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Category:Letter
MONTHYEARIR 05000269/20240032024-10-31031 October 2024 Integrated Inspection Report 05000269/2024003 and 05000270/2024003 and 05000287/2024003 (2) ML24255A3322024-10-16016 October 2024 SLRA - Revised SE Letter ML24297A6172024-10-11011 October 2024 PCA Letter to NRC Oconee Hurricane Helene ML24269A0912024-10-0909 October 2024 Request for Withholding Information from Public Disclosure ML24145A1782024-08-26026 August 2024 Issuance of Amendment Nos. 430, 432, and 431, to TS 5.5.2, Containment Leakage Rate Testing Program for a one-time Extension of the Type a Leak Rate Test Frequency IR 05000269/20240052024-08-26026 August 2024 Updated Inspection Plan for Oconee Nuclear Station, Units 1, 2 and 3 (Report 05000269/2024005, 05000270/2024005, and 05000287-2024005) 05000287/LER-2024-001, Procedure Deficiency Results in Inadvertent Automatic Feedwater Isolation and Automatic Emergency Feedwater Actuation2024-08-0202 August 2024 Procedure Deficiency Results in Inadvertent Automatic Feedwater Isolation and Automatic Emergency Feedwater Actuation IR 05000269/20240022024-07-25025 July 2024 Integrated Inspection Report 05000269/2024002 and 05000270/2024002 and 05000287/2024002 ML24192A1312024-07-15015 July 2024 Licensed Operator Positive Fitness-For-Duty Test ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 ML24183A2352024-06-29029 June 2024 Update 3 to Interim Report Regarding a Potential Defect with Schneider Electric Medium Voltage Vr Type Circuit Breaker Part Number V5D4133Y000 ML24179A1102024-06-27027 June 2024 Submittal of Updated Final Safety Analysis Report Revision 30, Technical Specifications Bases Revisions, Selected Licensee Commitment Revisions, 10 CFR 50.59 Evaluation Summary Report, and 10 CFR 54.37 Update, and Notification ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc IR 05000269/20240012024-05-0303 May 2024 Integrated Inspection Report 05000269/2024001, 05000270/2024001 and 05000287/2024001 IR 05000269/20244022024-04-24024 April 2024 Security Baseline Inspection Report 05000269/2024402 and 05000270/2024402 and 05000287/2024402 ML24108A0792024-04-16016 April 2024 EN 57079 Paragon Energy Solutions Email Forwarding Part 21 Interim Report Re Potential Defect with Schneider Electric Medium Voltage Vr Type Circuit Breaker Part Number V5D4133Y000 IR 05000269/20244012024-03-28028 March 2024 – Security Baseline Inspection Report 05000269-2024401 and 05000270-2024401 and 05000287-2024401 ML24088A3052024-03-25025 March 2024 Fws to NRC, Agreement with Nlaa Determination for Tricolored Bat for Oconee Lr 05000270/LER-2023-001, Inappropriate Procedural Guidance for Planned Online Maintenance Results in Event or Condition That Could Have Prevented Fulfillment of a Safety Function Licensee2024-02-29029 February 2024 Inappropriate Procedural Guidance for Planned Online Maintenance Results in Event or Condition That Could Have Prevented Fulfillment of a Safety Function Licensee 05000287/LER-2023-002, Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications2024-02-29029 February 2024 Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications IR 05000269/20230062024-02-28028 February 2024 Annual Assessment Letter for Oconee Nuclear Station Units 1, 2 and 3 - (NRC Inspection Report 05000269/2023006, 05000270/2023006, and 05000287/2023006) ML24045A3042024-02-16016 February 2024 Ltr. to Lisa M. Collins Chief the Wassamasaw Tribe of Varnertown Indians Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24030A0052024-02-16016 February 2024 Ltr. to Brian Harris, Chief, Catawba Indian Nation; Re., Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A2942024-02-16016 February 2024 Ltr. to Carolyn Chavis Bolton Chief Pee Dee Indian Nation of Upper Sc Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A2962024-02-16016 February 2024 Ltr. to David Hill Principal Chief Muscogee Creek Nation Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A2992024-02-16016 February 2024 Ltr. to Eric Pratt Chief the Santee Indian Organization Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3082024-02-16016 February 2024 Ltr. to Ralph Oxendine Chief Sumter Tribe of Cheraw Indians Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3022024-02-16016 