05000323/LER-2006-002, Re Steam Generator Tube Plugging Due to Stress Corrosion Cracking

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Re Steam Generator Tube Plugging Due to Stress Corrosion Cracking
ML061450136
Person / Time
Site: Diablo Canyon Pacific Gas & Electric icon.png
Issue date: 05/19/2006
From: Becker J
Pacific Gas & Electric Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
DCL-06-068 LER 06-002-00
Download: ML061450136 (7)


LER-2006-002, Re Steam Generator Tube Plugging Due to Stress Corrosion Cracking
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(ii)

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
3232006002R00 - NRC Website

text

W Pacific Gas and Electric Company-James R. Becker Diablo Canyon Power Plant Vice President P. 0. Box 56 Diablo Canyon Operations and Avila Beach, CA 93424 Station Director 805.545.3462 May 19, 2006 Fax: 805.545.4234 PG&E Letter DCL-06-068 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Docket No. 50-323, OL-DPR-82 Diablo Canyon Unit 2 Licensee Event Report 2-2006-002-00 Steam Generator Tube Plugging Due to Stress Corrosion Cracking

Dear Commissioners and Staff:

In accordance with Technical Specification (TS) 5.6.10.a, TS 5.6.10.c, and 10 CFR 50.73(a)(2)(ii), Pacific Gas & Electric Company is submitting the enclosed Licensee Event Report regarding steam generator (SG) tube plugging due to stress corrosion cracking identified during the Unit 2 Thirteenth Refueling Outage. TS 5.6.10.c requires a special report since more than one percent of the tubes inspected in SG 2-4 were identified as defective, and TS 5.6.10.a requires reporting of the number of tubes plugged in each SG.

This event did not adversely affect the health and safety of the public.

Since ly, James R. Be cker ddm/2246/A0665987 Enclosure cc:

Bruce S. Mallett, NRC Region IV Terry W. Jackson, NRC Senior Resident Inspector Alan B. Wang, NRR Project Manager Diablo Distribution INPO State of California, Pressure Vessel Unit A member of the STARS (Strategic Teaming and Resource Sharing) Alliance CaLtaway

  • Comanche Peak
  • Diablo Canyon
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LICENSEE EVENT REPORT (LER)

FACILITY NAME (1)

DOCKET NUMBER (2)

PAGE (3 Diablo Canyon Unit 2

°0l 5 0 1 010 1 3 2l 3 1 i OF l 6 TITLE (4)

Steam Generator Tube Plugging Due to Stress Corrosion Cracking EVENT LER NUMBER (6)

REPORT OTHER FACILITIES INVOLVED (8)

DATE (5)

DATE (7)

MO DAY YEAR YEAR SEQUENTIAL NUMBER REVISION MO DAY YEAR FACILITY NAME DOCKET NUMBER I

I I ~NUMBER II 05 0 2006 2006 - 0 0 l 2 l- 0 0 05 19 2006 OPERATING

_ THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR (11)

MODE (9)

X 10 CFR 50.73(a)(2)(ii)(A)

POWERS LEVEL 10 X

OTHER Special Report perTS 5.6.10.a and c l0 (SPECIFY IN ABSTRACT BELOW AND IN TEXT, NRC FORM 366A)

LICENSEE CONTACT FOR THIS LER (12)

TELEPHONE NUMBER AREA CODE 1 Lawrence M. Parker - Senior Regulatory Services Engineer 805 1545-3386 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

CAUSE

SYSTEM COMPONENT MANUFACTURER REPORTABLE

CAUSE

SYSTEM COMPONENT MANUFACTURER REPORTABLE TO EPIX TO EPIX B A I SIGI I W111210 N

I III I I SUPPLEMENTAL REPORT EXPECTED(14)

ExPECTED MON

[]YES (If yes, complete EXPECTED SUBMISSION DATE) p] NO SUBMISSION DATE (15)

ABSTRACT (Liit tO 1400 spaces. I e., appm.xintely 15 sifle-spacea typewritten lines.) (16)

On May 3, 2006, at 0214 PDT, with Unit 2 in Mode 6 (refueling, with the reactor defueled), analysis of eddy current testing on Steam Generator (SG) 2-4 indicated that greater than one percent of the tubes were defective. Pacific Gas and Electric Company (PG&E) made a nonemergency report to the NRC as required by Technical Specification (TS) Table 5.5.9-2, 'Steam Generator (SG)

Tube Inspection," at 0928 PDT, via NRC Event 42547.

