05000321/LER-2004-003
Edwin I. Hatch Nuclear Plant - Unit 1 | |
Event date: | 3-03-2004 |
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Report date: | 4-28-2004 |
Reporting criterion: | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
3212004003R00 - NRC Website | |
U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) DOCKET LER NUMBER (6) PAGE (3)
PLANT AND SYSTEM IDENTIFICATION
General Electric - Boiling Water Reactor Energy Industry Identification System codes are identified in the text as (EIIS Code XX).
DESCRIPTION OF EVENT
On March 3, 2004 at 1345 EST, the 'swing' (1B) emergency diesel generator (DG) started unexpectedly during the planned removal of the normal supply breaker for the IF 4160 VAC emergency bus (1R22-S006, Frame 11) (EIIS Code EB). A problem with the shutter in this breaker cubicle caused it to become hung up on the breaker when it was being removed from the cubicle. This caused the shutter linkage to depress the Mechanism Operated Cell (MOC) switch, which in turn caused an undervoltage signal to be generated, starting the 'swing' DG (EDG, EIIS Code EK). The shutter problem was caused by inadequate procedures that did not ensure there would be no interferences with the shutter assembly during the installation and racking in of the breaker.
The event was the result of the shutter assembly for the normal supply breaker for the 1F 4160 VAC emergency bus (1R22-S006, Frame 11) becoming hung on the conductor fingers of the breaker as it was being racked out. When the breaker was subsequently being removed from the cubicle, the front of the shutter linkage arm (used to raise or lower the shutter) pivoted downward until it momentarily depressed the Mechanism Operated Cell (MOC) switch. The logic interpreted the depression of the MOC switch as the normal supply breaker being closed in. This caused the alternate supply breaker to trip. With the normal supply breaker being removed from the cubicle and the alternate supply breaker tripped, the 'swing' DG started on a bus undervoltage signal. As the breaker continued to be removed from the cubicle, the shutter became free from the breaker's conductor fingers and fell back into the cubicle releasing the MOC switch. The release of the MOC switch permitted the alternate supply breaker to re-close before the DG output breaker tied to the de-energized bus.
The shutters for the 4160 VAC breakers are raised when the breakers are installed and are lowered when the breakers are removed from their cubicles. It was determined from an inspection of the shutter involved in this event that the C-channel (which functions as a guide for the shutter as it is raised or lowered during breaker installation or removal) was deformed in two locations. The location of these C-channel deformations coincided with where the cubicle's fixed pins contacted the C- channel when the breaker was installed in the cubicle (i.e., the shutter was in the raised position). The location and type of C-channel deformations led to the conclusion that the shutter had been pried off of the fixed pins while it was in the raised position.
An investigation of the event concluded that a breaker previously installed in this cubicle had either a mounting bolt or L-bracket (used for fastening the barrier to the side of the breaker) installed improperly, causing an interference with the slotted bracket for the shutter linkage arm. This interference caused the slotted bracket attached to the shutter C-channel to become bent while prying FACILITY NAME (1) _ DOCKET _ LER NUMBER (6) _ PAGE (3) Edwin I. Hatch Nuclear Plant - Unit 1 05000-321
- 1 _ SEQUENTIAL _ I REVISION off the C-channel from the lower fixed pin. The breaker that was installed during this event was inspected, and it was determined that it did not have the mounting bolt or L-bracket installed improperly. However, interviews with plant personnel revealed that there have been past instances where this L-bracket and mounting bolt assembly has been installed incorrectly. With the shutter off of this lower fixed pin, the shutter had more of a tendency to bind when being raised or lowered while the breaker was being racked in or out. It also permitted the shutter to tilt slightly. Both of these conditions made it more likely for the shutter to hang up on the breaker conductor fingers. It is concluded that this event occurred because the shutter did hang up on the fingers when the breaker was racked out, prying the shutter off of the top fixed pin. Subsequently, when the breaker was being removed from the cubicle, the shutter was pulled completely off the top fixed pin. Then as the shutter continued to be drawn out of the cubicle with the breaker its linkage arm was forced downward depressing the MOC switch. The fiberglass portion of the shutter resisted the movement out of the cubicle and eventually the shutter became free from the breaker fingers and fell to the floor releasing the MOC switch.
CAUSE OF EVENT
The shutter problem was caused by procedure omissions. The 4160 VAC switchgear Preventive Maintenance procedure did not require checks to ensure the shutter assembly travels freely and the C- channel is not deformed. Additionally, the procedure did not contain guidance for the installation of an L-bracket or mounting bolt that could interfere with the shutter linkage arm when the breaker is being put into the cubicle and subsequently racked in.
REPORTABILITY ANALYSIS AND SAFETY ASSESSMENT
This event is reportable per 10 CFR 50.73 (a)(2)(iv)(A) because an automatic actuation of a system listed in paragraph (a)(2)(iv)(B)(8) occurred. Specifically, the 'swing' DG automatically started from an undervoltage signal generated when the MOC switch for the normal supply breaker was depressed causing the alternate supply breaker to trip.