February 2024 Ltr. to Joe Bunch United Keetoowah Band of Cherokee Indians in Ok Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3072024-02-16016 February 2024 Ltr. to Pete Parr Chief Pee Dee Indian Tribe Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3032024-02-16016 February 2024 Ltr. to John Creel Chief Edisto Natchez-Kusso Tribe of Sc Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3012024-02-16016 February 2024 Ltr. to Harold Hatcher Chief the Waccamaw Indian People Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A2952024-02-16016 February 2024 Ltr. to Chuck Hoskin, Jr, Principal Chief Cherokee Nation Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A2972024-02-16016 February 2024 Ltr. to Dexter Sharp Chief Piedmont American Indian Assoc Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3052024-02-16016 February 2024 Ltr. to Louis Chavis Chief Beaver Creek Indians Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24045A3062024-02-16016 February 2024 Ltr. to Michell Hicks, Principal Chief Eastern Band of Cherokee Re Oconee Nuclear Station Units 1,2, and 3 Section 106 ML24019A1442024-02-13013 February 2024 Letter to Reid Nelson, Executive Director, Achp; Re Oconee Nuclear Station Units 1, 2, and 3 Section 106 ML24011A1532024-02-13013 February 2024 Letter to Tracy Watson EPA-Oconee Nuclear Sta, Unites 1, 2 & 3 Notice of Avail of the Draft Site-Specific Supp. 2, 2nd Renewal to the Generic EIS for Lic. Renew of Nuclear Plants ML24030A5212024-02-13013 February 2024 Letter to Elizabeth Johnson, Director, SHPO; Re Oconee Nuclear Stations Units 1, 2, and 3 Section 106 ML24011A1482024-02-13013 February 2024 Letter to Steven M. Snider-Oconee Nuclear Sta, Unites 1,2 & 3 Notice of Avail of the Draft Site-Specific Supp. 2, 2nd Renewal to the Generic EIS for Lic. Renew of Nuclear Plants IR 05000269/20230042024-02-13013 February 2024 Integrated Inspection Report 05000269/2023004, 05000270/2023004, and 05000287/2023004; and Inspection Report 07200040/2023001 ML23304A1422024-02-0101 February 2024 Issuance of Environmental Scoping Summary Report Associated with the U.S. Nuclear Regulatory Commission Staff’S Review of the Oconee Nuclear Station, Units 1, 2, & 3, Subsequent License Renewal Application ML24005A2492024-01-24024 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting) IR 05000269/20243012024-01-11011 January 2024 Notification of Licensed Operator Initial Examination 05000269/2024301, 05000270/2024301, and 05000287/2024301 ML23331A7982023-12-14014 December 2023 Review of the Fall 2022 Steam Generator Tube Inspection Report (01R32) ML23262A9672023-12-13013 December 2023 Alternative to Use RR-22-0174, Risk-Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems Section XI, Division 1 ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000269/20230032023-11-14014 November 2023 Integrated Inspection Report 05000269/2023003, 05000270/2023003, and 05000287/2023003; and IR 07200040/2023001; and Exercise of Enforcement Discretion ML23219A1402023-10-10010 October 2023 Audit Report Proposed Alternative to Use ASME Code Case N-752, Risk Informed Categorization and Treatment for Repair/Replacement Activities in Class 2 and 3 Systems XI, Division 1 ML23269A1102023-10-0606 October 2023 Letter to Steven Snider-Revised Schedule for the Environmental Review of the Oconee Nuclear Station, Unit 1, 2, and 3, Subsequent License Renewal Application ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds 2024-08-26
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000287/LER-2024-001, Procedure Deficiency Results in Inadvertent Automatic Feedwater Isolation and Automatic Emergency Feedwater Actuation2024-08-0202 August 2024 Procedure Deficiency Results in Inadvertent Automatic Feedwater Isolation and Automatic Emergency Feedwater Actuation 05000270/LER-2023-001, Inappropriate Procedural Guidance for Planned Online Maintenance Results in Event or Condition That Could Have Prevented Fulfillment of a Safety Function Licensee2024-02-29029 February 2024 Inappropriate Procedural Guidance for Planned Online Maintenance Results in Event or Condition That Could Have Prevented Fulfillment of a Safety Function Licensee 