On May 3, 2006, PG&E discussed the preliminary results of the SG eddy current inspection during a phone conference with the Office of Nuclear Reactor Regulation. The primary cause of the SG tube cracking was axial outside diameter stress corrosion cracking at the hot leg tube support plates.

In accordance with TS 5.5.9, "Steam Generator (SG) Tube Surveillance Program," PG&E has plugged all defective Unit 2 tubes identified during the current refueling outage. All defective tubes met condition-monitoring

- requirements at the end of Cycle 13. PG&E maintains a comprehensive program to minimize SG tube degradation, and plans to replace the Unit 2 SGs at the end of Cycle 14.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER NUMBER Diablo Canyon Unit 2 0 5 0 0 0 l 3 2 3 2006

0. 0 0 2

0 l 0 2

OF 6

TEXT I.

Plant Conditions

Unit 2 was in Mode 6 (refueling, with the reactor defueled) in its Thirteenth Refueling Outage (2R13).

II.

Description of Problem A.

Background

Technical Specification (TS) 5.5.9, "Steam Generator (SG) Tube Surveillance Program," requires that the results of each SG tube inspection be classified as Category C-3 if more than one percent of the total tubes inspected are defective. Defective tubes have service induced degradation in excess of TS tube repair limits. Defective tubes must be removed from service by plugging.

TS 5.6.10, "Steam Generator (SG) Tube Inspection Report," paragraph a, requires the number of tubes plugged in each SG [AB][TBG] to be reported within 15 days following the completion of each inservice inspection. TS 5.6.10, paragraph c, requires the results of SG tube inspections, which fall into Category C-3, to be reported in a special report to the Commission within 30 days and prior to resumption of plant operation.

If the results of the SG tube inspections are classified as Category C-3, then NRC notification is required in accordance with TS Table 5.5.9-2, "Steam Generator (SG) Tube Inspection," and submittal of a special report is required in accordance with TS 5.6.10.c.

B.

Event Description

On May 3, 2006, at 0214 PDT, final analysis of eddy current testing on SG 2-4 indicated that greater than one percent of the tubes inspected were defective, therefore, classifying the SG as Category C-3, per TS 5.5.9. SG 2-4 had 34 defective tubes that were removed from service by tube plugging during 2R1 3. An additional degraded tube was also preventively plugged.

On May 3, 2006, a nonemergency report was made in accordance with TS Table 5.5.9-2 at 0928 PDT.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER REVISION NUMBER Diablo Canyon Unit2 0 T5 0 l 0 l 0 l 3 12 1 3 2006 0

0 2

0 0 1 31 OF 6

TEXT On May 3, 2006, Pacific Gas and Electric Company (PG&E) discussed the results of the inspection during a scheduled phone conference with the Office of Nuclear Reactor Regulation at approximately 1000 PDT.

C.

Status of Inoperable Structures, Systems, or Components that Contributed to the Event None.

D.

Other Systems or Secondary Functions Affected

None.

E.

Method of Discovery

The defective tubes were found during routine scheduled eddy current testing of Unit 2 SG tubing performed during 2R13.

F.

Operator Actions

None.

G.

Safety System Responses None.

Ill.

Cause of the Problem A.

The number of defective tubes in SG 2-4 identified during 2R13 exceeded one percent of the total tubes inspected, placing the SG in Category C-3, per TS 5.5.9.

B.

Root Cause The majority of the tube defects are attributed to axial outside diameter stress corrosion cracking (ODSCC) at the hot leg tube support plates.

C.

Contributory Cause None.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER REVISION Diablo Canyon Unit2 0 1510 0 l 0 l 3 12 l 3 2006 0 0 2

0 0 4

OF l 6 TEXT IV.

Assessment of Safety Consequences

The licensing-basis, large-break, loss-of-coolant accident analysis assumes a tube-plugging limit of 15 percent per SG. Including the tubes plugged during 2R1 3, the following table presents the number of tubes (out of a total of 3,388 tubes for each SG) that are currently plugged in each of the four Unit 2 SGs.

SG Tubes Plugged in Total Tubes Total Percentage of No.

2R13 Plugged to Date Tubes Plugged 2-1 6

125 3.7 2-2 23 268 7.9 2-3 6

130 3.8 2-4 35 367 10.8 The plugging percentage for each Unit 2 SG remains within the current allowable limit of 15 percent.

