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At approximately 12:20 hours on 1/7/87 with the plant at full power, a Reactor Protection System (RPS) Motor Generator set (MG) tripped. The resulting loss of power to half of RPS caused a half SCRAM, a Group 3 primary containment isolation, shutdown of Reactor Building ventilation and start of the Standby Gas Treatment System.
The trip of the MG set was caused by a failed coil (open circuit) on a control relay in the MG set. The reley/ coil operated for approximately 15 years and its failure my te attrib'.ted to end of life.
The events of this report did not have adverse saf ety implications. The RT'S snd Primary Contairment Isolation System (PCIS) operated as designed upon experiencing a power loss to half of RPS.
No specific actions beyond replacing the failed relay coil were determined to be necessary. We will continue to trend failures of this type and initiate additional corrective actions as necessary.
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w =c -.mn DESCRIPTION OF EVENTS At approximately 12:20 hours on 1/7/87 with the plant at full power the 'B' Reactor Protection System Motor Generator (RPS MG) set tripped.
The resulting loss of power to half of RPS caused a half SCRAM, a Group 3 primary containment isolation, shutdown of Reactor Building ventilation and the start of the Standby Gas Treatment System. The event was reported to plant management by the Shift Engineer.
CAUT OF EVENTS The trip of the MG set was caused by a failed coil (open circuit) on a General Electric CR120 series control relay in the MG set. The Energy Industry Identification System (EIIS) component identifier for the failed relay is RLY.
It is believed that the relay was original plant equipment and the coil failure is attributed to end of life (i.e., approximately 15 years operation).
ANALYSIS OF EVENTS The events of this report did not have adverse safety implications. The RPS and Primary Containment Isolation Systems (PCIS) operated as designed. A half SCRAM is the expected response due to loss of power to half of RPS.
The PCIS System is designed to shutdown Reactor Building ventilation, start Standby Gas Treatment and initiate a Group 3 isolation upon a single upscale trip of the Reactor Building or Refuel Floor radiation monitors. The de-energization of half of RPS simulated this condition by dropping out the associated logic relays.
Following the trip of the MG set, operator action restored power to the "B" side of RPS almost immediately by using the RPS alternate pcwer source.
The half SC9AM and the Group 3 isolation were reset, Reactor Building ventilation was restarted and the Standby Gas Treatment System was secured within ten minutes.
After replacement of the control relay coil, the MG sit was returned to sar-vice in approxirately 2 tnurs.
There have betti no other s'.milar failures of CR120 reitys in the RPS system.
A similar result occurred from failure of a CR205 contactor which caused a full SCRAM and a Group 3 isciation. This event was reported to the ccmmission under LER 86-10.
CORRECTIVE ACTIONS
No specific actions beyond replacing the failed relay coil were determined to be necessary. We will continue to trend failures of this type and initiate i
additional corrective actions as necessary.
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' VERMONT YANKEE NUCLEAR POWER CORPORATION ~
P. O. BOX 157 GOVERNOR HUNT ROAD VERNON, VERMONT 05354 February 6,1987 WV 487-022 U.S. Nuclear Regulatory Commission Document No. 50-271 Washington, D.C.
20555 REFERENCE: Operating License DPR-28 Docket No. 50-271 Reportable Occurrence No. LER 87-01
Dear Sirs:
As defined by 10CFR50.73, we are reporting the attached Reportable Occurrence as LER 87-01.
