| | | Reporting criterion |
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| 05000323/LER-1985-001-02, :on 850705,automatic Isolation of Containment Ventilation Sys Occurred W/Unit in Mode 5.Caused by Spurious Spike in Vent Gaseous Radiation Monitor RM14A.Alarm Reset. No Corrective Action Identified |
- on 850705,automatic Isolation of Containment Ventilation Sys Occurred W/Unit in Mode 5.Caused by Spurious Spike in Vent Gaseous Radiation Monitor RM14A.Alarm Reset. No Corrective Action Identified
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-001, :on 850102,while in Mode 1,low Flow in RCS Initiated Reactor Trip.Caused by Turbine Overspeed Protection Controller Sys Solenoid Valve Failure.Valve Replaced |
- on 850102,while in Mode 1,low Flow in RCS Initiated Reactor Trip.Caused by Turbine Overspeed Protection Controller Sys Solenoid Valve Failure.Valve Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-002-01, :on 850719,while Restoring Train a to Svc, Inadvertent Actuation of Train B Safety Injection Occurred. Caused by Operator Inadvertently Moving Reset Block Switch Instead of Block Position |
- on 850719,while Restoring Train a to Svc, Inadvertent Actuation of Train B Safety Injection Occurred. Caused by Operator Inadvertently Moving Reset Block Switch Instead of Block Position
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-002, :on 850104,w/unit in Mode 1,reactor Tripped on Turbine Auto Stop Oil Pressure.Caused by Voltage Transient Due to Second Condensate Booster Pump Startup.All Automatic Equipment Responded as Designed |
- on 850104,w/unit in Mode 1,reactor Tripped on Turbine Auto Stop Oil Pressure.Caused by Voltage Transient Due to Second Condensate Booster Pump Startup.All Automatic Equipment Responded as Designed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-003-02, :on 850809,automatic Isolation of Containment Ventilation Sys Occurred.Caused by Switching of Radiation Monitor Mode Switch to Reset & Back During Troubleshooting. Events Under Study |
- on 850809,automatic Isolation of Containment Ventilation Sys Occurred.Caused by Switching of Radiation Monitor Mode Switch to Reset & Back During Troubleshooting. Events Under Study
| |
| 05000275/LER-1985-003, :on 850105,while in Mode 1,diesel Generator (Ek) 1-1 Started Automatically Due to Undervoltage on 4 Kv Bus H.Event Classified as Anticipated Operational Transient |
- on 850105,while in Mode 1,diesel Generator (Ek) 1-1 Started Automatically Due to Undervoltage on 4 Kv Bus H.Event Classified as Anticipated Operational Transient
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-004, :on 850104,30-day Special Rept Submittal Period Exceeded.On 841128,public Address Sys Cable Installation Led to Inoperability of Two Fire Barriers.On 850108,unsealed Penetrations Discovered |
- on 850104,30-day Special Rept Submittal Period Exceeded.On 841128,public Address Sys Cable Installation Led to Inoperability of Two Fire Barriers.On 850108,unsealed Penetrations Discovered
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-004-02, :on 850816,containment Purge Supply & Exhaust Valves Not Maintained Closed When Solid State Protection Sys Train a Removed from Svc.Caused by Technician & Operator Errors.Procedure Revised |
- on 850816,containment Purge Supply & Exhaust Valves Not Maintained Closed When Solid State Protection Sys Train a Removed from Svc.Caused by Technician & Operator Errors.Procedure Revised
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-005-02, :on 850815,automatic Isolation of Containment Ventilation Sys Occurred.Caused by Spurious Spike in Containment Gaseous Radiation Monitor RM11.Noise Reduction Task Force Will Investigate Spurious Signals |
- on 850815,automatic Isolation of Containment Ventilation Sys Occurred.Caused by Spurious Spike in Containment Gaseous Radiation Monitor RM11.Noise Reduction Task Force Will Investigate Spurious Signals
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-005, :on 850120,both RHR Trains Became Inoperable. Caused by Technician Checking Wrong Breaker & Verifying Breaker as Open.Rhr Pump 1-1 Restarted & RHR Flow Established |
- on 850120,both RHR Trains Became Inoperable. Caused by Technician Checking Wrong Breaker & Verifying Breaker as Open.Rhr Pump 1-1 Restarted & RHR Flow Established
