LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved |
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UPDATE REPORT PREVIOUS RFPORT DATE 11/13/79 N:C P M M 364 U O. NUCl.E AR 9238ULAT@AY COMMsE3aCN APPROVEO Y OMll l'd*,Q n LICENSEE EVENT REPORT 2150 8081 CONTROL BLOCK: l l
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n EVENT DESCRIPTION ANO FRO 3ABLE CONSEQUENCES b10 l o l2 l During normal unit 3 operation, the RER service water supply to the 2B RHR l
j o l 3 l l heat exchanger was isolated for maintenance. The isolation of the watar
______J jol4]l supply also isolated the standby coolant supply to unit 3 (T.S. 3 5.C.3 and l
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There was no hazard to the public health or safety. Previous j
lolsll occurrences: None.
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 l
[igoll Isolation of the unit 3 water a ly during unit 2 maintenance was caused by a lac l, j, l l of administrative control over system cross-connect valves. Upon error discovery, l i l 2 l l RHR heat exchanger 2B was returned to service within four hours and water supply j i l 3 l l restored. Administrative controls have' been improved.
Changes were made to Tech.;
I t I 4 I l Specs, to allow a 10-day standby coolant supply outage, i
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PHONE. 205 729-ORM 8400190207 840427 i
PDR ADOCK 05000296 L
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T nneIsea Vallcy Auth:rity Browns F;rry NuslGrr Plant LER SUPPLEMENTAL INFORMATION I
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- - BFRO-50-296/79005 R2 Technical Specification Involved 1.5.C.1 and 9.5.C.5
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Reported Under Technical Specification 6.7.2.A.2 l,
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Date of Occurrence 5/6/70 Time of Occurrence 1900 Unit 3
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Identificaiton and Descrintion of Occurrence l
The RRR service water supply to the 2B RHR heat exchanger was isolated for maintenance.
The isolation of the water supply also isolated the stardby I
ooolant supply to unit 3 l
Conditions Prior to Occurrence:
i Unit 2 - refueling outage in progress.
Unit 3 - operating normally at 755 power.
Action specified in the Technical Specification Surveillance Requirements met i
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due to inonerable ecuinment.
Describe
. Place the unit in cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Annarent Cause of Occurrence:
- - The isolation of the water supply for maintenance was the direct cause; however, lack of administrative controls over cross-connect valves was the proximate i
cause of the accident.
1 Annivsis of OccurreGC11 There was no hazard to the public health or safety.
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Corrective Action
l Upon discovery of the standby coolant supply isolation, action was immediately taken to restore the heat exchanger and the standby coolant was returned to j
service in four hours. The ' standby coolant supply valve was painted a i
distinctive color and strict administrative controls imposed on its operation.
A revision was made to the technical specification for standby coolant supply to allow removal of the standby coolant supply for up to 10 days. This allows ample time for performing maintenance during future outages.
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i Retention Period: Lifetime. Responsibility - Administrative Services h
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TENNESSEE VALLEY AUTHORITY Browns Ferry Nuclear Plant P. O. Box 2000 Decatur, Alabama 35602 April 27, 1984 3
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Mr. James P. O'Reilly, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303
Dear.Mr. O'Reilly:
TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT UNIT 3 - DOCKET NO. 50-296 - FACILITY OPERATING LICENSE DPR REPORTABLE OCCURRENCE REPORT BFRO-50-296/79005 R2 The enclosed report provides followup information concerning isolation of RHR service water supply to the 2B RHR heat exchanger for maintenance.
'This report is submitted in accordance with Browns Ferry Unit 3 Technical Specification 6.7.2.A.2.
