam 6on.xe(vio(A)
Nm Fa"a =64) to.4at.xix4) 60.73(ana(v64(8) 60.73(axP)(d) r ane.,m,v, e,n tynimi,si Bfl ?ta)mfe!
1 4
s Lirene : can..d Fo, The LE R (1a l
N.,.
i n a. wo.
A, cm G.P McGEE SUPERVISOR. COMPLIANCE 8 l 117 8 l 917 l-l 5 I 41717 co,W,. o u,,. r., E-., c.,,.,.
r.u,. O o., T,. R
, n ai
,=
37 a;e a=;
son c
s,.-
co,oo.<
um.,
c.e s,.
co,w,.4 u.noi.,ao,,
W l
l l l l l l
<>i l
l l l l l l s s i
i l i I I l av l
l l l l l l h' "
$wtvl.,mnial R.pon Esp.cl.d 04)
E sp.ct.d M o'n D.y v.a, se
" " ')
v...,. E.- s-.
o..i l
l l
u,-ouo.no i.-...no
,.. n.,W.,,-..., W,
) n.)
At 1428 on September 8,1990, Comanche Peak Steam Electric Station Unit 1 was automatically tripped from 38 percent power. A lightning strike is believed to have caused a surge in the input power resulting in the de energization of power supplies in the rod drive system, causing the rods controlled by one rod control cabinet to drop into the core. This resulted in the reactor trip from high negative flux rate.
No specific component or system failures were identified as the cause of this event. The inst @ation of surgo suppressors in the input supply to rod drive power supplies will provide additione! assurance that power supplies remain available during lightning strikes.
l l
L
. ~ ~ _.,
-. ~ _.
..... - ~. - -...__
i Enclosure to TXX 90338 hac FORy 3ech U.S. NurAL AR HLGVLA10HY COWW4 SON W MDNSE3W W ESTIMATED BURDEN PER RES CouPLY WITH TH4 PFORMATON LICENSEE EVENT REPORT (LER) gg,'j",LT8';,'*lQ'ggy,*g7,*gggg, TEXT CONTINUATION
'f g f,$'gy,*/p g,","# 7,% g
a OrFCE OF WANAGEMENT AND BUDGET, WASHINGTON, DC. 2LV03.
Iaceay Name(t)
Opaket Nuevtser 9)
LL A 88W'stier 30)
Page(3)
Year g
gue isp g---.
0l2l8 COMANCHE PEAK - UNIT 1 015101010l414l5 910 010 012 OF 016 n..n...
. no..
.. w o.A w i) j i
l.
DESCRIPTION OF THE REPORTABLE EVENT
A.
PLANT OPERATING CONDITIONS PRIOR TO THE EVENT On September 8,1990 at 1428, Comanche Peak Steam Electric Station (CPSES)
Unit 1 was in Mode 1, Power Operation, operating at 38 percent power.
B.
REPORTABLE EVENT CLASSIFICATION
An event or condition that resulted in an automatic actuation of any Engineered Safety Feature (ESF), including the Reactor Protection System (RPS)(Ells:(JC)).
C.
STATUS OF STRUCTURES. SYSTEMS. OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT Not applicable - no structures, systems or components were inoperable at the start of the event that contributed to the event.
l D.
NARRATIVE
SUMMARY OF THE EVENT. INCLUDING DATES AND APPROXIMATE TIMES On September 8,1990, during a lightning storm, two out of ten 25 Voltage Direct Current (VDC) power supply overvoltage protection circuits actuated (located in the rod drive (Ells:(AA)) power cabinets). This actuation resulted in loss of control power to the rod drive system and allowed the rods controlled by the two 25 VDC power supplies to fallinto the core. The dropped control rods actuated the Nuclear --
Instrumentation System (Ells:(JC)) power range high negative neutron flux rate reactor trip. All safety systems responded as expected.
