05000286/LER-1917-003, Regarding Condensate Storage Tank Declared Inoperable Per Technical Specification
| ML17248A467 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 08/29/2017 |
| From: | Vitale A Entergy Nuclear Operations |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| NL-17-112 LER 17-003-00 | |
| Download: ML17248A467 (6) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(ix)(A) 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) |
| 2861917003R00 - NRC Website | |
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- ='~* Entergx NL-17-112 August 29, 2017 U.S. Nuclear Regulatory Co!Jlmission Attn: Document Control Desk Mail Stop O-P1-17 Washington, D.C. 20555-0001 Indian Point Energy Center 450 Broadway, GSB P.O. Box249 Buchanan, N.Y. 10511-0249 Tel (914) 254-6700 Anthony J. Vitale Site Vice President
Subject:
Licensee Event Report# 2017-003-00, "Condensate Storage Tank Declared Inoperable Per Technical Specification" Indian Point Unit No. 3 Docket No. 50-286 DPR-26
Dear Sir or Madam:
Pursuant to 10 CFR 50. 73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2017-003-00. The Condensate Storage Tank Declared Inoperable Per Technical Specification, which is reportable under 10 CFR
- 50. 73(a)(2)(V)(B). This condition was recorded in the Entergy Corrective Action Program as Condition Report CR-IP3-2017-03504.
There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. Robert Walpole, Manager, Regulatory Assurance, at Indian Point Energy Center at (914) 254-6710.
AJV/trj
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cc:
Mr. Daniel H. Dorman, Regional Administrator, NRC Region I NRC Resident Inspector's Office Ms. Bridget Frymire, New York State Public Service Commission
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 (04-2017) httg ://www.nre.gov/read ing-rm/d oc-col lections/n ur~s/staff/s r1 022/r3/)
the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 13. PAGE Indian Point Unit 3 05000286 1 OFS
- 4. TITLE Condensate Stora~e Tank Declared Inoperable Per Technical Specification
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED SEQUENTIAL FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR REV MONTH DAY YEAR N/A NUMBER NO.
05000 06 30 2017 2017
- - 003
- - 00 08 29 2017 FACILITY NAME DOCKET NUMBER N/A 05000
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply) 1 D 20.2201(b)
D 20.2203(a)(3)(i)
D 50.73(a)(2)(ii)(A)
D 50.73(a)(2)(viii)(A)
D 20.2201(d)
D 20.2203(a)(3)(ii)
D 50.73(a)(2)(ii)(B)
D 50.73(a)(2)(viii)(B)
D 20.2203(a)(1)
D 20.2203(a)(4)
D 50.73(a)(2)(iii)
D 50.73(a)(2)(ix)(A)
D 20.2203(a)(2)(i)
D 50.36(c)(1)(i)(A)
D 50.73(a)(2)(iv)(A)
D 50.73(a)(2)(x)
- 10. POWER LEVEL D 20.2203(a)(2)(ii)
D 50.36(c)(1)(ii)(A)
D 50.73(a)(2)(v)(A)
D 73.71(a)(4)
D 20.2203(a)(2)(iii)
D 50.36(c)(2)
[8] 50.73(a)(2)(v)(B)
D 73.71(a)(5) 100%
D 20.2203(a)(2)(iv)
D 50.46(a)(3)(ii)
D 50.73(a)(2)(v)(C)
D 73.77(a)(1)
D 20.2203(a)(2)(v)
D 50.73(a)(2)(i)(A)
D 50.73(a)(2)(v)(D)
D 73.77(a)(2)(i)
D 20.2203(a)(2)(vi)
D 50.73(a)(2)(i)(B)
D 50.73(a)(2)(vii)
D 73.77(a)(2)(ii)
D 50.73(a)(2)(i)(C)
D OTHER Specify in Abstract below or in NRG Form 366A
- 12. LICENSEE CONTACT FOR THIS LER LICENSEE CONTACT
~LEPHONE NUMBER (Include Area Code)
!Nelson Azevedo 9142546775 CAUSE SYSTEM COMPONENT MANU-REPORTABLE
CAUSE
SYSTEM COMPONENT MANU-REPORTABLE FACTURER TO EPIX FACTURER TO EPIX x
KA RV Tyco y
- 14. SUPPLEMENTAL REPORT EXPECTED
~NO SUBMISSION DATE ABSTRACT On June 30, 2017, at 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> [EDT], the Condensate Storage Tank was declared inoperable per Technical Specification 3.7.6. A pinhole sized through wall leak was discovered on the downstream side of CD-123, the 32 Auxiliary Boiler Feed Pump Bearing Cooling Relief Valve, which was unisolable to the Condensate Storage Tank.
