05000387/LER-2003-003

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LER-2003-003,
Steam Electric Station - Tiriit 1 ,Susquehanna
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
3872003003R00 - NRC Website

EVENT DESCRIPTION

At 22:35 on April 16, 2003 with Unit 1 In Mode 1 at 100% power and Unit 2 in Mode 4 at 0% power, a 24-month Secondary Containment Drawdown and In-leakage Surveillance Test revealed that the 'B' train of the Standby Gas Treatment system (SGTS) inlet damper PDD07554B would not modulate to its open position. That condition rendered the 'B' SGTS train (EIIS Code: BH) inoperable. Electrical Maintenance personnel (utility, non-licensed) investigated the condition and discovered that the control circuit wiring configuration external to the damper actuator was incorrect. The external wires from the controller to the damper actuator were terminated with their polarities reversed. During the investigation it was determined that the Incorrect configuration had existed since January 21, 1998 and resulted in the damper becoming inoperable during subsequent actuator replacement work performed on November 19, 2002. The error in the wiring configuration was promptly corrected and the 'B' SGTS train was returned to operable status at 14:15 on April 17, 2003. Additionally, it was determined that the 'A' SGTS train was removed from service for maintenance and testing activities from February 10, 2003 through February 12, 2003, from February 24, 2003 through February 25, 2003, on April 11, 2003 and again on April 12, 2003. Therefore, during the time periods in which the 'A' train was removed from service, both the 'A' and 'B' trains were inoperable.

CAUSE OF EVENT

Three root causes were found for the event. The maintenance procedure used to replace the damper actuator was not explicit enough with respect to control circuit wiring configuration. Work Management personnel did not specify the correct operability testing for the actuator replacement on the work order release form in 2002. Lastly, Operations personnel that released and closed out the work order release form did not detect the omission.

On January 21, 1998 Electrical Maintenance personnel (utility, non-licensed) replaced the damper actuator for PDDM07554B with a rebuilt actuator using maintenance procedure MT-GE-030 as part of its five-year Equipment Qualification (EQ) program. The replaced damper actuator failed to stroke dUring subsequent post maintenance operability testing. An investigation at that time revealed that the control circuit-wiring configuration internal to the damper actuator was incorrect. The wires from the actuator force coil were soldered in-place to the internal side of the termination block with their polarities reversed. Since the actuator force coil is one of the subcomponents replaced during the five-year actuator rebuild, MT-GE-030 acknowledged that there may be a need to reverse the force coil wires once the actuator is installed and tested. However, MT-GE-030 did not discuss changing the configuration of the external wires from the controller to the termination block since their configuration is shown on plant electrical drawings. To remedy the January 21, 1998 problem, Electrical Maintenance personnel incorrectly interpreted the instructions in MT-GE-030 and reversed the wires from the controller to the external side of damper actuator termination block instead of re-soldering the internal force coil wires to their correct polarity.

Operability testing was then re-performed and the damper functioned conectly. A review of that event revealed that the cause for the procedure misinterpretation was MT-GE-030 did not make a sufficient distinction in the terminology used to describe the wires that are internal to the actuator (force coil wires) and those wires that are external to the actuator.

CAUSE OF EVENT (continued) On November 19, 2002 Electrical Maintenance personnel (utility, non-licensed) again replaced the damper actuator for PDDM075548 with a rebuilt actuator as part of its five-year EQ program using maintenance procedure MT-GE-030. The force coil wires for that rebuilt actuator were soldered to the internal side of the termination block with correct polarity. Procedure MT-GE-030 directed Electrical Maintenance personnel to document the as-found location of the external wires from the controller to the termination block prior to removing the old actuator. Once the rebuilt actuator was installed, the procedure directed them to terminate the external wires at their as-found location. The damper stroked in-place with the control wires (external) determinated when Electrical Maintenance personnel used a simulated control signal. However, when the control wires were terminated with reverse polarity at the terminal block, damper PDDIV107554B would not have functioned on an actual signal from the system controller. In addition, the operability testing specified for the work did not reveal that the actuator was incorrectly wired. The 'B' Standby Gas Treatment train was subsequently returned to an operable status.