6 0
)
Enclosure to TXX 90338
.x o,w.
u.um An atouuroav co.unoN
,,,,,o EsinAATED DURDEN PER RElp0NSE TO COMPLY WITH TH4 INFORMATON LICENSEE EVENT REPORT (LER)
"'l,'%,1%',';,'*l"fgg,% gf,'jff,@,
3 l
TEXT CONTINUATION
'Of,*,g,y,3E,1%^$LC,'OcQ7,%
OFFCE OF MANAGEMENT AND BJDOCT, WASHINGTON. DC.20503.
LER Nontier Sp Pap (h Facsey wme p) m wnourg) v-a T a.
. c2 Ol218 COMANCHE PEAK - UNIT 1 015l0l010141415 910 0I0 013 OF 016 i..m,,,,e
. _,... v orm w., O n An event or condition that results in an automatic actuation of any ESF, including the RPS is reportable within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> under 10CFR50.72(b)(2)(ll). At approximately 1618 on September 8,1990, the Nuclear Regulatory Commission Operations Center was notified of the event via the Emergency Notification System. The plant was stable in Mode 3, Hot Standby.
E.
THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE OR PROCEDURAL ERROR The overvoltage protection for the 25 VDC rod drive power supplies was found tripped upon investigation of a non urgent alarm on rod drive control cabinet 2AC received at the time of the trip.
II.
COMPONENT OR SYSTEM FAILURES A.
FAILURE MODE. MECHANISM. AND EFFECT OF EACH FAILED COMPONENT Not applicable - no failed components have been identified.
B.
Qd)fE OF EACH COMPONENT OR SYSTEM FAILURE Not applicable - no component or system failures have been identified.
C.
SYSTEMS OR SECONDARY FUNCTIONS THAT WERE AFFECTED BY FAILURE OF COMPONENTS WITH MULTIPLE FUNCTIONS Not applicable - there were no failed components with multiple functions that affected this event.
Enclosute to TXX 90338 N4C FORW 366A U.S. NUCLE AR REGULATORY COMWi& BON APPROVED OWS NO. 31to.0104 i
ESTlWATED BURDEN PER RES T COMPLY WITH THS NFORWATON LICENSEE EVENT REPORT (LER)
- y,C * ", $,,';,'y "ff g g,*, M,' f,o g m TEXT CONTINUATION
""^""N"*"**^""'**'"'*""****"**"-
3C. #0555. AND TO THE PAPERWORK REDUCil0N P8to. LECT (3120104)-
OFFICE OF WANAGEWENT AND SUDGET. WASHINGTON. DC.30601 Facan Name op h Nons.or (2)
LE R Nunter (6)
Page(h v-q Te as e 0l2l8 COMANCHE PEAK UNIT 1 0l5101010141415 910 010 014 OF 0l 6 i. e.or..-...
. -.=64.,on D.
FAILED COMPONENT INFORMATION
Not applicable - no failed components have been identified.
1 Ill.
ANALYSIS OF THE EVENT
A.
SAFETY SYSTEM RESPONSES THAT OCCURRED The Reactor Protection System (Ells:(JC)) and Auxiliary Feedwater System (Ells:(BA)) actuated during the event; all associated components within these systems functioned as designed.
B.
DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY Not applicable - there were no safety systems which were rendered inoperable due to a failure.
C.
SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT The event consisted of a multiple control rod drop resulting in a reactor trip. This is bounded by FSAR, Section 15.4.3 and concludes that the successful automatic actua ion of the reactor trip will ensure there is no reduction in the margin to core thermallimits and that the Departure from Nucleate Boiling design basis is met.
Consequently, there were no adverse impacts to plant safety or the health and safety of the public.
i l
l
_ - ~ -
Enclosute to TXX 90338 NPUQlW 3664 U.b. N4LE AR HLOMIORY COMW46 EON AF' PROVED OMG NO. 91040t04 E811 MATED BURDEN PER RES T 00MPLY WITH THIS NFORMATON LICENSEE EVENT REPORT (LER)
" 'l,'" " 8';y*l"ffg y,*"D g g,*g g,
3 TEXT CONTINUATION
- ^" " N"'. us MAR mAm oo. son. WA HuotoN 3C. 30665. AND TO THE PAPERWORK REDUCTON PROJECT (31640104)
OFFICE OF WANAGEMENT AND DUDGET. WASHINGTON, DC 30603.