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 05000275/LER-1985-006, :on 850125,both RHR Trains Inoperable.Caused by Closure of Loop 4 RHR Suction Valve MOV-8702 Due to Loss of 4-kV Bus Voltage.Suction Valve Opened & RHR Flow Established within 2 Minutes |
- on 850125,both RHR Trains Inoperable.Caused by Closure of Loop 4 RHR Suction Valve MOV-8702 Due to Loss of 4-kV Bus Voltage.Suction Valve Opened & RHR Flow Established within 2 Minutes
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
| 05000323/LER-1985-006-01, :on 850824,during Startup,Random Failure of Rod Drive Motor Generator Set Relays Resulted in Rod Insertion & Manual Reactor Trip.Caused by Burned Out Coil on Auxiliary Relay & Relay Drift.Relays Replaced |
- on 850824,during Startup,Random Failure of Rod Drive Motor Generator Set Relays Resulted in Rod Insertion & Manual Reactor Trip.Caused by Burned Out Coil on Auxiliary Relay & Relay Drift.Relays Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-007-01, :on 850829,reactor Trip on Low Steam Generator Level Coincident W/Steam Flow/Feed Flow Mismatch Occurred. Caused by Personnel Error.Operator Counseled on Significance of Understanding Abnormal Plant Conditions |
- on 850829,reactor Trip on Low Steam Generator Level Coincident W/Steam Flow/Feed Flow Mismatch Occurred. Caused by Personnel Error.Operator Counseled on Significance of Understanding Abnormal Plant Conditions
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-007, :on 850204 & 05,control Room Ventilation Sys Automatically Transferred from Normal Mode to Pressurization Mode.Caused by Contractor Technician Performing Startup Testing on Unit 2 Solid State Protection Sys |
- on 850204 & 05,control Room Ventilation Sys Automatically Transferred from Normal Mode to Pressurization Mode.Caused by Contractor Technician Performing Startup Testing on Unit 2 Solid State Protection Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-008, :on 850205,time Limit for Performing Isotopic I Analysis Exceeded.Caused by Communication Failure. Operating Procedure Revised to Prevent Recurrence & Operators Retrained |
- on 850205,time Limit for Performing Isotopic I Analysis Exceeded.Caused by Communication Failure. Operating Procedure Revised to Prevent Recurrence & Operators Retrained
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-008-01, :on 850913,while Unit in Cold Shutdown, Automatic Isolation of Containment Ventilation Sys Occurred. Investigation Continuing.Alarm Reset & Gaseous Radiation Monitor Isolation Valves Returned to Position |
- on 850913,while Unit in Cold Shutdown, Automatic Isolation of Containment Ventilation Sys Occurred. Investigation Continuing.Alarm Reset & Gaseous Radiation Monitor Isolation Valves Returned to Position
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-009, :on 850213,steam Line Differential Pressure Injection Signal Received,Resulting in Safety Injection, Turbine Trip & Reactor Trip.Caused by Frequency Interference from Radio.Procedure Revised |
- on 850213,steam Line Differential Pressure Injection Signal Received,Resulting in Safety Injection, Turbine Trip & Reactor Trip.Caused by Frequency Interference from Radio.Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-009-01, :on 851022,generator & Reactor Trip Occurred. Caused by Technician Inadvertently Actuating Current Test Block of Main Generator Differential Relay.Technician Counseled & Instructions Installed on Panel |
- on 851022,generator & Reactor Trip Occurred. Caused by Technician Inadvertently Actuating Current Test Block of Main Generator Differential Relay.Technician Counseled & Instructions Installed on Panel
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-010-01, :on 851024,turbine & Reactor Tripped Due to High Water Level in Steam Generator.Caused by Inadequate Procedures.Procedures for Operation of Condensate Booster Pumps During Unusual Plant Conditions Revised |
- on 851024,turbine & Reactor Tripped Due to High Water Level in Steam Generator.Caused by Inadequate Procedures.Procedures for Operation of Condensate Booster Pumps During Unusual Plant Conditions Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-010, :on 850205,audit Determined That 6-month Leak Test on 400-mCi Cs-137 Check Source Not Performed within Time Requirement.Caused by Incorrect Classification of Sealed Source.Applicable Records Corrected |
- on 850205,audit Determined That 6-month Leak Test on 400-mCi Cs-137 Check Source Not Performed within Time Requirement.Caused by Incorrect Classification of Sealed Source.Applicable Records Corrected