The pinhole leak was identified following the performance of 3PT-Q120B, 32 Auxiliary Boiler Feed Pump Functional Test. All Operability and Acceptance Criteria of 3PT-Q120B were sat. The relief valve was removed from the system and sent to a vendor for evaluation. After the vendor evaluation, it was determined that the valve pinhole area leak was due to a casting defect.
This event was determined to be reportable as a Loss of Safety Function pursuant to 10 CFR 50.72(b)(3)(v)(B)-Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat.
NRC FORM 366 (04-2017)
- 3. LER NU\\/IBER SEQUENTIAL NUMBER
- - 003 REV NO.
- - 00 On June 30, 2017 at 0130 [EDT], the Condensate Storage Tank was declared inoperable per Technical Specification 3.7.6. The Condensate Storage Tank shall be OPERABLE in MODES 1, 2, 3 and MODE 4 when steam generator is relied upon for heat removal. A pin hole sized through wall leak was discovered on the downstream side of CD-123, the 32 Auxiliary Boiler Feed Pump Bearing Cooling Relief Valve, which is unisolable to the Condensate Storage Tank. The function of the relief valve is to protect the bearing housings of the turbine-driven Auxiliary Boiler Feedwater Pump and its steam driven turbine from over pressme. The pinhole leak was identified following performance of 3PT-Q120B, 32 Auxiliary Boiler Feed Pump Functional Test. All Operability and Acceptance Criteria of 3PT-Q120B were sat.
The relief valve CD-123, had a through body wall leak of pin holed size with a steady stream of water leaking out. The valve body is cast iron.* No type ofNon-Destructive Examination (NDE) could be used to effectively characterize the defect. Based on the inability to characterize the defect and the fact that the degradation mechanism was not readily apparent, the valve was considered inoperable because the valve has lost its ability to maintain a pressure boundary. As a result, the Condensate Storage Tank was d~clared inoperable. The Condensate Storage Tank had 580,000 gallons of water contained in the tank at the time of the leak discovery, which is well above the minimum required amount of360,000 gallons.
City water is the backup water supply to the Auxiliary Feedwater System, and was verified to be operable in accordance with the Actions of the Technical Specification. The Technical Specification requirements were to restore the Condensate Storage Tank to operable status within 7 days.
The Condensate Storage Tank provides cooling water to remove decay heat. The minimum amount of water in the Condensate Storage Tank is the amount needed to maintain the plant for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at hot shutdown following a trip from full power.
This event was determined to be reportable as a Loss of Safety Function pursuant to 10 CFR 50.72(b)(3)(v)(B) -Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. Page 2 ofS (04-2017)
U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/readinq-rm/doc-collections/nuregs/staff/sr1022/r3/)
, the NRG may not conduct or sponsor, and a person is not required to respond to, the infonnation collection.
Indian Point Unit 3 05000-286 YEAR
- 3. LER NUMBER SEQUENTIAL NUMBER REV NO.
2017
- - 003
- - 00
CAUSE OF EVENT
The 32 Auxiliary Boiler Feed Pump Bearing Cooling Relief Valve was removed from service and submitted to a vendor for full evaluation of the pinhole area. After the vendor evaluation, it was determined that the valve pinhole area leak was due to a casting defect. Based on the amount of material and the cross-section remaining around the casting void, gross structural integrity of the valve body and associated piping would not have been challenged with this porosity defect present under design conditions.
The vendor performed an evaluation included metallographic examination and quantitative chemical analysis.
Results of the vendor evaluation indicate the leak through the body occurred along a tortuous path through a cavity consistent with a casting void defect. The casting void had a diameter of approximately 10 mm, and mold sand material was present in this cavity. Corrosion wastage or pitting was not evident on either the exterior or interior of the valve body surfaces.
