LER-1981-008, Updated LER 81-008/03X-1:on 810217 & 0310,primary Coolant I-131 Dose Equivalent Value Observed Following Reactor Trip Exceeded Tech Spec 3.4.8.a.Caused by Expected Spike in Primary Coolant Activity Following Trip |
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Update Report-Previous Report Date 3/12/81
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,e 76 ut,ont oats so EVENT DESCRIPTION AND PRC8 A8LE CONSEQUENCES to I On two occasions, during Mode Toperation following a Reactor trip from i o 2 100% rated reactor power, a primary coolant Iodine-131 dose equivalent i
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i value was observed. exceeding the limit of T.S.3.4.8.a A spike of 1.59 I o a i microcuries per gram occurred on 2/17/81 and a spike of 1.66 microcuries I o s l
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This nccitrrence jg similar tg f_EDag gI 50-368/80-009. Reportable per T.S.6.9.1.9.b.
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M 33 40 el el 43 se e7 CAUSE DESCRIPTION AND CC4 REC flVE ACTIONS 27 gl The specific activity increase was caused by an oxnocted sniko in nri-I m i mary coolant activity following a reactor trip.
The reactor coolant i
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,, i the concentration of radioactive iodine to within acceptable limits.
i e i Additional historical information is attached Der the reauirements of T.1.3.4.8.d
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.l Attachment to LER 50-368/81-008 Occurrence'Date:
2/17/81 Items 1.& 3.
Reactor Power & Cleanup Flow History Starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to ist sample.in which limit was exceeded
. Iodine DE = 1.59 uCi/GM 2/17/81 0 1515 (Sample time 1312)
Rx Power LD Flow CHRG PWMP
~
1300 100%
<38 GPM
$46 GPM 1400 2
l 2/15/81
~ 1500 1600 1700 1800 1900 2000 2100 2200 2300 2400-2/16/81 0100 0200 t
0300 i
0400 0500 0600 0700 i
0800 0900 l
1000 1100 1200 1
1300 i
q 3.
e i
Attachment to LER 50-368/81-008 Occurrence Date: 2/17/81 Rx Power LO Flow CHRG Pump 2/16/81' 1500 100%
N33 GPM S46 GPM 1600 1700 1800 1900 2000 2100 2200 2300 i
2400 2/17/81 0100 0200 0300 0400 0500 4
0600 0700 0800 0900
'1000, 1100 0%
83 GPM 89 GPM 1 -
1200 38 GPM 45 GPM 1300 1400 1500 0
Attachment to LER 50-368/81-008 Occurrence Date: 2/17/81 Item 2.
Fuel Burnup By Core Region Fuel Type Batch Exposure (MWD /MTU) 1 6383.4543 2
8558.8705 3
10076.9981 4
11735.7655 5
12500.5411 6
11931.9310 7
6657.1972 Core Average 11089.5 MWD /MTU Item 4.
History of Degassing Operation tio degassing prior to exceeding IDE of 1.0 uCi/GM.
Normal letdown / makeup until time of notficiation of
>1.0 uCi/GM.
1 Item 5.
Time Duration of DE I-131
> 1.0 uCI/gm The duration with activity 1.0 uCi/ Gram was approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />.
A sample of reactor coolant was taken at 1312 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.99216e-4 months <br /> on 2/17/81, showing an activity of 1.59 uCi/gm.
Samples were taken at four hour intervals until activity indicated I-131 DE equal tc 0.69 uCi/gm.
The cumulative operating time at a primary coolant specific activi ty
> 1.0 uCi/gm DE I-131 equals approximately 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> for the last six month period (less than 500 hour0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> limit of T.S.
3.4.8 Action a).
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Attachment to LER 50-368/81-008 Occurrence Date: 3/10/81 Items 1 & 3:
Reactor Power & Cleanup Flow History starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to ist sample in which limit was exceeded.