05000287/LER-2023-002, Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications2024-02-29029 February 2024 Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications 05000287/LER-2023-001, Condition Prohibited by Technical Specifications Due to Isolation Valve Exceeding Inservice Testing Leakage Requirements2023-03-0909 March 2023 Condition Prohibited by Technical Specifications Due to Isolation Valve Exceeding Inservice Testing Leakage Requirements 05000269/LER-1922-002, Reactor Coolant Oconee Nuclear Station, Unit 1, System Pressure Boundary Leak on Reactor Coolant Pump Lower Bearing Thermowell2023-01-12012 January 2023 Reactor Coolant Oconee Nuclear Station, Unit 1, System Pressure Boundary Leak on Reactor Coolant Pump Lower Bearing Thermowell 05000269/LER-2022-001, Ultrasonic Examination Indications Identifies Degraded Reactor Coolant System Pressure Boundary2022-12-21021 December 2022 Ultrasonic Examination Indications Identifies Degraded Reactor Coolant System Pressure Boundary 05000287/LER-2022-002, Automatic Actuation of Emergency Feedwater System Due to Malfunctioning Startup Feedwater Control Valve2022-07-0101 July 2022 Automatic Actuation of Emergency Feedwater System Due to Malfunctioning Startup Feedwater Control Valve 05000270/LER-2022-003, Manual Reactor Trip Due to Main Feedwater Control Valve Positioner Malfunction2022-04-21021 April 2022 Manual Reactor Trip Due to Main Feedwater Control Valve Positioner Malfunction 05000270/LER-2022-002, Regarding Automatic Actuation of Emergency Feedwater System Due to Main Feedwater Pump Malfunction2022-04-14014 April 2022 Regarding Automatic Actuation of Emergency Feedwater System Due to Main Feedwater Pump Malfunction 05000270/LER-2022-001, Regarding Automatic Reactor Trip Due to Loss of Power to Reactor Coolant Pumps2022-04-0606 April 2022 Regarding Automatic Reactor Trip Due to Loss of Power to Reactor Coolant Pumps 05000287/LER-2022-001, Response Actions Resulted in Brief Inoperability of Both Onsite and Offsite Emergency AC Power Paths2022-03-28028 March 2022 Response Actions Resulted in Brief Inoperability of Both Onsite and Offsite Emergency AC Power Paths 05000270/LER-2021-005, Automatic Reactor Trip Due to Spurious Trip Signal Concurrent with System Testing2022-02-0808 February 2022 Automatic Reactor Trip Due to Spurious Trip Signal Concurrent with System Testing 05000270/LER-2021-004, More than One Axial Power Shaping Rod Not Aligned within Technical Specification Limits2022-02-0707 February 2022 More than One Axial Power Shaping Rod Not Aligned within Technical Specification Limits 05000270/LER-2021-003, Conditions Prohibited by Technical Specifications Due to Ssf and Psw Inoperability2022-02-0707 February 2022 Conditions Prohibited by Technical Specifications Due to Ssf and Psw Inoperability 05000270/LER-2021-002, Actuation of the Keowee Hydroelectric Station Due to Loss of AC Power to the Unit 2 Main Feeder Buses2022-01-26026 January 2022 Actuation of the Keowee Hydroelectric Station Due to Loss of AC Power to the Unit 2 Main Feeder Buses 05000270/LER-2021-001, B Motor Driven Emergency Feedwater Pump Past Inoperability Resulted in Condition Prohibited by Technical Specifications2021-10-0404 October 2021 B Motor Driven Emergency Feedwater Pump Past Inoperability Resulted in Condition Prohibited by Technical Specifications 05000287/LER-2017-0012017-09-20020 September 2017 Unit 3 Reactor Protection System Actuation - Reactor Trip due to Turbine Trip from Generator Lockout, LER 17-001-00 for Oconee Nuclear Station, Unit 3, Regarding Reactor Protection System Actuation - Reactor Trip due to Turbine Trip from Generator Lockout 05000287/LER-2016-0012016-08-26026 August 2016 1 of 3, LER 16-001-00 for Oconee, Unit 3, Regarding Reactor Building Cooling Unit Inoperability Exceeds Technical Specification Completion Time 05000269/LER-2016-0012016-05-0505 May 2016 1 of 3, LER 16-001-00 for Oconee Nuclear Station, Unit 1, Regarding RPS Actuation - Unit 1 Reactor Trip Initiated by a Generator Lockout/Turbine Trip ML11364A0462011-12-23023 December 2011 Special Report Per Technical Specification 5.6.6, Problem Investigation Process Nos.: 0-11-13855, 0-11-14092 ML12006A1922011-12-19019 December 2011 LER 11-03-001 for Oconee, Units 1, 2, and 3 Regarding