At PPL Susquehanna, LLC components and systems are released for work using a Release Work Order (RLWO) which is prepared by a Work Week Manager (utility, non-licensed) and reviewed by Unit Supervisor (utility, licensed). That document lists the operability testing that is required to return the component or system to an operable status. When all work and operability testing is completed, the RLWO is closed by a Unit Supervisor (utility, licensed) to ensure that the released equipment is operable. The operability testing stated on the RLWO used for the actuator replacement on November 19, 2002 was not adequate to detect the incorrect wiring configuration. The Work Week Manager omitted the necessary testing requirement and the error went undetected by the two Unit Supervisors involved. A review of those errors revealed that operability testing process roles and responsibilities are discussed in several levels of station procedures and computerized work flow steps but there are inconsistencies between them. For example, the RLWO computerized work flow steps provide an entry for operability testing but it is not required to be filled in. If the entry is left blank by the Work Week Manager, the computerized process does not require the Unit Supervisor to concur that `none` is the correct operability testing to be performed.

ANALYSIS / SAFETY SIGNIFICANCE

This event is reportable as a Condition Prohibited by the Technical Specifications per 10 CFR 50.73(a)(2)(i)(B) and as an Event or Condition That Alone Could Prevent Fulfillment of a Safety Function per 10 CFR 50.73(a)(2)(v)(C). The 'B' train of SGTS was inoperable greater than the seven days allowed by Technical Specification 3.6.4.3 Condition A and the 'A' train of SGTS was removed from service on several occasions while the 'B' train was inoperable. Although Unit 2 was shut down for a refueling outage at the time of the discovery, the conditions apply to both Unit 1 and Unit 2 since Unit 2 was in Mode 1 prior to its shutdown on March 8, 2003.

ANALYSIS / SAFETY SIGNIFICANCE (continued) The SGTS is designed to accomplish the following safety related objectives:

a) Exhaust sufficient filtered air from the Reactor Building (E1IS Code: NG) to maintain a negative pressure of about 0.25 inches water gauge in the affected volumes following secondary containment isolation for a spent fuel handling accident in the refueling floor area and for a Loss Of Coolant Accident (LOCA).

b) Filter the exhausted air to remove radioactive particulates and both radioactive and non-radioactive forms of iodine to limit the offsite dose to the guidelines of 10 CFR100.

There were no actual consequences to the health and safety of the public as a result of this event since neither train of SGTS were required to actuate during the time they were inoperable. During those periods when both trains of SGTS were inoperable there were no irradiated fuel moves taking place. However, the SGTS would not have been able to fulfill the above objectives during those times if a LOCA would have occurred. During the remaining periods from November 19, 2002 until April 16, 2003 (when only the 'B' train was inoperable), the 'A' train was operable and would have been capable of meeting the above safety related objectives.

In accordance with guidance in NUREG-1022, Revision 2, the due date for this report is June 16, 2003.

CORRECTIVE ACTIONS

Corrective actions that have been completed:

  • The error in the wiring configuration was corrected and the 'B' SGTS train was returned to operable status.

■ It was confirmed that the 'A' SGTS train was not affected by wiring configuration problems via proper system testing.

Corrective actions to be completed:

  • Revise the maintenance procedures that remove, rebuild and replace the subject damper actuators to provide sufficient distinction in the terminology used to describe the wires that are internal to the actuator (force coil wires) and those wires that are external to the actuator.
  • Revise operability testing process procedures and computerized workflow steps guides to eliminate the inconsistencies.
  • Revise RLWO computerized workflow steps to require an entry for operability testing even if the testing required is "none!
  • Provide training to Unit Supervisor personnel on the requirement to evaluate component and system operability testing during RLWO release and close out.

ADDITIONAL INFORMATION

Past Similar Events: None Failed Component : 'B' SGTS train inlet Damper PDD075548 Manufacturer ITT Model: NH93