,., s.
m m. e, a a ~~ =
rm v.-
ai n-me 0I2l8 COMANCHE PEAK
, UNIT 1 0151010101414 l 5 910 010 015 OF 0l6 1 i u e,..
o. snc e m 3%A.,iir, i
IV. CAUSE OF THE EVENT
ROOT CAUSE The initiating cause of this event is a lightning strike on the containment causing a surge in the 120 Voltage Alternating Current (VAC) input power creating a voltage surge in the 25 VDC output of the rod control power supplies. This surge actuated the overvoltage protection circuit on two 25 VDC power supplies which isolated the output of the supply.
The loss of this output voltage to the rod control system caused the rods controlled by the affected power supplies to fall.
V.
CORRECTIVE ACTIONS
A.
IMMEDIATE The Operator responded appropriately to the RPS actuation. Plant Emergency Operating Procedures were implemented and the plant was stabilized in Mode 3.
B.
CORRECTIVE ACTIONS TO PREVENT RECURRENCE The rod control power supplies tripped from the surge on the 120 VAC input. To prevent this, a design modification to install surge suppressors on the 120 VAC lines feeding for the system has been submitted. The installation of this modification will minimize the potential for an overvoltage trip of the 25 VDC power supplies from a lightning induced surge.
t Enclosute to TXX 90338 N4C IO4,W 3e6A U S NUCLE AR REOULATORY COMWSSON APPR0WD Out W. seps a
ESTIMATED BURDEN PER RES 00MpLY WrTH TH18 PFORMATON LICENSEE EVENT REPORT (LER)
"' " " 8
GURDEN ESTiWATE TO THE RECCRDS AND REPORT 8 WANAGEWENT TEXT CONTINUATION
- 30. 30655. AND TO THE PAPERWORK REDUCTON PROJECT (3120104)
OFFCE OF WANAGEMENT AND DUDGET. WASHINGTON DC.30001 6 acany Na,e (1)
W Nur%er (2)
LE R Nunter (6)
Peps (3)
V oet jg peoantei 1_ -_.
COMANCHE PEAK - UNIT 1 01510101014 l 4 l 5 910 0l2l8 010 016 OF 016 u.n.,~.
. -.... w - uA.wn i
VI.
PREVIOUS SIMllAR EVENTS Although there have been previous events that resulted in RPS actuation, the root cause of those events were unrelated to the root cause of this event. The corrective actions taken to resolve the root causes of the previous events would not have prevented this event. Therefore, no previous similar events have been reported pursuant to 10CFR50.73.
Vll. ADDITIONAL INFORMATION The times listed in the report are approximate and Central Daylight Savings Time (CDT).
l j
j ll A
._ a
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000445/LER-1990-001, :on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to Withdrawal |
- on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to Withdrawal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-003, :on 900305,both Source Range Flux Doubling Actuation Signals Not Restored to Normal Configuration from Test Configuration.Caused by Personnel Error Due to Not Recognizing That Block Permissives Illuminated |
- on 900305,both Source Range Flux Doubling Actuation Signals Not Restored to Normal Configuration from Test Configuration.Caused by Personnel Error Due to Not Recognizing That Block Permissives Illuminated
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-004, :on 900312,ESF Actuation Occurred,Resulting in Initiation of Train a Safety Injection W/Flow to Rcs.Caused by Failed Diode on Safeguards Driver Board.Station Procedures Revised |
- on 900312,ESF Actuation Occurred,Resulting in Initiation of Train a Safety Injection W/Flow to Rcs.Caused by Failed Diode on Safeguards Driver Board.Station Procedures Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-005, :on 900327,discovered That Insp to Ensure No Loose Debris Could Be Transported to Containment Sumps During LOCA Not Performed.Caused by Inadequate Procedural Requirements.Administrative Controls Improved |
- on 900327,discovered That Insp to Ensure No Loose Debris Could Be Transported to Containment Sumps During LOCA Not Performed.Caused by Inadequate Procedural Requirements.Administrative Controls Improved
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-006, :on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures Changed |
- on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures Changed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-007, :on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation Monitor |
- on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation Monitor
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-008, :on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure Revised |
- on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure Revised
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-009, :on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control Boards |