Inoperability of the Standby Shutdown Facility Diesel Generator ML0932902002009-11-18018 November 2009 10 CFR 71.95 Report of Non-Compliance with Certificate of Compliance USA/9319/B(U)F-96, Revision, for the Model No. MAP-12/MAP-13 Package ML0534104592005-12-0101 December 2005 Special Report Per Selected Licensee Commitment 16.9.9, Problem Investigation Process No.: O-05-7215 for Oconee Regarding the Inoperability of the Station Auxiliary Service Water (Asw) System and the Stand-by Shutdown Facility (Ssf) Asw Sys ML0426503832004-09-0909 September 2004 LER 04-02-001 for Oconee Nuclear Station Re Main Steam Line Break Mitigation Design/Analysis Deficiency ML0313204452003-04-24024 April 2003 LER 03-S01-00 for Oconee, Units 1, 2 & 3 Re Security Access Revoked for Falsification of Criminal Record ML0232303392002-11-12012 November 2002 LER 02-S02-00 for Oconee Nuclear Station Regarding Uncontrolled Safeguards Information ML0215802872002-05-28028 May 2002 LER 2002-02-00 Re Potential for Fire to Indirectly Damage Mitigation Component for Oconee Nuclear Station Unit 1 ML0211201432002-04-0909 April 2002 LER 02-01-00 for Oconee Nuclear Station Unit 1 Re Security Access Revoked for Falsification of Criminal Record 2024-08-02
[Table view] |
LER-2023-002, Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications |
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text
David A. Wilson Manager, Nuclear Support Services Oconee Nuclear Station
Duke Energy ON01SC l 7800 Rochester Hwy Seneca, SC 29672
o. 864.873.3451 f: 864.873.5791 David.Wilson2@duke-energy.com
RA-2 4-0 071
February 29, 202 4 10 CFR 50.73
Attn: Document Control Desk U. S. Nuclear Regulatory Commission 11555 Rockville Pike Rockville, MD 20852-2746
Duke Energy Carolinas, LLC Oconee Nuclear Station Unit 3 Docket Number: 50-2 87 Renewed Operating License: DPR-55
Subject: Licensee Event Report 287/2023-002, Revision 00 - Passive Containment Isolation Device Inoperability Results in Operation or Condition Prohibited by Technical Specifications
Licensee Event Report 287/ 202 3-002, Revision 00, is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
There are no regulatory commitments associated with this LER.
If there are questions, or further information is needed, contact Laura Boyce, Regulatory Affairs, at (864) 873-6774.
Sincerely,
David A. Wilson Manager, Nuclear Support Services Oconee Nuclear Station
Enclosure: Licensee Event Report 287-2023 -0 02 Rev.00
RA-2 4-0 071 February 29, 202 4 Page 2
cc (w/Enclosure):
Ms. Laura Dudes, Administrator, Region II U.S. Nuclear Regulatory Commission Marquis One Tower 245 Peachtree Center Ave., NE, Suite 1200 Atlanta, GA 30303-1257
Mr. Shawn Williams, Project Manager U.S. Nuclear Regulatory Commission 11555 Rockville Pike Mail Stop O-08B1A Rockville, MD 20852-2738
Mr. Jared Nadel NRC Senior Resident Inspector Oconee Nuclear Station
Abstract
On June 22, 2023, Oconee Unit 3 was operating at approximately 100 percent power. At approximately 22:50 Eastern Daylight Time (EDT), an unexpected increase in Unit 3 Reactor Building Normal Sump (RBNS) input rate was identified. The source of the Unit 3 RBNS input was identified at approximately 21:45 EDT on June 24, 2023, as a 3/4-inch instrument line broken upstream of normally closed instrument valve 3LPS-IV-0081. The direct cause is associated with the physical failure of a short section of 3/4 inch carbon steel instrument piping due to internal corrosion of the carbon steel piping at a carbon steel (CS) to stainless steel (SS) weld. The most probable cause of the failure was a deficiency in either the design scope or implementation of a 1998 Engineering Change; resulting in small segments of small-bore CS instrument piping not being replaced with SS as intended.
Immediate corrective actions included: replacing piping configuration at 3LPS-IV-0081 to resolve the leak and performing an extent of condition (EOC) review to identify additional small-bore instrument piping locations with CS to SS welds. Planned corrective actions include installation of alternate piping configurations for components with CS to SS welds identified during EOC review and revision of design documentation to reflect existing stainless steel pipe configurations.