Very truly yours, TENNESSEE VALLEY AUTHORITY ks
/)BrownsFerryNuclearPlant f
G. T. Jones Power Plant Superintendent Enclosure oo (Enclosure):
U. S. Nuclear Regulatory Commission Document Control Desk Washington D.C.
20555 NRC Inspector, Browns Ferry Nuclear Plant OFFICI AL COPI, 3
fAW I t An Equal Opportunity Employer p
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| 05000296/LER-1979-001-03, /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | /03L-0 on 790111:switch on LIS-3-56B Failed to Trip Reactor Recirculation Pump Motor Generator.Caused by Misadjusted Switch on Yarway Model 4418CE.Switch Recalibr & Tested Satisfactorily | | | 05000296/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000259/LER-1979-001, Forwards LER 79-001/01T-0 | Forwards LER 79-001/01T-0 | | | 05000259/LER-1979-001-01, /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | /01T-0 on 790118:reactor Scrammed Due to High Flux Actuating Intermediate Range Monitor high-high Neutron Monitoring Circuit;Reactor Neared Criticality.Caused by Withdrawal of High Reactivity Worth Rod | | | 05000260/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000260/LER-1979-001-03, /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | /03L-0 on 790113:during Test of high-pressure Injection Coolant Sys,Steam Supply Valve FCV-73-16 Failed to Open,Rendering Sys Inoperative.Caused by Failure of Limitorque Valve Operator Limit Switch | | | 05000296/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000259/LER-1979-002-03, /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | /03L-0 on 790129:during Normal Operation While Performing Surveillance Test,Standby Liquid Control Pump 1B Relief Valve Opened Below Tech Spec Min.Caused by Valve Seat Surface Deterioration | | | 05000259/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000260/LER-1979-002-03, /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | /03L-0 on 790203:alarm for Fire Protection Panel 25-236 Annunciated in Control Room.Panel Was Not Alarmed Condition.Caused by Normal End of Life Electrical Failure of Annunciator Point Card.Card Replaced & Sys Normalized | | | 05000260/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000296/LER-1979-002-03, /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | /03L-0 on 790117:during Maintenance of Reset Switch,Short Circuit Damaged Power Supply & Sensor Circuit Board,Rendering Fixed Spray Automatic Initiation Circuit for Fire Protection Inoperable | | | 05000296/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000259/LER-1979-003-01, /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | /01T-1 on 790120:during Cold Shutdown,Local Leak Rate Test Indicated Excessive Total Leakage.Caused by Leaking Valve Seating Surface in Eight Valves.Valves Repaired & Retested | | | 05000259/LER-1979-003, Forwards LER 79-003/01T-1 | Forwards LER 79-003/01T-1 | | | 05000260/LER-1979-003-01, /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | /01T-0 on 790214:rod Position Info Sys Power Supply Ps X-5 Failed,Causing Loss of Rod Position Indication in Bottom Half of Vertical Core Display.Caused by Failure of Cooling Fan in Trygon Model L5B6-70-OVS4989 | | | 05000259/LER-1979-003-03, /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | /03L-2 on 790120:during Cold Shutdown,Local Leak Rate Test Revealed Total Leakage Exceeded Allowable 60% La Per 24-h.Caused by Excessive Leakage of Valve Seating Surface.Eight Leaking Valves Were Repaired & Retested | | | 05000296/LER-1979-003-03, /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | /03L-0 on 790202:linear Heat Generation Rate Out of Tech Spec Limits.Caused by Operation Close to Limiting Values & Increase in Reactivity Due to Gadolina Burnup. Greater Margin to Limiting Value Will Be Maintained | | | 05000260/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000260/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000259/LER-1979-004-03, /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on | /03L-0 on 790227:during Normal Operation,Review of Surveillance Test Data Indicated Monthly Samples of Diesel Fuel Taken in Dec 1978 Have Not Been Analyzed.Caused by Loss of Samples in Transit.Will Try to Measure Samples on Site | | | 05000296/LER-1979-004-03, /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | /03L-0 on 790411:during Normal Operation,Heat Detector Alarmed & Would Not Clear.Alarm Would Have Masked Signals from Other Detector,Required to Be