| 10 CFR 50.73(a)(2)(1) |
| 05000275/LER-1985-011, :on 850217,manual Reactor Trip Initiated in Response to Automatic Shutdown of Main Feedwater Pumps 1-1 & 1-2 from Excessive Thrust Bearing Wear Indication.Thrust Bearing Wear Detection Sys Reset |
- on 850217,manual Reactor Trip Initiated in Response to Automatic Shutdown of Main Feedwater Pumps 1-1 & 1-2 from Excessive Thrust Bearing Wear Indication.Thrust Bearing Wear Detection Sys Reset
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-011-01, :on 851025,auxiliary Feedwater Steam Supply Line Snubber Inoperability Not Determined Before Exceeding Limiting Condition for Operation.Caused by Miscommunication Between Technician & Engineer.Snubber Replaced |
- on 851025,auxiliary Feedwater Steam Supply Line Snubber Inoperability Not Determined Before Exceeding Limiting Condition for Operation.Caused by Miscommunication Between Technician & Engineer.Snubber Replaced
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-012-01, :on 851017,review of Completed Surveillance Test Procedure Data Sheet Determined Three Feedwater Control Valves Had Exceeded Closure Time Requirements of Tech Spec Table 3.3-5.Caused by Personnel Error |
- on 851017,review of Completed Surveillance Test Procedure Data Sheet Determined Three Feedwater Control Valves Had Exceeded Closure Time Requirements of Tech Spec Table 3.3-5.Caused by Personnel Error
| 10 CFR 50.73(a)(2)(1) |
| 05000275/LER-1985-012, :on 850321,automatic Reactor & Turbine Trips Occurred.Caused by Technicians Inadvertently Shorting 115-volt Vital Power Supply While Testing Level Channels. Personnel Reinstructed |
- on 850321,automatic Reactor & Turbine Trips Occurred.Caused by Technicians Inadvertently Shorting 115-volt Vital Power Supply While Testing Level Channels. Personnel Reinstructed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-013-01, :on 850430,Mode 4 Entered W/Two ESF Timers Out of Tech Spec Limits.Caused by Personnel Failure to Verify Timer Settings.Personnel Given Addl Training on Importance of Verifying Data |
- on 850430,Mode 4 Entered W/Two ESF Timers Out of Tech Spec Limits.Caused by Personnel Failure to Verify Timer Settings.Personnel Given Addl Training on Importance of Verifying Data
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-013, :on 851106,during Startup Procedure 43.7, Reactor Tripped on lo-lo Steam Generator Level.Caused by Turbine Interceptor Valves Opening Too slowly.Electro- Hydraulic Control Sys Modified |
- on 851106,during Startup Procedure 43.7, Reactor Tripped on lo-lo Steam Generator Level.Caused by Turbine Interceptor Valves Opening Too slowly.Electro- Hydraulic Control Sys Modified
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-013, :on 850430,Mode 4 Entered W/Timer Settings Outside Acceptable Tech Spec Limits.Caused by Personnel Error.Personnel Received Addl Training & Procedure Revised |
- on 850430,Mode 4 Entered W/Timer Settings Outside Acceptable Tech Spec Limits.Caused by Personnel Error.Personnel Received Addl Training & Procedure Revised
| 10 CFR 50.73(a)(2)(1) |
| 05000275/LER-1985-014, :on 850518,reactor Tripped Followed by Safety Injection.Caused by Failure of Slave 2.S Kva Regulating Transformer.Transformer Replaced & Inverter Returned to Svc |
- on 850518,reactor Tripped Followed by Safety Injection.Caused by Failure of Slave 2.S Kva Regulating Transformer.Transformer Replaced & Inverter Returned to Svc
| 10 CFR 50.73(a)(2)(1) |
| 05000275/LER-1985-014-02, Forwards LER 85-014-02 Re Reactor Trip & Safety Injection. Rev Repts Discovery of Addl Damaged Snubber Resulting from Water Hammer After Reactor Trip | Forwards LER 85-014-02 Re Reactor Trip & Safety Injection. Rev Repts Discovery of Addl Damaged Snubber Resulting from Water Hammer After Reactor Trip | 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-014-01, :on 851005,unit Entered Mode 2 (Hot Shutdown) W/Steam Generator Main Feedwater Isolation Valve FCV-439 Inoperable.Caused by Incorrect Wiring Terminations in Control Sys.Maint Bulletin Issued |
- on 851005,unit Entered Mode 2 (Hot Shutdown) W/Steam Generator Main Feedwater Isolation Valve FCV-439 Inoperable.Caused by Incorrect Wiring Terminations in Control Sys.Maint Bulletin Issued
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-015-01, :on 851109,P-14 signal,hi-hi Steam Generator Level Resulted in Turbine Trip & Subsequent Reactor Trip. Caused by Personnel Error.Addl Training Being Provided to Applicable Operations Personnel |