Very truly yours, VERMONT YANKEE NUO_ EAR POWER CDRPORATION h
p Plant Manager James P. Pelletie PBC/ mmh cc: Regional Administrator USNRC Office of Inspection and Enforcement Region I 631 Park AveRJe Xing of Prussia, Pennsylvania 19106 1
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| 05000271/LER-1987-001, :on 870107,reactor Protection Sys Motor Generator Set Tripped,Resulting in Half Scram & Initiation of ECCS Sys.Caused by Failed Coil on Control Relay Due to End of Life.Coil Replaced |
- on 870107,reactor Protection Sys Motor Generator Set Tripped,Resulting in Half Scram & Initiation of ECCS Sys.Caused by Failed Coil on Control Relay Due to End of Life.Coil Replaced
| | | 05000271/LER-1987-002, :on 870501,primary Containment Isolation Sys Group III & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Technician Exposing Operating Radiation Detector.Detector Location Labeled |
- on 870501,primary Containment Isolation Sys Group III & Subsequent Standby Gas Treatment Sys Initiation Occurred.Caused by Technician Exposing Operating Radiation Detector.Detector Location Labeled
| | | 05000271/LER-1987-003, :on 870724,resident Inspector Noted That Calibr Procedure for Toxic Gas Monitor Chlorine Analyzer Did Not Satisfy Tech Spec Setpoint Requirements.Caused by Procedural Inadequacy.Calibr Procedure Revised |
- on 870724,resident Inspector Noted That Calibr Procedure for Toxic Gas Monitor Chlorine Analyzer Did Not Satisfy Tech Spec Setpoint Requirements.Caused by Procedural Inadequacy.Calibr Procedure Revised
| | | 05000271/LER-1987-004, :on 870729,discovered That Surveillance of Inside Fire Hose Stations Had Not Been Completed.Caused by Personnel Errors.Surveillance Procedure Revised to Include 18-month Inside Fire Hose Surveillance Insp |
- on 870729,discovered That Surveillance of Inside Fire Hose Stations Had Not Been Completed.Caused by Personnel Errors.Surveillance Procedure Revised to Include 18-month Inside Fire Hose Surveillance Insp
| | | 05000271/LER-1987-005, :on 870807,while Shutting Down for Scheduled Refueling Outage,Reactor Scram Occurred.Caused by Inability of Mechanical Pressure Regulator Sys to Take Control from Electrical Pressure Regulator Sys |
- on 870807,while Shutting Down for Scheduled Refueling Outage,Reactor Scram Occurred.Caused by Inability of Mechanical Pressure Regulator Sys to Take Control from Electrical Pressure Regulator Sys
| | | 05000271/LER-1987-006, :on 870810,operations Personnel Increased Standby Liquid Control Storage Tank Level W/O Requesting Chemistry Sample Analysis.Caused by Communication Deficiency.Operating Procedures Revised |
- on 870810,operations Personnel Increased Standby Liquid Control Storage Tank Level W/O Requesting Chemistry Sample Analysis.Caused by Communication Deficiency.Operating Procedures Revised
| | | 05000271/LER-1987-007, :on 870812,18 & 23,while Performing Type C Leak Rate Testing,Listed Valves Found to Have Seat Leakage Above Tech Spec Requirements.Util Will Perform Maint on Valves to Determine Cause of Failure |
- on 870812,18 & 23,while Performing Type C Leak Rate Testing,Listed Valves Found to Have Seat Leakage Above Tech Spec Requirements.Util Will Perform Maint on Valves to Determine Cause of Failure
| | | 05000271/LER-1987-008, :on 870817,loss of Normal Power During Shutdown Occurred.Caused by Routing of All Sources of Offsite Power Through One Set of Breakers While Plant in Outage. Precautions to Be Added to Procedures |
- on 870817,loss of Normal Power During Shutdown Occurred.Caused by Routing of All Sources of Offsite Power Through One Set of Breakers While Plant in Outage. Precautions to Be Added to Procedures
| | | 05000271/LER-1987-009, :on 870818,main Steam Relief Valve Accumulator Assembly C Found to Have Seat Leakage Exceeding Acceptance Criteria.Caused by Dirt/Corrosion Product on Solenoid Seat Valve Precluding Proper Closing of Valve |
- on 870818,main Steam Relief Valve Accumulator Assembly C Found to Have Seat Leakage Exceeding Acceptance Criteria.Caused by Dirt/Corrosion Product on Solenoid Seat Valve Precluding Proper Closing of Valve
