05000336/LER-2010-002

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LER-2010-002, Manual Reactor Trip on High Steam-Generator Water Level
Docket Numbersequential Rev
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(B), System Actuation
Initial Reporting
ENS 45945 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation
3362010002R00 - NRC Website

1. !Event Description On May 22, 2010 at 1645 with the Millstone Power Station Unit 2 (MP-32) at 100% power in Mode 1, the reactor [AA] [RCT] was manually tripped by operators due to a high water level condition in the number 2 steam generator oscillations occurred because of feedwater level [SJ] control problems associated with the number 2 feedwater regulating valve [V] (2-FW-518). When the number 2 S/G water level rose to 84.4% on narrow range instrumentation, the operators manually tripped the reactor in accordance with established operating procedures.

In accordance with their training and also established procedures, the operators closed the number 2 steam generator feedwater regulating valve block valve-(2-FW-42B) and tripped both main feedwater pumps.

The auxiliary feedwater [BA] system automatically actuated,as expected on low level in number 1 steam generator at the setpoint of 18.1% water level. The steam dump valves continued to control main steam [SB] pressure.

Safety systems functioned as expected based upon the signals received. The operators took actions as trained and in accordance with established procedures. No equipment was damaged as a result of the-event. The unit was brought to a stable condition in hot-standby (Mode 3) and the degraded valve positioner was replaced.

This event is being reported pursuant to 10 CFR 50.73(a)(2XivXA) as an event that resulted in manual or automatic actuation of the reactor protection system and the auxiliary feedwater system.

This-event is being reported pursuant to 10CFR50.73(a)(2Xiv)(A) as an event that resulted in manual or automatic actuation of the reactor protection system and the auxiliary feedwater system.

2. Cause The cause of this event was determined to be vibration induced worn threads on the number 2 feedwater regulating valve (2-FW-51B) positioner beam screw.

3. Assessment of Safety Consequences The safety consequences associated with this event were very low. The reactor was manually tripped by operators when the number 2 S/G water level rose to 84.4% and the feedwater control system was not responding as expected. All control rods inserted into the reactor following the trip.

There was no safety injection system actuation. There was no significant increase in core power prior to the manual reactor trip. Neither the departure from nucleate boiling or fuel centerline melt fuel design limits were challenged. As such, there were no challenges to the fuel, reactor coolant system or containment fission product barriers.

NRC 'FORM 366A (9-2007)

  • 4. Corrective Action The following compensatory actions have been completed:
  • The degraded feedwater regulating valve successfully retested and returned to service on May 23, 2010.
  • The on-line preventative maintenance frequency has been increased for installed feedwater regulating valve positioners to improve reliability.

Long term corrective actions:

  • Design changes are being evaluated to reduce FRV positioner beam screw wear.

Additional corrective actions are being taken in accordance with the station's corrective action program.

5. Previous Occurrences No previous similar events/conditions were identified.

Energy Industry Identification System (ElIS) codes are identified in the-text as [XX]