- on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control Boards
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-010, :on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved Counseled |
- on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved Counseled
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-011, :on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve Locked |
- on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve Locked
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-012, :on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure Revised |
- on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure Revised
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-013, :on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review Performed |
- on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-014, :on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order Issued |
- on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order Issued
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-015, :on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample |
- on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-016, :on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of Calibr |
- on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of Calibr
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000445/LER-1990-017, :on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil Replaced |
- on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-019, :on 900726,source Range Flux Doubling Actuation Occurred Due to Spurious Source Range Signal Decrease.Cause Not Identified.Operation & Troubleshooting of Channel SR N32 Observed Indicating Correct Functioning |
- on 900726,source Range Flux Doubling Actuation Occurred Due to Spurious Source Range Signal Decrease.Cause Not Identified.Operation & Troubleshooting of Channel SR N32 Observed Indicating Correct Functioning
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-020, :on 900726,safety Injection Actuation Occurred. Caused by Sequencing Error While Hanging Clearance on Msivs. Corrective Actions Include Program Enhancements & Training |
- on 900726,safety Injection Actuation Occurred. Caused by Sequencing Error While Hanging Clearance on Msivs. Corrective Actions Include Program Enhancements & Training
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-021, :on 900730,safety Injection Actuation Occurred from Rate Compensated Low Steam Line Pressure Actuation Logic.Caused by Accumulation of Water in Main Steam Line. Procedures Will Be Enhanced & Revised |
- on 900730,safety Injection Actuation Occurred from Rate Compensated Low Steam Line Pressure Actuation Logic.Caused by Accumulation of Water in Main Steam Line. Procedures Will Be Enhanced & Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-022, :on 900807,realized That Pressurizer Heatup Limit Exceeded Due to Failure to Comply W/Tech Spec Action Statement Following 900726 & 30 Events.Caused by Inadequate post-trip Review.Procedures & Training Revised |
- on 900807,realized That Pressurizer Heatup Limit Exceeded Due to Failure to Comply W/Tech Spec Action Statement Following 900726 & 30 Events.Caused by Inadequate post-trip Review.Procedures & Training Revised
| 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-023, :on 900808,reactor Tripped on Loss of Feedwater Flow.Caused by Loose Fuse in Main Feedwater Control Power Circuit.Corrective Maint Performed on Malfunctioning Fuse Clip |
- on 900808,reactor Tripped on Loss of Feedwater Flow.Caused by Loose Fuse in Main Feedwater Control Power Circuit.Corrective Maint Performed on Malfunctioning Fuse Clip
| 10 CFR 50.73(a)(2) | | 05000445/LER-1990-025, :on 900825,reactor Trip Occurred.Caused by Feedwater Flow Control Valve Linkage Arm from Valve Stem to Valve Positioner Separating Due to Flow Induced Oscillations.Lock Washer Installed on Arm |
- on 900825,reactor Trip Occurred.Caused by Feedwater Flow Control Valve Linkage Arm from Valve Stem to Valve Positioner Separating Due to Flow Induced Oscillations.Lock Washer Installed on Arm
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-026, :on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures Revised |
- on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures Revised
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-027, :on 900907,manual Reactor Trip Due to Shearing of Feedwater Flow Control Valve Feedback Linkage Arm.W/ |
- on 900907,manual Reactor Trip Due to Shearing of Feedwater Flow Control Valve Feedback Linkage Arm.W/