The Unit 1 Class lE AC Electrical Power Distribution System AC sources consist of the offsite power sources (preferred power sources, normal and alternate), and the onsite standby power sources (DGs 1A, 1B, and 1C). As required by 10 CFR 50, Appendix A, GDC 17, the design of the AC electrical power system provides independence and redundancy to ensure an available source of power to the Engineered Safety Feature (ESF) systems. The Class lE AC distribution system is divided into redundant load groups, so loss of any one group does not prevent the minimum safety functions from being performed. Each load group has connections to two preferred offsite power supplies and a single DG. Offsite power is supplied to the 230 kV and 500 kV switchyards from the transmission network by eight transmission lines. From the 230 kV switchyards, two electrically and physically separated circuits provide AC power, through startup auxiliary transformers 1C and 1 D, to 4160 VAC ESF buses 1E, IF, and 1G.
Startup auxiliary transformer (SAT) 1D provides the normal source of power to ESF buses 1E, 1F, and 1G. If any 4160 VAC ESF bus loses power, an automatic transfer from SAT ID to SAT 1C occurs.
The onsite standby power source for 4160 VAC ESF buses 1E, 1F, and 1G consists of three DGs. DGs 1A and 1C are dedicated to ESF buses lE and 1G, respectively. DG 1B (the 'swing' DG) is a shared power source and can supply either Unit 1 ESF bus 1F or Unit 2 ESF bus 2F. A DG starts automatically on a loss of coolant accident (LOCA) signal (i.e., low reactor water level signal or high drywell pressure signal) or on an ESF bus degraded voltage or undervoltage signal. After the DG has started, it automatically ties to its respective bus after offsite power is tripped as a consequence of ESF bus undervoltage or degraded voltage, independent of or coincident with a LOCA signal.
In this event, the logic interpreted the depression of the MOC switch as the normal supply breaker being closed in. This caused the alternate supply breaker to trip. With the normal supply breaker being removed from the cubicle and the alternate supply breaker tripped, the 'swing' DG started on a bus undervoltage signal. As the breaker continued to be removed from the cubicle, the shutter became free from the breaker's conductor fingers and fell back into the cubicle releasing the MOC switch. The release of the MOC switch permitted the alternate supply breaker to re-close before the DG output breaker tied to the de-energized bus. .
In this event, all components and systems functioned as designed, given the momentary bus undervoltage signal generated. During this event, the 'swing' DG remained operable (with the exception of approximately 5 minutes while the DG was being barred over after being shutdown) and was capable of supplying power to the bus if the normal and alternate source of power to the bus remained unavailable. Based on this analysis, it is concluded that this event did not adversely affect nuclear safety.
CORRECTIVE ACTIONS
Unit 1's 4160 VAC breakers were inspected (without removing the breaker from the cubicle) and the gap between the breaker and the slotted bracket where the shutter linkage arm inserts was visually estimated. Of the breaker cubicles inspected, some damage was observed on four of the shutters. Two of the shutters were inspected further and Maintenance Engineering determined that the C-channels for the shutters were acceptable.
Unit 2's 4160 VAC breakers will be inspected (without removing the breaker from the cubicle) and any anomalies for the shutter assemblies will be noted. This action will be completed by June 30, 2004.
and any identified during the Unit 2 inspections). The tags will require that an electrician witness the removal of the breakers from their cubicle. The electrician will ensure that the shutter linkage arm FACILITY NAME (1
DOCKET
05000-321 LER NUMBER (6) 2004 -- 003 -- 0 does not move downward toward the MOC switch when these breakers are removed from their cubicles. This action will be completed by June 30, 2004.
Maintenance personnel involved in removing breakers from cubicles have been made aware of this 'event (by a shop bulletin) to ensure that the shutter linkage arm does not move downward toward the MOC switch when removing Unit 2 breakers from their cubicles before the June 2004 inspections are completed.
The 4160 VAC switchgear Preventive Maintenance procedure will be revised to require checks to ensure the shutter assembly travels freely and the C-channel is not deformed. Additionally, specific guidance will be added to the procedure concerning the installation of the L-bracket or mounting bolt that could interfere with the shutter linkage arm when the breaker is being put into the cubicle and subsequently racked in. This procedure revision will be completed by June 30, 2004.
ADDITIONAL INFORMATION
No systems other than those previously described in this report were affected by this event.
This LER does not contain any permanent licensing commitments.
There were no previous similar events reported in the past two years in which a failure of a 4160 VAC breaker shutter assembly caused an unplanned safety system actuation.
Failed Component Information:
Master Parts List: 1R22-S006, Frame 11 Manufacturer: Westinghouse Manufacturer Code: W120 Model Number: 437D937 GY01 Type: Shutter Assembly EIIS System Code: EB EIIS Component Code: CAB Root Cause Code: D Reportable to EPIX: Yes