Iodine DE = 1.66 uCi/gm on 3/10/81 0 0725 hours0.00839 days <br />0.201 hours <br />0.0012 weeks <br />2.758625e-4 months <br /> Time Rx Power LD Flow CHRG Flow 3/08/81 0700 100%
s44 GPM s44 GPM se s/
sr s4' GPM 4
3/09/81 0700 100%
s44 GPM 3/10/81 0240.
5/
- - V v
v 0%
s44 GPM s44 GPM 3/
S/
S/
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3/10/81 0725 0%
s44 GPM s44 GPM t
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l Attachment to LER 50-368/81-003 Occurrence Date: 3/10/81 Item 2:
Fuel Burnup by Core Region Batch Exposure (MWD /MTU) 1 6853.9 2
9154.2 3
10822.2 4
12588.2 5
13389.8 6
12758.4 7
7170.2 Item 4:
History of Degassing Operation No degassing prior to exceeding IDE of 1.0 uCi/gm.
Normal letdown / makeup until time of notification of
>1.0 uCi/gm.
Item 5:
Time Duration of IDE > uCi/GM 1
Duration with activity
>1.0 uCi/GM was approximately 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. A sample of the Reactor Coolant was taken at 0725 hours0.00839 days <br />0.201 hours <br />0.0012 weeks <br />2.758625e-4 months <br /> on 3/10/81, showing an activity of 1.66 uCi/GM. Samples were taken at 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> intervals until activity indicated IDE
<1.0 uCi/GM.
The cumulative operating time at a primary coolant specific activity
>1.0 uCi/GM I-131 equals approximately 29 hours3.356481e-4 days <br />0.00806 hours <br />4.794974e-5 weeks <br />1.10345e-5 months <br /> for the last 6 month period ( <500 hour limit of T.S. 3.4.8 Action a).
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| 05000313/LER-1981-001-01, /01T-0:on 810117,during Reactor Bldg Cooler Svc Water Lines Engineering Analysis,Discovered Previous Analyses Considering Cooling Unit Piping Nozzles as Rigid Anchors.Nozzle Loads Imposed by Vendor Overlooked | /01T-0:on 810117,during Reactor Bldg Cooler Svc Water Lines Engineering Analysis,Discovered Previous Analyses Considering Cooling Unit Piping Nozzles as Rigid Anchors.Nozzle Loads Imposed by Vendor Overlooked | | | 05000313/LER-1981-001, Forwards LER 81-001/01T-0 | Forwards LER 81-001/01T-0 | | | 05000368/LER-1981-001-03, /03L-0:on 810102,during Mode 1 Operation,Leak Was Found at Vent Line Weld on Charging Pump Stabilizer 2M115C. Leak Isolation Rendered Charging Pump 2P36C Inoperable. Caused by Dissolving Slag Inclusion.Weld Was Repaired | /03L-0:on 810102,during Mode 1 Operation,Leak Was Found at Vent Line Weld on Charging Pump Stabilizer 2M115C. Leak Isolation Rendered Charging Pump 2P36C Inoperable. Caused by Dissolving Slag Inclusion.Weld Was Repaired | | | 05000368/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000368/LER-1981-002-03, /03L-0:on 810106,postulated Failure of Masonry Wall 24-B-217/218 Per IE Bulletin 80-11,resulted in Loss of Cables 2BS3L1 & 2BS3L2 to Containment Cooling Fans.Wall Braced in Accordance W/New Design Criteria | /03L-0:on 810106,postulated Failure of Masonry Wall 24-B-217/218 Per IE Bulletin 80-11,resulted in Loss of Cables 2BS3L1 & 2BS3L2 to Containment Cooling Fans.Wall Braced in Accordance W/New Design Criteria | | | 05000368/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000313/LER-1981-002, Forwards LER 81-002/99X-0 | Forwards LER 81-002/99X-0 | | | 05000313/LER-1981-002-99, /99X-0:on 810303,during Steam Generator Tubing Surveillance Insp,First Sample Results on E24A Found Three Tubes Exceeded Plugging Limit.Cause Not Stated | /99X-0:on 810303,during Steam Generator Tubing Surveillance Insp,First Sample Results on E24A Found Three Tubes Exceeded Plugging Limit.Cause Not Stated | | | 05000313/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000313/LER-1981-003-03, /03L-0:on 810113,penetration