- on 851109,P-14 signal,hi-hi Steam Generator Level Resulted in Turbine Trip & Subsequent Reactor Trip. Caused by Personnel Error.Addl Training Being Provided to Applicable Operations Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-015, :on 850520,reactor Trip Followed by Safety Injection Occurred.Caused by Loose Connection to Output Circuit Breaker for Instrument Inverter IY-1-2.Connections Reterminated & Inverter Returned to Svc |
- on 850520,reactor Trip Followed by Safety Injection Occurred.Caused by Loose Connection to Output Circuit Breaker for Instrument Inverter IY-1-2.Connections Reterminated & Inverter Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-016, :on 850520,automatic Reactor Trip Occurred. Caused by Deenergization of Bistables for Source Range Channel 32 (Jc)(Ri) Due to Voltage Transient.Event Reviewed W/Applicable Personnel & Procedure Revised |
- on 850520,automatic Reactor Trip Occurred. Caused by Deenergization of Bistables for Source Range Channel 32 (Jc)(Ri) Due to Voltage Transient.Event Reviewed W/Applicable Personnel & Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-016-01, :on 851126 & 1201,automatic Reactor Trips Occurred During 50% Load Rejection Startup Testing.Caused by Steam Dump Control Sys & Feedwater Control Sys Settings Inadequately Adjusted,Respectively |
- on 851126 & 1201,automatic Reactor Trips Occurred During 50% Load Rejection Startup Testing.Caused by Steam Dump Control Sys & Feedwater Control Sys Settings Inadequately Adjusted,Respectively
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-017, :on 850523,maint Employee Permitted to Enter High Radiation Area W/O Positive Exposure Control W/Unit in Mode 1.Caused by Personnel Error.Technician Counseled & Will Be Disciplined |
- on 850523,maint Employee Permitted to Enter High Radiation Area W/O Positive Exposure Control W/Unit in Mode 1.Caused by Personnel Error.Technician Counseled & Will Be Disciplined
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-017-01, :on 851128,reactor Trip Occurred Due to Steam Flow/Feed Flow Mismatch.Caused by Leak in Condensing Pot of Steam Generator Water Level Transmitter Ref Leg.Exhaustive Testing of Reactor Trip Breaker B Performed |
- on 851128,reactor Trip Occurred Due to Steam Flow/Feed Flow Mismatch.Caused by Leak in Condensing Pot of Steam Generator Water Level Transmitter Ref Leg.Exhaustive Testing of Reactor Trip Breaker B Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-018-01, :on 850505,test Leads Mistakenly Left Connected to Reactor Coolant Outlet Temp Monitor Circuit & Did Not Meet Electrical Separation Criteria.Caused by Technician Oversight.Personnel Received Addl Training |
- on 850505,test Leads Mistakenly Left Connected to Reactor Coolant Outlet Temp Monitor Circuit & Did Not Meet Electrical Separation Criteria.Caused by Technician Oversight.Personnel Received Addl Training
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-018-02, :on 851202,spurious Safety Injection Occurred After Initiation of Manual Reactor Trip in Response to Digital Rod Position Indication Sys Data a Failure.Exact Cause Under Investigation |
- on 851202,spurious Safety Injection Occurred After Initiation of Manual Reactor Trip in Response to Digital Rod Position Indication Sys Data a Failure.Exact Cause Under Investigation
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-018, :on 850505,test Leads Left Connected to Reactor Coolant Outlet Temp Monitors After Completion of Surveillance Test Procedure.Caused by Lack of Communication Between Shift Personnel.Leads Removed 850510 |
- on 850505,test Leads Left Connected to Reactor Coolant Outlet Temp Monitors After Completion of Surveillance Test Procedure.Caused by Lack of Communication Between Shift Personnel.Leads Removed 850510
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-018, :on 851202,digital Rod Position Indication Sys Experienced Data a Failure & General Warning on Each Control Rod,Resulting in Reactor Trip.Caused by Faulty Dc Logic Power Supply.Power Supply Repaired |
- on 851202,digital Rod Position Indication Sys Experienced Data a Failure & General Warning on Each Control Rod,Resulting in Reactor Trip.Caused by Faulty Dc Logic Power Supply.Power Supply Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-019, :on 850602,limiting Condition for Operation Time Requirement Exceeded Re Thermocouple Monitoring Sys Channel Check.Caused by Personnel Failure to Review Computer Generated Preventive Maint Tracking Sys |
