05000352/FIN-2017002-02
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Finding | |
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Title | Follow -Up of Events and Notices of Enforcement Discretion |
Description | Inspection Scope On March 20, 2016, Limerick Unit 1 was performing a planned shutdown to support a refueling outage. The drywell leak inspection team identified a 0.5 gallons per minute reactor coolant system (RCS) pressure boundary leak on the shutdown cooling equalizing line. The apparent cause evaluation determined that the 34 inch A RHR shutdown cooling return check valve equalizing line developed a crack at the toe of the weld due to high cyclic fatigue induced by vibration from the reactor recirculation system. This check valve was previously replaced in 2006, and the equalizing line came pre - fabricated to the valve body. The affected section of the piping was replaced with a new socket weld with a 2x1 overlay to improve the pipe stability and minimize stresses. The Unit 1 B RHR shutdown cooling return check valve equalizing line weld was also reworked using the 2x1 weld method during the Unit 1 refueling out age in April 2016. The similar Unit 2 welds on the equalizing lines were examined and reinforced during the May 2017 refueling outage. The LER and associated evaluations and follow -up actions were reviewed for accuracy, the appropriateness of corrective actions, violations of requirements, and potential generic issues. This LER is closed. b. Findings Description. On March 20, 2016, Limerick Unit 1 was performing a planned shutdown to support a refueling outage. The drywell leak inspection team identified a 0.5 gallons per minute RCS pressure boundary leak on the shutdown cooling equalizing line. Additionally, Exelon determined that this leakage constituted a violation of the Unit 1, TS 3.4.3.2. Operational Leakage that requires the RCS leakage to be limited to no pressure boundary leakage. The condition was reported in event notification 51809 as required by 10 CFR 50.72(b)(3)(ii)(A ) because it represented a degradation of a principal safety barrier. Exelon evaluated the flaw and determined the cause of the RCS pressure boundary leakage was that the 34 inch A RHR shutdown cooling return check valve equalizing line developed a crack at the toe of the weld due to high cyclic fatigue induced by vibration from the reactor recirculation system. The inspectors reviewed the LER and Exelons apparent cause evaluation of the event. The inspectors reviewed the event information and leakage data over the previous cycle and concluded that reactor pressure boundary leakage reasonably began on an unknown date that was more than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> before March 20, 2016. However, the inspectors determined that the existence of R CS pressure boundary leakage was not within Exelons ability to foresee and correct and therefore was not a performance deficiency. In particular, the RHR shutdown cooling return check valve was replaced on the recommended periodicity, and the equalizing line that developed the crack came pre- fabricated to the valve body when replaced in 2006. For information, the inspectors screened the significance of the condition using IMC 0609, Appendix A, The Significance Determination Process For Findings At -Power , and determined that the condition represented very low safety significance (Green) because it would not result in exceeding the RCS leak rate for a small LOCA and would not have likely affected other systems used to mitigate a LOCA. 19 Enforcement. TS 3.4.3.2 requires, in part, that RCS operational leakage shall be limited to no pressure boundary leakage. If pressure boundary leakage exists, the TS 3.4.3.2 limiting condition for operation action statement requires Unit 1 to be in at least hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Contrary to the above, for a period that began on an unknown date that was very likely more than 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> before March 20, 2016, and ending on March 20, 2016, RCS pressure boundary leakage existed, and Exelon did not place Unit 1 in at least hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and in cold shutdown within the next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. This issue is considered within the traditional enforcement process because there was no performance deficiency associated with the violation of NRC requirements. Inspection Manual Chapter 0612, Power Reactor Inspection Reports, Section 03.22 states, in part, that traditional enforcement is used to disposition violations receiving enforcement discretion or violations without a performance deficiency. The NRC Enforcement Policy, Section 2.2.1 states, in part, that, whenever possible, the NRC uses risk information in assessing the safety significance of violations. Accordingly, after considering that the condition represented very low safety significance, the inspectors concluded that the violation would be best characterized as Severity Level IV under the traditional enforcement process. However, the NRC is exercising enforcement discretion (EA- 17- 076) in accordance with Section 3.10 of the NRC Enforcement Policy which states that the NRC may exercise discretion for violations of NRC requirements by reactor licensees for which there are no associated performance deficiencies. In reaching this decision, the NRC determined that the issue was not within the licensees ability to foresee and correct; the licensees actions did not contribute to the degraded condition; and the actions taken were reasonable to identify and address the condition. Furthermore, because the licensees actions did not contribute to this violation, it will not be considered in the assessment process or the NRCs Action Matrix. |
Site: | Limerick |
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Report | IR 05000352/2017002 Section 4OA3 |
Date counted | Jun 30, 2017 (2017Q2) |
Type: | Violation: Severity level Enforcement Discretion |
cornerstone | No Cornerstone |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | S Rutenkroger M Fannon H. Anagnostopoulus J Cherubini D Hardage A Turilin D Schroeder |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Limerick - IR 05000352/2017002 | ||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Limerick) @ 2017Q2
Self-Identified List (Limerick)
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