Fire Barrier Between North Wall & Compressor C2B Removed W/O Establishing Fire Watch Per Tech Specs.Caused by Inadequate Instructions to Contractor Personnel.Contractor Procedures Modified | /03L-0:on 810113,penetration Fire Barrier Between North Wall & Compressor C2B Removed W/O Establishing Fire Watch Per Tech Specs.Caused by Inadequate Instructions to Contractor Personnel.Contractor Procedures Modified | | | 05000368/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000368/LER-1981-003-03, /03L-0:on 810113,plant Computer Failed & Would Not Restart,Rendering Core Operating Limits Supervisory Sys Inoperable.Caused by Capacitor in Floating Point Power Supply & Generstor Noise Due to Short.Capacitor Replaced | /03L-0:on 810113,plant Computer Failed & Would Not Restart,Rendering Core Operating Limits Supervisory Sys Inoperable.Caused by Capacitor in Floating Point Power Supply & Generstor Noise Due to Short.Capacitor Replaced | | | 05000313/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000313/LER-1981-004-03, /03L-0:on 810227,diesel Fire Pump Battery Bank Surveillance Test Found Not Completed within Grace Period. Caused by Failure to Notify Supervisor That Procedure Could Not Be Completed During Shift | /03L-0:on 810227,diesel Fire Pump Battery Bank Surveillance Test Found Not Completed within Grace Period. Caused by Failure to Notify Supervisor That Procedure Could Not Be Completed During Shift | | | 05000368/LER-1981-004-03, /03L-0:on 810124,core Protection Calculator C Declared Inoperable.Caused by Failed Power Amplifier for C Excore Detector Which Caused Low Power Signal to Set Off Alarm,Alerting Staff.Amplifier Replaced | /03L-0:on 810124,core Protection Calculator C Declared Inoperable.Caused by Failed Power Amplifier for C Excore Detector Which Caused Low Power Signal to Set Off Alarm,Alerting Staff.Amplifier Replaced | | | 05000368/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000368/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000368/LER-1981-005-03, /03L-0:on 810204,core Operating Limit Supervisory Sys Rendered Inoperable.Caused by Computer Failure.Software Reloaded & Computer Restarted.Backup Computer Will Be Installed | /03L-0:on 810204,core Operating Limit Supervisory Sys Rendered Inoperable.Caused by Computer Failure.Software Reloaded & Computer Restarted.Backup Computer Will Be Installed | | | 05000313/LER-1981-005-03, /03L-0:on 810408,steam Driver Emergency Feedwater pump,P7A,was Started & Then Tripped by Turbine Overspeed Mechanism.Caused by Worn Edges on Trip Mechanism.Mechanism Adjusted to Latch Firmly.Preventive Maint Program Revised | /03L-0:on 810408,steam Driver Emergency Feedwater pump,P7A,was Started & Then Tripped by Turbine Overspeed Mechanism.Caused by Worn Edges on Trip Mechanism.Mechanism Adjusted to Latch Firmly.Preventive Maint Program Revised | | | 05000313/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000368/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000368/LER-1981-006-03, /03L-0:on 810204,containment Sump Level Indicator 2LI-5645-1 Was Declared Inoperable.Caused by Defective Converter.Converter Replaced | /03L-0:on 810204,containment Sump Level Indicator 2LI-5645-1 Was Declared Inoperable.Caused by Defective Converter.Converter Replaced | | | 05000313/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000313/LER-1981-006-03, /03L-0:on 810408,emergency Feedwater Feed Valve CV-2670 to Steam Generator a Control Power Fuse Blew on Valve Actuator.Caused by Fuse Opening on Transient Current. Fuse Replaced W/Slower Acting Fuse | /03L-0:on 810408,emergency Feedwater Feed Valve CV-2670 to Steam Generator a Control Power Fuse Blew on Valve