05000353/LER-2008-002

From kanterella
Jump to navigation Jump to search
LER-2008-002, Automatic Actuation Of The Reactor Protection System At Power
Limerick Generating Station, Unit 2
Event date: 02-01-2008
Report date: 03-31-2008
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3532008002R00 - NRC Website

Unit Conditions Prior to the Event Unit 2 was in Operational Condition (OPCON) 1 (Power Operation) at approximately 100% power. There were no structures, systems or components out of service that contributed to this event.

Description of the Event

On Friday, February 1, 2008, Limerick Unit 2 was operating at 100% power. At approximately 04:45 hours an automatic actuation of the reactor protection system (RPS) (EIIS:JC) occurred as a result of a phase-to-ground fault at the 2A Main Transformer (EIIS:XFMR) low voltage (22 kV) bushing connection to the Iso-Phase Bus (EIIS:EL). The Main Generator neutral overvoltage relay actuated and tripped the generator protection lockout relays, which resulted in a Main Turbine trip. The operators entered the trip procedure for reactor pressure vessel (RPV) control (T-101) and stabilized reactor parameters. All control rods fully inserted.

Reactor wide range level indication decreased to -2.0 inches and then increased to a maximum of +46 inches and stabilized at +35 inches. Reactor pressure was approximately 1042 psig prior to the automatic scram, peaked at 1140 psig, and stabilized at approximately 965 psig one minute after scram.

The reactor high pressure scram setpoint of 1096 psig was exceeded but RPS had previously initiated due to the main turbine control valve closure. The redundant reactivity control system (RRCS) setpoint of 1149 psig was not exceeded. The lowest main steam relief valve (MSRV) setpoint of 1170 psig was not exceeded; therefore, no MSRVs actuated. The main steam bypass valves opened as designed to control pressure post scram.

Primary containment isolation signals were automatically initiated at +12.5 inches reactor level. A Group 2 isolation occurred at +12.5 inches but the isolation valves were in the closed position prior to the event. The reactor recirculation pumps motor-generator set breakers tripped due to the main generator lockout.

The investigation determined that a phase-to-ground fault occurred on the Iso-Phase Bus connection at the 2A Main Transformer low voltage (22kV) bushing due to overheating of the connection.

This event resulted in an actuation of RPS when the reactor was critical and a valid actuation of RPS and containment isolation valves. The 4-hour ENS notifications required by 10CFR50.72(b)(2)(iv)(B) and the 8-hour notification required by 10CFR50.72(b)(3)(iv)(A) were performed on Friday February 1, 2008 at 05:46 hours (#43949).

This event resulted in automatic actuations of RPS and containment isolation valves. Therefore, this LER is being submitted pursuant to the requirements of 10CFR50.73(a) (2) (iv) (A).

Analysis of the Event

There were no actual safety consequences associated with this event. The potential safety consequences of this event were minimal. A turbine trip with bypass transient is categorized as an incident of moderate frequency per UFSAR section 15.2.3, "Turbine Trip". The plant equipment performed as designed during the transient and the operators effectively stabilized reactor parameters.

The 2A Main Transformer low voltage (22kV, air side) X1 bushing failed at the electrical connection between the bushing flange and the flexible copper link to the Iso-Phase Bus. This failure caused a phase-to-ground fault. Both X1 and X2 bushings on this transformer went into service in March 2007 when 2A Main Transformer was exchanged with the on-site spare.

The failure likely initiated in the electrical contact surface between the bushing and the copper links. This failure then propagated to the grounded Iso-Phase enclosure and caused the Main Generator protective relay actuation.

The failure was initiated by a degraded contact surface that was conducting rated electrical current.

Cause of the Event

The scram was caused by a Main Turbine trip as a result of a Main Generator Iso-Phase Bus ground fault. The ground fault was due to overheating of the 'A' phase connection between the Iso-Phase bus flexible link and the X1 low voltage (22 kV) bushing at the 2A Main Transformer.

The root cause of this event was inadequate change management when the Limerick Main Transformer maintenance ownership was transitioned from Exelon Energy Delivery (EED) to the site in January 2001. Specifically, procedure connection details were not subsequently transferred from EED procedures into station site procedures.

There were two contributing causes related to procedural deficiencies and the lack of training.

Corrective Action Completed 1)Both X1 and X2 bushings were replaced with reconditioned bushings having the 2x7 bolt pattern (i.e., original configuration).

2)All Unit 2 main transformer low voltage bushings were prepared and assembled using the upgraded guidance now contained in procedure M-035-003.

Corrective Action Planned The Limerick electrical work force and electrical planners will be provided training on proper treatment and assembly of electrical power conductors.

Previous Similar Occurrences There were no previous similar occurrences of scrams caused by Iso-Phase bus ground faults. However, a scram due to overheating of the Doble links of a Main Transformer high voltage bushing was reported in LER 1-00-002. The corrective actions for the previous event were effectively implemented. However, during the transition of Main Transformer maintenance from EED to the station Maintenance organization, they were not subsequently transferred from EED procedures into station site procedures due to less than adequate change management.

Component data:

Component description: 2A Main Transformer Component number: 2A-X101 Manufacturer: M175 McGraw Edison Co Model number: CC-464368 DWG Serial number: C-07005-5-3

References:

M-035-003, X101 Oil Cooled Transformers Cleaning, Examination, and Testing M-200-005, Non-safety Related Oil Cooled Transformers Clean and Examine