05000324/FIN-2011003-01
From kanterella
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Failure To Adequately Evaluate And Correct A Condition Adverse To Quality Involving A Manufacturing Defect Of Barton Model 199 Dual Dampener Differential Pressure Units |
Description | A self revealing non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action was identified for failure to promptly correct a condition adverse to quality regarding a manufacturing defect of a Barton Model 199 dual dampener differential pressure unit (DPU) used in the 1B residual heat removal (RHR) loop. Specifically, the licensee failed to replace the DPU after the vendor determined that the manufacturing process was incorrect and could lead to a slow response of the component in safety-related applications. This led to a failure of the RHR system 1B loop minimum flow bypass valve, 1-E11-F007B, to operate on February 18, 2011. The failure of the defective DPU was tracked as NCR 448471 in the corrective action program, and the licensee replaced the defective DPU. The inspectors determined that the licensees failure to promptly correct a condition adverse to quality regarding a manufacturing defect for Barton Model 199 dual dampener DPUs was a performance deficiency. The finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems Cornerstone and adversely affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, the corrosion buildup in the DPU used in the control of the position of the minimum flow bypass valve for the 1B RHR loop had degraded, such that the availability and reliability of the 1B RHR loop was adversely affected. This finding was evaluated using Inspection Manual Chapter 0609, Significance Determination Process, Phase 1 Worksheet for mitigating systems. The finding required phase two and phase three SDP analyses by a regional Senior Reactor Analyst (SRA) because the 1B loop of RHR was assumed to be inoperable for longer than its Technical Specifications (TS) allowed outage time. The SRA performed a phase three analysis using the NRCs site-specific risk model. Common cause factors were not propagated to the other loop of RHR during the modeling because of the prior instrument changes in the other loop. Operator recovery for the impact of the failed instrument was deemed to be credible, because the valves hand switch remained functional, and was evaluated using the SPAR-H methodology. The short duration of non-functionality since the last known proper functioning of the instrument, combined with the high likelihood of operator recovery, and the lack of an increase in common cause failures resulted in a finding that is characterized as Green. This finding does not have a cross-cutting aspect because the performance deficiency occurred greater than three years ago and does not reflect current licensee performance. |
Site: | Brunswick |
---|---|
Report | IR 05000324/2011003 Section 4OA5 |
Date counted | Jun 30, 2011 (2011Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | |
Inspectors (proximate) | A Minarik A Nielsen G Kolcum M Speck P O'Bryan R Musser |
INPO aspect | |
' | |
Finding - Brunswick - IR 05000324/2011003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Brunswick) @ 2011Q2
Self-Identified List (Brunswick)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||