There were no actual safety consequences involved in this event since all defective tubes met the performance criteria of the Nuclear Energy Institute (NEI) 97-06, Revision 2, "Steam Generator Program Guidelines."

Also, the condition is not considered a Safety System Functional Failure.

Therefore, the event is not considered risk significant, and it did not adversely affect the health and safety of the public.

V.

Corrective Actions

A.

Immediate Corrective Actions

The Unit 2 SG tubes classified as defective during 2R1 3 have been plugged in accordance with Diablo Canyon Power Plant (DCPP) TS 5.5.9.

B.

Corrective Actions to Prevent Recurrence PG&E has initiated several programs to minimize SG tube degradation and implemented alternate repair criteria (ARC) to leave certain indications in service, thus extending the SG service life.

PG&E maintains a comprehensive program to minimize SG tube degradation, and plans to replace the Unit 2 SGs at the end of Cycle 14.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1)

DOCKET NUMBER (2)

LER NUMBER (6)

PAGE (3)

YEAR SEQUENTIAL NUMBER REVISION NUMBER DiabloCanyonUnit20 51 0 13 21 3 2006 0 1 2 0- 00 5

OFa6 TEXT Secondary side initiatives to minimize tube degradation:

1.

EPRI secondary chemistry recommendations were implemented to minimize ODSCC at tube support plates (TSPs) (e.g., hydrazine levels were increased in 1992, the secondary side pH treatment was converted from ammonia to ethanol amine, and a molar ratio control program was implemented in 1993 and 1994).

2.

Tube sheets have been sludge lanced during each prior refueling outage to minimize ODSCC at the tube sheet.

3.

DCPP has an upgraded plant makeup water system to minimize SG contaminate levels.

4.

SG blowdown is maintained at approximately one percent of the main steaming rate to minimize SG contaminate levels.

5.

A boric acid addition program is in effect, including boric acid soaks at startup to mitigate denting and ODSCC at TSPs.

6.
  • DCPP has condensate polishers and emergency (plant curtailment) procedures to mitigate the consequences of any seawater condenser tube leaks.
7.

The SGs on both Units 1 and 2 were chemically cleaned in 2004.

Primary side initiatives to minimize tube degradation:

1.

Rows 1 and 2 U-bends were heat treated in 1987 and 1988 to prevent primary water stress corrosion cracking (PWSCC).

2.

The tubes in the hot leg tube sheet region were shot peened in 1992 and 1993 to minimize PWSCC.

3.

Reactor coolant system (RCS) contaminants are maintained at low levels in accordance with EPRI guidelines.

4.

Lithium and boron concentrations are coordinated to minimize pH swings in the RCS.

5.

Zinc addition to the RCS was implemented in Units 1 and 2 starting in Cycle 9 to inhibit PWSCC in SG tubes.

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Tea~

Alternate repair criteria (ARC):

1.

Voltage-based ARC for axial ODSCC at TSPs was implemented starting in the Unit 2 Eighth Refueling Outage (2R8) and the Unit 1 Ninth Refueling Outage (1 R9).

2.

W* ARC for axial PWSCC contained in the WEXTEX tube sheet was implemented starting in 1 R9 and the Unit 2 Ninth Refueling Outage.

3.

PWSCC ARC for axial PWSCC at dented TSPs was implemented starting in the Unit 1 Eleventh Refueling Outage and the Unit 2 Eleventh Refueling Outage,(2R1 1).

VI.

Additional Information

A.

Failed Components Component:

SG tubes (Series 51 SG)

Manufacturer:

Westinghouse B.

Previous Similar Events

Licensee Event Report (LER) 2-96-003, submitted via DCL-96-105, dated March 13, 1996, reported that greater than one percent of the tubes inspected in SG 2-1, SG 2-2, and SG 2-4, during the Unit 2 Seventh Refueling Outage, were defective.

LER 2-1998-002-00, submitted via DCL-98-041, dated March 19,1998, reported that greater than one percent of the tubes inspected in SG 2-2, during 2R8, were defective.

LER 2-2003-001-00, submitted via DCL-03-031, dated March 14,2003, reported that greater than one percent of the tubes inspected in SG 2-4, during 2R1, weredefective. The defects were due to ODSCC at the TSP intersections and exceeded the conditional burst probability reporting threshold of 0.01. PG&E also informed the NRC that circumferential indications were detected in Row 3 to Row 10 U-bends.