Actuator.Caused by Fuse Opening on Transient Current. Fuse Replaced W/Slower Acting Fuse | | | 05000368/LER-1981-007-03, /03L-0:on 810206,control Room Emergency Chiller, 2VE-1B,tripped.Caused by Low Suction Pressure Due to Leaking Expansion Valve.Valve Repaired & Sys Refilled W/Freon | /03L-0:on 810206,control Room Emergency Chiller, 2VE-1B,tripped.Caused by Low Suction Pressure Due to Leaking Expansion Valve.Valve Repaired & Sys Refilled W/Freon | | | 05000368/LER-1981-007, Updated LER 81-007/03L-1:on 810206 & 0318,control Room Emergency Chillers 2VE-1B & 2VE-1A,respectively,were Declared Inoperable.Caused by Low Oil Pressure in Former & Oil Unloader Relief Misadjustment in Latter | Updated LER 81-007/03L-1:on 810206 & 0318,control Room Emergency Chillers 2VE-1B & 2VE-1A,respectively,were Declared Inoperable.Caused by Low Oil Pressure in Former & Oil Unloader Relief Misadjustment in Latter | | | 05000313/LER-1981-007-03, /03L-0:on 810427,emergency Diesel Generator K4B Failed to Start,Tripping Lockout Relay & Loss of Excitation Relay.Caused by Blocking Device in Auxiliary Contacts of Loss of Excitation Relay.Device Removed.Procedure Revised | /03L-0:on 810427,emergency Diesel Generator K4B Failed to Start,Tripping Lockout Relay & Loss of Excitation Relay.Caused by Blocking Device in Auxiliary Contacts of Loss of Excitation Relay.Device Removed.Procedure Revised | | | 05000313/LER-1981-007, Forwards LER 81-007/03L-0 | Forwards LER 81-007/03L-0 | | | 05000368/LER-1981-008-03, /03L-0:on 810217,during Mode 3 Operation,Following Reactor Trip from 100% power,I-131 Dose Equivalent of 1.59 Uci Observed.Caused by Expected Spike in Coolant Activity. Liquid Processed Through Primary Demineralizers | /03L-0:on 810217,during Mode 3 Operation,Following Reactor Trip from 100% power,I-131 Dose Equivalent of 1.59 Uci Observed.Caused by Expected Spike in Coolant Activity. Liquid Processed Through Primary Demineralizers | | | 05000368/LER-1981-008, Updated LER 81-008/03X-1:on 810217 & 0310,primary Coolant I-131 Dose Equivalent Value Observed Following Reactor Trip Exceeded Tech Spec 3.4.8.a.Caused by Expected Spike in Primary Coolant Activity Following Trip | Updated LER 81-008/03X-1:on 810217 & 0310,primary Coolant I-131 Dose Equivalent Value Observed Following Reactor Trip Exceeded Tech Spec 3.4.8.a.Caused by Expected Spike in Primary Coolant Activity Following Trip | | | 05000313/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000313/LER-1981-008-03, /03L-0:on 810602,sodium Hydroxide Tank Level Fell Below Tech Spec Requirements.Caused by Test Procedure Assuming Familiarity W/Sys Layout & Idiosyncrasies.Tank Refilled | /03L-0:on 810602,sodium Hydroxide Tank Level Fell Below Tech Spec Requirements.Caused by Test Procedure Assuming Familiarity W/Sys Layout & Idiosyncrasies.Tank Refilled | | | 05000368/LER-1981-009-03, /03L-0:on 810211,during Mode 1 Operation,While Performing Refueling Water Tank Level Indication Channel Checks,Channel a Indicated Greater than 100%,followed by Channel B 3-h Later.Caused by Frozen Transmitter Lines | /03L-0:on 810211,during Mode 1 Operation,While Performing Refueling Water Tank Level Indication Channel Checks,Channel a Indicated Greater than 100%,followed by Channel B 3-h Later.Caused by Frozen Transmitter Lines | | | 05000368/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000313/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000313/LER-1981-009-03, /03L-0:on 810727,during Start Test of Steam Driven Emergency Feedwater Pump P7A,steam Generator B Valve CV-2617 Did Not Open on Demand.Caused by Excessive Play Due to Wear.Switch Replaced | /03L-0:on 810727,during Start Test of Steam Driven