Energy Industry Identification System (EIIS) codes are identified in text as [XX].
BACKGROUND
The Low Pressure Service Water (LPSW) system [BI, KG] provides cooling for essential and non-essential components in the Turbine Building (TB)[NM], Auxiliary Building (AB)[NF], and the Reactor Building (RB)[NH] and is required to be operable per Technical Specification (TS) 3.7.7. Unit 3 has two LPSW pumps which can supply multiple combinations of pathways.
One of the non-essential cooling functions performed by the LPSW system is to provide cooling water to the Reactor Coolant Pump (RCP) motor coolers [KG]. A common header supplies LPSW to all four RCP motors and LPSW flow can be isolated to individual RCPs using pairs of motor-operated isolation valves located inside the Unit 3 Reactor Building outside the secondary shield wall. LPSW supply to the RCP motor coolers enters the Unit 3 Reactor Building through Penetration 21 and exits through Penetration 22.
While the normal function of this portion of the Unit 3 LPSW system is not safety-related, the Reactor Coolant Pump (RCP) motor cooling piping has a safety related function to serve as a closed-loop mechanical piping system inside containment forming the inside containment isolation barrier for Penetrations 21 and 22. Redundant containment isolation for Penetrations 21 and 22 is provided by motor-operated Containment Isolation Valves (CIVs) located immediately outside the Unit 3 Reactor Building (valves 3LPSW-6 and 3LPSW-15). These CIVs automatically close on Engineered Safety Feature Actuation Signal (ESFAS) channels 5 and 6 [JM] for High Reactor Building Pressure.
EVENT DESCRIPTION
On June 22, 2023, Oconee Unit 3 was operating at approximately 100 percent power. At approximately 22:50 Eastern Daylight Time (EDT), an unexpected increase in Unit 3 Reactor Building Normal Sump (RBNS)[IJ] input rate was identified, with RBNS input rate increasing from approximately 0.013 gallons per minute (gpm) to approximately 0.36 gpm.
Reactor Coolant System (RCS)[AB] leakage calculations were performed, and RCS leakage was ruled out, but a Reactor Building [NH] entry was needed to determine the leak source. Over the next three shifts, Operators and Maintenance technicians systematically isolated and inspected all possible sources of the RBNS input that were accessible with Unit 3 at 100% power. During this time, on June 23, 2024, at approximately 13:00 EDT, the Unit 3 RBNS input rate abruptly increased from approximately 0.3-0.4 gpm to approximately 6 gpm. At 14:00 EDT on June 24, 2023, with no source of the Unit 3 RBNS input identified on any components accessible with Unit 3 at 100% power, Operators began reducing Unit 3 reactor power to allow for investigation of possible leak sources inside the Steam Generator cavities. By approximately 20:33 EDT on June 24, 2023, Unit 3 reactor power was reduced to approximately 20% and inspections inside the Steam Generator cavities were initiated. The source of the Unit 3 RBNS input was identified at approximately 21:48 EDT as a 3/4-inch instrument line broken upstream of normally closed instrument valve 3LPS-IV-0081. The instrument location is for taking pressure readings on the LPSW cooling water header for the 3A1 RCP and is valved out when the Unit is Online. With the source of the leak identified, Operators determined that leak isolation would require the 3A1 RCP to be removed from service. To minimize potential reactor power perturbations that may occur during shutdown of an RCP with the reactor in Mode 1, Operators decided to shut down Unit 3 to Mode 3 prior to securing the 3A1 RCP. This shutdown was completed by 05:40 EDT on June 25, 2023. The 3A1 RCP was subsequently secured at 08:12 EDT, and the leak was isolated at approximately 08:34 EDT by isolating the LPSW cooling water supply and return piping associated with the 3A1 RCP. The broken instrument pipe repairs were completed by 23:00 EDT on June 25, 2023. Repairs consisted of installing a modified instrument connection design. Unit 3 reactor startup was initiated on June 26, 2023, and Unit 3 was returned to approximately 100% power on June 27, 2023.