| | | 05000271/LER-1987-010, :on 870820,primary Containment Isolation Sys Group III Isolation Occurred Due to High Radiation Signal from Refuel Floor Zone Radiation Detector.Caused by Defective Procedure.Isolation Reset |
- on 870820,primary Containment Isolation Sys Group III Isolation Occurred Due to High Radiation Signal from Refuel Floor Zone Radiation Detector.Caused by Defective Procedure.Isolation Reset
| | | 05000271/LER-1987-011, :During 870818 & 20,requirements of Tech Spec 3.5.H.4 for Min Subsystems Required for Refueling Not Satisfied.Caused by Procedural Error.Required Equipment During Refueling & Operation Clarified |
- During 870818 & 20,requirements of Tech Spec 3.5.H.4 for Min Subsystems Required for Refueling Not Satisfied.Caused by Procedural Error.Required Equipment During Refueling & Operation Clarified
| | | 05000271/LER-1987-012, :on 870826,high Main Steam Line Radiation Scram Occurred.Caused by Inadequate Procedures Re Radiography of Pipe Weld Near Main Steam Line Radiation Detectors. Radiography Testing Requirements Revised |
- on 870826,high Main Steam Line Radiation Scram Occurred.Caused by Inadequate Procedures Re Radiography of Pipe Weld Near Main Steam Line Radiation Detectors. Radiography Testing Requirements Revised
| | | 05000271/LER-1987-013, :on 870904,full Reactor Scram & Primary Containment Isolation Sys (PCIS) Actuation Occurred.Caused by Personnel Error.Scram & PCIS Isolations Reset & Sys Returned to Normal |
- on 870904,full Reactor Scram & Primary Containment Isolation Sys (PCIS) Actuation Occurred.Caused by Personnel Error.Scram & PCIS Isolations Reset & Sys Returned to Normal
| | | 05000271/LER-1987-014, :on 870908 & 10,inadvertent Scrams Occurred Due to Lack of Inputs to Power Range Neutron Monitor.Caused by Personnel Error & Inadequate Determination of First Event. Operator Training Will Be Revised |
- on 870908 & 10,inadvertent Scrams Occurred Due to Lack of Inputs to Power Range Neutron Monitor.Caused by Personnel Error & Inadequate Determination of First Event. Operator Training Will Be Revised
| | | 05000271/LER-1987-015, :on 871003,reactor Scramed Due to Turbine Control Valve Rapid Opening & Fast Closure.Caused by Turbine Control Oil Sys Malfunction.Turbine Vendor Utilized Onsite to Rebalance Turbine Oil Pressure |
- on 871003,reactor Scramed Due to Turbine Control Valve Rapid Opening & Fast Closure.Caused by Turbine Control Oil Sys Malfunction.Turbine Vendor Utilized Onsite to Rebalance Turbine Oil Pressure
| | | 05000271/LER-1987-016, :on 871105,HPCI Sys Declared Inoperable Due to Erroneous Flow Indication.Caused by Improper Venting of Flow Transmitters.Transmitter Vented & Filled W/Water to Remove Air |
- on 871105,HPCI Sys Declared Inoperable Due to Erroneous Flow Indication.Caused by Improper Venting of Flow Transmitters.Transmitter Vented & Filled W/Water to Remove Air
| | | 05000271/LER-1987-017, :on 871108,main Turbine Trip & Reactor Scram Occurred.Caused by Mechanical Restriction of Manual Operators on Feedwater Regulating Valves.Valve Restrictions Removed & Repaired.Scram Procedure Revised |
- on 871108,main Turbine Trip & Reactor Scram Occurred.Caused by Mechanical Restriction of Manual Operators on Feedwater Regulating Valves.Valve Restrictions Removed & Repaired.Scram Procedure Revised
| | | 05000271/LER-1987-018, :on 871114,RCIC Sys Inoperable Due to Damaged Turbine Exhaust Check Valve.Broken Disc Replaced & RCIC Sys Tested Satisfactorily.Disc Will Be Evaluated Regularly Per Rev to Inservice Testing Program |
- on 871114,RCIC Sys Inoperable Due to Damaged Turbine Exhaust Check Valve.Broken Disc Replaced & RCIC Sys Tested Satisfactorily.Disc Will Be Evaluated Regularly Per Rev to Inservice Testing Program
| | | 05000271/LER-1987-019, :on 871215,surveillance of LPCI Reactor Vessel Shroud Level Permissive for Containment Spray Missed.Caused by Personnel Error.Personnel Counseled & Test in Question Immediately Completed |
- on 871215,surveillance of LPCI Reactor Vessel Shroud Level Permissive for Containment Spray Missed.Caused by Personnel Error.Personnel Counseled & Test in Question Immediately Completed
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