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-028, :on 900908,automatic Reactor Trip Occurred Due to Lightning Strike |
- on 900908,automatic Reactor Trip Occurred Due to Lightning Strike
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-029, :on 900910,turbine/reactor Trip Caused by Failure of Personnel to Assure Availability of Drain Path. Operators Responded to Trip Per EOP & Stabilized Plant in Mode 3 |
- on 900910,turbine/reactor Trip Caused by Failure of Personnel to Assure Availability of Drain Path. Operators Responded to Trip Per EOP & Stabilized Plant in Mode 3
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-030, :on 900915,reactor Trip Occurred Due to Improper Routing of Heater Drain Pump Cable Shield Ground Lead |
- on 900915,reactor Trip Occurred Due to Improper Routing of Heater Drain Pump Cable Shield Ground Lead
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-031, :on 901017,containment Atmosphere Gaseous Radioactivity Monitoring Sys Declared Inoperable Due to Nonconservative Alarm Setpoints |
- on 901017,containment Atmosphere Gaseous Radioactivity Monitoring Sys Declared Inoperable Due to Nonconservative Alarm Setpoints
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-032, :on 900919,proper Identification of Design Bases Resulted in Operation/Testing of Containment Personnel Airlock Hydraulic Sys Inconsistent W/Existing Design.W/ |
- on 900919,proper Identification of Design Bases Resulted in Operation/Testing of Containment Personnel Airlock Hydraulic Sys Inconsistent W/Existing Design.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000445/LER-1990-033, :on 900926,personnel Error Lead to Momentary Loss of Containment Integrity |
- on 900926,personnel Error Lead to Momentary Loss of Containment Integrity
| 10 CFR 50.73(a)(2)(i) | | 05000445/LER-1990-034, :on 900928,surveillance Missed for Channel Response Time Due to Personnel Error |
- on 900928,surveillance Missed for Channel Response Time Due to Personnel Error
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000445/LER-1990-035, :on 901011,potential common-mode Failure of HPSI Pumps Discovered Due to Incorrect Suction Vent Valve Application |
- on 901011,potential common-mode Failure of HPSI Pumps Discovered Due to Incorrect Suction Vent Valve Application
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000445/LER-1990-036-01, Forwards Correspondence sign-off Sheet for LER 90-036-01. Suppl Acceptable for Submittal to NRC | Forwards Correspondence sign-off Sheet for LER 90-036-01. Suppl Acceptable for Submittal to NRC | | | 05000445/LER-1990-038, :on 901105,gas Channel Alarm Initiated Containment Ventilation Isolation |
- on 901105,gas Channel Alarm Initiated Containment Ventilation Isolation
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000445/LER-1990-039, :on 901030,inadequate Design Implementation Led to Potential for Overpressurization of Containment |
- on 901030,inadequate Design Implementation Led to Potential for Overpressurization of Containment
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000445/LER-1990-041, :on 901119,protection Set Inverter IV1PC3 Not Operable within 24 H of Trip.Cause of Trip Attributed to Ac Voltage Transients,Inadequate Termination on Loose Wire & Failure to Identify Damaged Components |
- on 901119,protection Set Inverter IV1PC3 Not Operable within 24 H of Trip.Cause of Trip Attributed to Ac Voltage Transients,Inadequate Termination on Loose Wire & Failure to Identify Damaged Components
| 10 CFR 50.73(a)(2)(1) | | 05000445/LER-1990-042, :on 901120,ESF Actuation Circuitry Disabled. Caused by Personnel Error in Review of Tech Spec Requirements |
- on 901120,ESF Actuation Circuitry Disabled. Caused by Personnel Error in Review of Tech Spec Requirements
| 10 CFR 50.73(a)(9)(1) | | 05000445/LER-1990-043, :on 901117,post-accident Sampling Sys Declared Inoperable Due to Failure of Valve to Remain Closed.On 901119,discovered That Valve Stroke Tested W/O Upstream Valve Deactivated.Caused by Personnel Error |
- on 901117,post-accident Sampling Sys Declared Inoperable Due to Failure of Valve to Remain Closed.On 901119,discovered That Valve Stroke Tested W/O Upstream Valve Deactivated.Caused by Personnel Error
| | | 05000445/LER-1990-044, :on 901130,reactor Operator Performed Test on Wrong Train of Charging Sys Due to Procedural Inadequacy. Results for Previously Performed Tests & Enhancements of Test Info on Work Orders Reviewed |
- on 901130,reactor Operator Performed Test on Wrong Train of Charging Sys Due to Procedural Inadequacy. Results for Previously Performed Tests & Enhancements of Test Info on Work Orders Reviewed
| 10 CFR 50.73(a)(2)(1) |
|