REPORTABILITY
At the time of the leak identification, ONS personnel (Operations, Engineering, and Regulatory Affairs) evaluated applicability of various Technical Specifications and determined that no existing Technical Specifications appropriately addressed the leak. This was entered into the Corrective Action Program to drive out resolution, but this did not delay actions to identify and isolate the leakage. During a discussion with NRC headquarters personnel on January 17, 2024, ONS was verbally informed that NRC interpretation of ONS technical specifications was that Limiting Condition of Operation (LCO) 3.6.3, Containment Isolation Valves, was not met and the Conditions and Required Actions in TS 3.6.3 only apply to containment isolation valves (i.e., there are no CONDITIONS in TS 3.6.3 that apply to a leak in the pressure boundary on a closed loop containment isolation barrier). Thus, LCO 3.0.3 should have been entered. Per LCO 3.0.3:
When an LCO is not met and the associated ACTIONS are not met, an associated ACTION is not provided, or if directed by the associated ACTIONS, the unit shall be placed in a MODE or other specified condition in which the LCO is not applicable. Action shall be initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to place the unit, as applicable, in (a) MODE 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />; (b) MODE 4 within 18 hours2.083333e-4 days <br />0.005 hours <br />2.97619e-5 weeks <br />6.849e-6 months <br />; and (c) MODE 5 within 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />.
While the time from leak identification to leak isolation would have met Required Action times for LCO 3.0.3, there is firm evidence that there was a LPSW leak on this closed loop penetration piping longer than the LCO 3.0.3 Required Action times. A LPSW leak large enough to question operability of the closed loop piping as a containment isolation barrier existed since at least approximately 1300 on June 23, 2023, when the leak rate increased above approximately 0.6 gpm LPSW allowable leakage per station calculations. The approximately 43.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> it took to isolate the LPSW leak after it was large enough to question operability of the closed loop piping exceeded the LCO 3.0.3 Required Action times.
Therefore, this event is reportable as an Operation or Condition Prohibited by Technical Specifications 10CFR50.73(a)(2)(i)(B).
CAUSAL FACTORS The direct cause is associated with the physical failure of a short section of 3/4 inch carbon steel instrument piping due to internal corrosion of the carbon steel piping at a carbon steel (CS) to stainless steel (SS) weld.
The LPSW supply and return piping to the RCP motors was originally installed as carbon steel piping. An Engineering Change implemented in 1998 replaced most of this piping with stainless steel. The cause investigation was unable to determine why the Engineering Change scope did not result in replacement of the small-bore CS instrument piping that failed in this case. However, the most probable cause of the failure was a deficiency in either the design scope or implementation of the 1998 Engineering Change; resulting in small segments of small-bore CS instrument piping not being replaced with SS as intended.
CORRECTIVE ACTIONS
Immediate:
- 1. Performed RCS leakage calculation and concluded leakage was not from RCS.
- 2. Performed Reactor Building entry to determine leak source by direct observation/sump sample.
- 3. Replaced piping configuration at 3LPS-IV-0081 to resolve the leak.
- 4. Performed an extent of condition (EOC) review to identify additional small-bore instrument piping locations with CS to SS welds and replaced piping configuration at 3LPS-IV-0082 to resolve a degraded condition.
CORRECTIVE ACTIONS (CONT'D)
Planned:
- 1. For Unit 3 components with CS to SS welds identified during the EOC review, install alternate piping configurations at identified components during Spring 2024 Unit 3 Refueling Outage.
- 2. Complete EOC walkdowns for areas that are inaccessible at power at the next available opportunity (Spring 2024 Unit 3 Refueling Outage and Fall 2024 Unit 1 Refueling Outage)
- 3. Revise design documentation to reflect existing stainless steel pipe configurations.
SAFETY ANALYSIS
The Unit 3 LPSW leak resulting in the requirements of TS 3.6.3 not being met was evaluated for its risk impact. It was determined the condition had a negligible impact to public health and safety. The applicable risk metric is LERF as the condition resulted in failing to satisfy the requirements established in TS 3.6.3 pertaining to operability of the containment isolation devices. A leak rate more than allowable overall containment leakage limits existed for a period of approximately 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br />. An accident occurring during this limited window of time is very unlikely. Additionally, throughout the duration of the event the ability to isolate containment was maintained. Penetrations 21 and 22 affected by the condition were capable of being isolated via closure of valves 3LPSW-6 and 3LPSW-15. Both valves close automatically on ES signal.
Therefore, it has been concluded this event had a negligible impact to the health and safety of the public.
ADDITIONAL INFORMATION
A review of Duke Energy's Corrective Action Program did not identify any Oconee LERs or events in the last three years that involve the same underlying concerns or reasons as this event.
This event is considered INPO IRIS Reportable. There were no releases of radioactive materials, radiation exposures, or personnel injuries associated with this event.