Emergency Feedwater Pump P7A,steam Generator B Valve CV-2617 Did Not Open on Demand.Caused by Excessive Play Due to Wear.Switch Replaced | | | 05000368/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000368/LER-1981-010-03, /03L-0:on 810212,during Mode 1 Operation,Control Element Assembly Calculator (Ceac) 2 Found Inoperable.Cause Unknown.Ceac 2 Returned to Operable Status by Reinitializing Sys.All Failure Indications Returned to Normal | /03L-0:on 810212,during Mode 1 Operation,Control Element Assembly Calculator (Ceac) 2 Found Inoperable.Cause Unknown.Ceac 2 Returned to Operable Status by Reinitializing Sys.All Failure Indications Returned to Normal | | | 05000313/LER-1981-010-03, /03L-0:on 810804,during Calibr,Reactor Protective System Channel B Scaled Difference in Amplifier Gain Setting Differed from Value in Power Escalation Test.Caused by Incorrect Pentiometer Adjustment.Procedure Revised | /03L-0:on 810804,during Calibr,Reactor Protective System Channel B Scaled Difference in Amplifier Gain Setting Differed from Value in Power Escalation Test.Caused by Incorrect Pentiometer Adjustment.Procedure Revised | | | 05000313/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000368/LER-1981-011-03, /03L-0:on 810224,review of Plant Protection Sys Surveillance Procedure Identified That Channel A,Steam Generator High Level Trip Setpoint Less Conservative than Required.Caused by Deficiency in Surveillance Procedure | /03L-0:on 810224,review of Plant Protection Sys Surveillance Procedure Identified That Channel A,Steam Generator High Level Trip Setpoint Less Conservative than Required.Caused by Deficiency in Surveillance Procedure | | | 05000368/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000313/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000313/LER-1981-011-03, /03L-0:on 810810,during Stroke Test,Recirculation Valve of Makeup Pump & Redundant Valve Failed to Show Full Closed Indication.Caused by Valve Torque Settings Too Low to Move Valves Under Sys Pressure.Settings Increased | /03L-0:on 810810,during Stroke Test,Recirculation Valve of Makeup Pump & Redundant Valve Failed to Show Full Closed Indication.Caused by Valve Torque Settings Too Low to Move Valves Under Sys Pressure.Settings Increased | | | 05000368/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000368/LER-1981-012-03, /03L-0:on 810303,loop Two Svc Water Header Engineered Safety Feature Isolation Valve 2CV-1406-2 Would Not Open from Control Room.Caused by Valve Operator Torquing Out Due to Valve Stem Binding | /03L-0:on 810303,loop Two Svc Water Header Engineered Safety Feature Isolation Valve 2CV-1406-2 Would Not Open from Control Room.Caused by Valve Operator Torquing Out Due to Valve Stem Binding | | | 05000313/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000313/LER-1981-012-03, /03L-0:on 810821,when Emergency Diesel Generator (EDG) Was Given Autostart Signal Following Turbine Trip,Edg Came to Speed But Failed to Tie In.Overcrank Annunciator Alarmed.Caused by Defective Speed Sensing Relay | /03L-0:on 810821,when Emergency Diesel Generator (EDG) Was Given Autostart Signal Following Turbine Trip,Edg Came to Speed But Failed to Tie In.Overcrank Annunciator Alarmed.Caused by Defective Speed Sensing Relay | | | 05000313/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000368/LER-1981-013-03, /03X-1:on 810304,RCS Cold Leg Temp Indicator Discovered to Be Reading High.Caused by Defective Servo Motor.Motor Replaced.Indicator Calibr | /03X-1:on 810304,RCS Cold Leg Temp Indicator Discovered to Be Reading High.Caused by Defective Servo Motor.Motor Replaced.Indicator Calibr | |
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