This valve had previously been in service for a period from approximately 2009 through 2013, when it was removed, tested, and placed into storage as a spare. The valve was subsequently re-installed into the auxiliary boiler feed pump bearing cooling line during the Unit 3 2017 refueling outage. Upon testing the system, leakage from the valve was observed.
It was surmised by the vendor that sufficient blockage of mold sand material in the leakage path in the casting void was present to maintain service conditions during the prior (2009 through 2013) operating period. With the valve's removal and relief valve testing, followed by re-installation, material blockage in the void cavity became dislodged to some degree and a leak path was presented.
CORRECTIVE ACTIONS
The following corrective actions have been performed under the Corrective Action Program to address the cause of this event.
The CD-123, 32 Auxiliary Boiler Feed Pump Bearing Cooling Relief Valve was removed from the system and replaced with a pre-tested spare.
The CD-123, 32 Auxiliary Boiler Feed Pump Bearing Cooling Relief Valve was sent to a vendor for evaluation of the pinhole area. The evaluation confirmed the pinhole leak was due to a casting defect. Page 3 of5 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 (04-2017)
LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)
, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. LER NUMBER YEAR Indian Point Unit 3 05000-286 2017
EVENT ANALYSIS
SEQUENTIAL NUMBER
- - 003 REV NO.
- - 00 The Condensate Storage Tank provides cooling water to remove decay heat and the minimum amount of water in the Condensate Storage Tank is the amount needed to maintain the plant for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at hot shutdown following a trip from full power. The minimum water level for operability was maintained at all times. Based upon the vendor analysis, the pinhole leak identified on CD-123 did not challenge the functionality of the relief valve or any of the Technical Specification Safety Limits. With the pinhole leak in the valve, the station could not apply Code Case N-513-1 to this configuration, since the code case does not allow the use on valves. However, the vendor report showed that there was no loss of safety function to the 32 Auxiliary Boiler Feed Pump and the Condensate Storage Tank remained available at all times. Since we cannot use code case N-513 in this application, this event is reportable under 10 CFR 50.73(a)(2)(v)(B)-Any event or condition that could have prevented the fulfilment of the safety function of structures or systems that are needed to remove residual heat.
PAST SIMILAR EVENTS A review was performed of the past five years of Licensee Event Reports (LERs) for events reporting a Technical Specification violation due to inoperable piping caused by pinhole or through wall leaks or defects.
LER 2013-004-00 Technical Specification prohibited condition due to an inoperable essential Service Water header as a result of pinhole leaks in Code Class 3 Service Water Piping.
LER 2015-001-01 Technical Specification prohibited condition due to an inoperable Containment caused by a Service Water pipe leak that results in exceeding the allowed leakage rate for containment. Page 4 ofS U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 (04-2017)
LICENSEE EVENT REPORT (LER)
CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)
Estimated burden penesponse to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to lnfocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRG may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. LER NUVIBER YEAR Indian Point Unit 3 05000-286 2017
SAFETY SIGNIFICANCE
SEQUENTIAL NUMBER
- - 003 REV NO.
- - 00 There were no actual safety consequences during the time the Condensate Storage Tank was inoperable.
- After vendor evaluation it was determined that the valves pinhole leak area was due to a casting defect.
Based on the amount of material and the cross-section remaining around the casting void, gross structural integrity of the valve body and associated piping would not have been challenged with this porosity defect present under design conditions. The minimum water level for operability was maintained at all times. Based upon the vendor analysis, the pinhole leak identified on CD-123 did not challenge the functionality of the relief valve or any of the Technical Specification Safety Limits. With the pinhole leak in the valve, the station could not apply Code Case N-513-1 to this configuration, since the code case does not allow the use on valves. However, the vendor report showed that there was no loss of safety function to the 32 Auxiliary Boiler Feed Pump and the Condensate Storage Tank remained available at all times. Moreover, consistent with guidance provided in Section 2.2 of Nuclear Energy Institute (NEI) 99-02 (Regulatory Assessment Performance Indicator Guideline), Revision 7, this event did not represent, and should not pe counted as, a safety system functional failure. As such, Entergy will not record this event as a safety system functional failure in the NRC Mitigating Systems Performance Indicators for Indian Point Unit 3. Page 5 ofS