Operational.Caused by Personnel Damaging Detector | | | 05000260/LER-1979-004-03, /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | /03L-0 on 790414:reactor Bldg,Turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Failed Surveillance Test SI 4.8.B-4.3,Section 4e.Caused by Failure of Input Card for Radiation Monitor | | | 05000296/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved | | | 05000296/LER-1979-005-01, /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | /01T-1:on 790506,BHR Water Supply Isolation to 2B RHR Heat Exchanger Isolated Standby Coolant Supply to Unit 3.Caused by Lack of Administrative Control Over Sys Cross Connect Valves.Administrative Controls Have Been Improved | | | 05000259/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000259/LER-1979-005-03, /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | /03L-0 on 790225:reactor,turbine Bldg & Refueling Zone Vent Exhaust Monitor RM-90-250 Became Inoperable.Caused by Moisture Collection in Detector SC-2.-1.S.Detector Replaced & Moisture Removed | | | 05000260/LER-1979-005-03, /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | /03L-0 on 790419:broken Terminal Discovered on Shutdown Board D Battery.Cause Unknown.Affected Cells Replaced & Personnel Instructed in Proper Tightening Methods | | | 05000260/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000296/LER-1979-006-03, During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | During Normal Operation, Erratic Indication of Torus Hydrogen Sensor Observed. Hydrogen Sensor Replaced & Tested Satisfactory.Design Change Request Initiated | | | 05000296/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000259/LER-1979-006-03, /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | /03L-0 on 790228:reactor,turbine Bldg & Refueling Zone Ventilation Exhaust Monitor RM-90-250 Became Inoperable for 3.5-h.Caused by Moisture in SC-2B Detector & Leaking Flanges.Moisture Removed & Flanges Tightened | | | 05000259/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000260/LER-1979-006-03, /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | /03L-0 on 790427:prior to Refueling Shutdown, Drywell Prepurge Tritium Sample Not Taken.Caused by Lack of Understanding Between Operational & Lab Personnel.Operating Instructions Amended to Prevent Recurrence | | | 05000260/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000296/LER-1979-007-03, /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | /03L-0 on 790612:during Performance of Procedure SI 4.1.A-14,turbine First Stage Permissive Pressure Switches PS-1-81A & B & PS-1-91A & B Setpoints Exceeded Tech Specs. Caused by Setpoint Drift.Switches Recalibr | | | 05000260/LER-1979-007-03, /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | /03L-0 on 790503:during Refueling Outage,Five MSIVs Exceeded Leakage Limits.Caused by Irregularities on Valve Seating Surfaces & Entrapment of Debris Under Seating Surfaces.Valves Will Be Repaired & Retested | | | 05000260/LER-1979-008-01, /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | /01T-0 on 790504:while Preparing for Refueling Outage,Secondary Containment Integrity Was Not Conclusively Demonstrated Prior to Breaking Primary Containment.Test Improperly Performed Due to Personnel Error | | | 05000259/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000259/LER-1979-008-03, /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | /03L-0 on 790612:during Normal Operation, Pressure Switches PS-1-81 a & B & PS-1-91 a & B Setpoints Exceeded Tech Specs by 3-15 Psig. Caused by Model B2T-A12SS Switches Drifting | | | 05000296/LER-1979-008-03, /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | /03L-0 on 790627:no Speed Indication Noted on Reactor Core Isolation Coolant.Caused by Broken Wires to Magnetic Pickup EG-M Box.Wires Repaired | | | 05000260/LER-1979-008, Forwards LER 79-008/01T-0 | Forwards LER 79-008/01T-0 | | | 05000296/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000296/LER-1979-009-03, /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | /03L-0 on 790717:hydrogen Ignition Damaged HEPA Filters.Caused by Improper Offgas Recombiner Preheater Operation.Sys HEPA Filters & Charcoal Bed Inspected.Three Filters Replaced.Procedures Will Be Revised | | | 05000260/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000296/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | |
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