- on 850602,limiting Condition for Operation Time Requirement Exceeded Re Thermocouple Monitoring Sys Channel Check.Caused by Personnel Failure to Review Computer Generated Preventive Maint Tracking Sys
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-019-01, :on 851127,blown Fuse Discovered on Solenoid Valve SV-306 During post-safety Injection Review.Caused by Wiring Error.Short Cause of Previous Fuse Failures on 850814 & 29.Wiring Error Corrected |
- on 851127,blown Fuse Discovered on Solenoid Valve SV-306 During post-safety Injection Review.Caused by Wiring Error.Short Cause of Previous Fuse Failures on 850814 & 29.Wiring Error Corrected
| 10 CFR 50.73(a)(2)(i) |
| 05000323/LER-1985-019, 0l:on 851127,blown Fuse Discovered on Solenoid Valve SV-306 During post-safety Injection Review.Caused by Incorrect Wiring Change & Personnel Error.Wiring Corrected | 0l:on 851127,blown Fuse Discovered on Solenoid Valve SV-306 During post-safety Injection Review.Caused by Incorrect Wiring Change & Personnel Error.Wiring Corrected | 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-020-01, :on 851116,discovered That Plant Vent Particulate & Iodine Monitor RE-24 Sample Collection Pump Deenergized.Caused by Switching Off of RE-24 Power Switch. Protective Cover Installed Over Switch |
- on 851116,discovered That Plant Vent Particulate & Iodine Monitor RE-24 Sample Collection Pump Deenergized.Caused by Switching Off of RE-24 Power Switch. Protective Cover Installed Over Switch
| 10 CFR 50.73(a)(2)(i) |
| 05000275/LER-1985-020, :on 850613,start Signal Applied to Diesel Generator 1-2,not 1-3.Caused by Personnel Misunderstanding of Verbal Instructions.Generator 1-2 Secured.Improvements in Communications & Identification Implemented |
- on 850613,start Signal Applied to Diesel Generator 1-2,not 1-3.Caused by Personnel Misunderstanding of Verbal Instructions.Generator 1-2 Secured.Improvements in Communications & Identification Implemented
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-021, :on 850618,while in Mode 1,axial Flux Difference Could Not Be Reduced to within Target Band,Nor Could Reactor Power Be Reduced to Less than 90% within 15 Min.Caused by Rapid Xenon Burnout |
- on 850618,while in Mode 1,axial Flux Difference Could Not Be Reduced to within Target Band,Nor Could Reactor Power Be Reduced to Less than 90% within 15 Min.Caused by Rapid Xenon Burnout
| 10 CFR 50.73(a)(2)(i) |
| 05000323/LER-1985-021-01, :on 851204,spurious Safety Injection Occurred. Caused by Safety Injection Signal Received on Train a of Solid State Protection Sys While Preparing to Investigate 851202 Event.No Corrective Action Required |
- on 851204,spurious Safety Injection Occurred. Caused by Safety Injection Signal Received on Train a of Solid State Protection Sys While Preparing to Investigate 851202 Event.No Corrective Action Required
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000323/LER-1985-022-01, :on 851221,automatic Reactor & Turbine Trips Occurred.Caused by Loose Wiring to Feedwater Regulating Valve Solenoid & Personnel Error Causing Momentary Opening of Connection.Connection Properly Terminated |
- on 851221,automatic Reactor & Turbine Trips Occurred.Caused by Loose Wiring to Feedwater Regulating Valve Solenoid & Personnel Error Causing Momentary Opening of Connection.Connection Properly Terminated
| 10 CFR 50.73(a)(2)(iv), System Actuation |
| 05000275/LER-1985-022, :on 850501,four Accumulators Became Inoperable W/Unit in Mode 3.Caused by Conflict in Procedures & Misunderstanding Re Requirements for Use of Seals.Procedures Revised & Breaker Panels Labeled |
- on 850501,four Accumulators Became Inoperable W/Unit in Mode 3.Caused by Conflict in Procedures & Misunderstanding Re Requirements for Use of Seals.Procedures Revised & Breaker Panels Labeled
| 10 CFR 50.73(a)(2)(1) |
| 05000323/LER-1985-023-01, :on 850725,unit Entered Hot Shutdown W/O Necessary Surveillance on Some ECCS & Associated Containment Spray Motor Operated Valves.Caused by Personnel Error. Procedure STP V-7B Satisfactorily Performed |
- on 850725,unit Entered Hot Shutdown W/O Necessary Surveillance on Some ECCS & Associated Containment Spray Motor Operated Valves.Caused by Personnel Error. Procedure STP V-7B Satisfactorily Performed
| 10 CFR 50.73(a)(2)(i) |