05000364/FIN-2017003-01
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Finding | |
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Title | Failure to perform adequate corrective maintenance on the 2B EDG |
Description | The NRC identified a non-cited violation (NCV) of Technical Specification (TS) 5.4.1.a, Procedures, for the licensees failure to implement corrective maintenance work order instructions to identify and replace piping as necessary for a degraded threaded joint on the 2B emergency diesel generator (EDG) jacket water keep warm system piping. As a result, a leak occurred at this threaded pipe joint during surveillance testing which rendered the 2B EDG inoperable. The inspectors determined that the failure to follow work order instructions to replace degraded jacket water system piping during corrective maintenance on the 2B EDG on March 3, 2017, was a performance deficiency (PD). The finding was more than minor because it was associated with the equipment reliability attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The significance of this finding was evaluated using IMC 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012. Initial screening by the resident inspectors using the Saphire Farley 1 & 2 SPAR Model resulted in a potentially greater-than-green significance. Therefore, a detailed risk analysis was performed by a regional senior reactor analyst (SRA). The NRC Farley SPAR model was used for internal events, seismic and tornado/high winds risk estimates and the licensees Farley fire probabilistic risk assessment model was used for fire risk estimation. The major analysis assumptions included: a 51-day exposure period, EDG 2B operation at nominal failure to run probability until 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> when EDG assumed to fail due to the PD, PD treated as having common cause failure to run potential, no recovery of the 2B EDG was assumed, and no credit for FLEX equipment was assumed. The operation of the EDG for 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> prior to failure and remaining mitigating equipment limited the risk. The dominant sequence was a station blackout sequence consisting of a site-wide weather-related loss of offsite power, successful reactor shutdown, random failure to run of the 1/2A and 1C EDGs, failure of the 2B EDG due to the performance deficiency, failure to manually operate the turbine driven auxiliary feedwater pump long term, and failure to recover offsite power or an EDG leading to loss of core heat removal and core damage. The detailed risk evaluation (DRE) determined that the increase in core damage frequency due to the PD was <1.0 E-6 per year, a Green finding of very low safety significance. The finding had a cross-cutting aspect of Conservative Bias in the Human Performance area, because the decision to leave the diesel in a degraded condition following maintenance on March 3, 2017 was neither conservative nor prudent when additional action could have been taken to adequately repair or evaluate the threaded pipe joint [H.14]. |
Site: | Farley |
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Report | IR 05000364/2017003 Section 4OA3 |
Date counted | Sep 30, 2017 (2017Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | P Niebaum K Miller R Kellner W Pursley A Nielsen G Ottenberg B Collins |
Violation of: | Technical Specification - Procedures |
CCA | H.14, Conservative Bias |
INPO aspect | DM.2 |
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Finding - Farley - IR 05000364/2017003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Farley) @ 2017Q3
Self-Identified List (Farley)
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