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Category:Letter
MONTHYEARML25059A4082025-03-0303 March 2025 Project Manager Reassignment for Monticello Nuclear Generating Plant L-MT-25-012, Pressure Temperature Limits Report for the Monticello Nuclear Generating Plant, Revision 22025-02-25025 February 2025 Pressure Temperature Limits Report for the Monticello Nuclear Generating Plant, Revision 2 IR 05000263/20240042025-01-30030 January 2025 Integrated Inspection Report 05000263/2024004 ML25006A1522025-01-16016 January 2025 Section 106 Consultation of Monticello SLR-Shakopee ML25006A1502025-01-16016 January 2025 Section 106 Consultation for Monticello SLR-Lower Sioux Indian Community ML25006A1512025-01-16016 January 2025 Section 106 Consultation for Monticello SLR-Mille Lacs Band of Ojibwe ML25010A0722025-01-10010 January 2025 Notification of NRC Baseline Inspection and Request for Information Inspection Report 05000263/2025002 IR 05000263/20244042025-01-0606 January 2025 Material Control and Accounting Program Inspection Report 05000263/2024404 (Public) ML24310A3442024-12-30030 December 2024 Transmittal Letter for Renewed License ML24270A1552024-12-19019 December 2024 Issuance of Amendment No. 213 Revise Technical Specification 5.6.5, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (Ptlr), and Update Neutron Fluence Methodology ML24354A2952024-12-18018 December 2024 ISFSI and Monticello Nuclear Generating Plant - Independent Spent Fuel Storage Installation Decommissioning Funding Plans L-MT-24-045, 2024 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.462024-12-13013 December 2024 2024 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.46 ML24353A1192024-12-12012 December 2024 Usepa Monticello Re-license Feis Comments (1) IR 05000263/20244022024-12-0606 December 2024 – Security Baseline Inspection Report 05000263/2024402; Independent Spent Fuel Storage Installation Security Inspection Report 07200058/2024401 IR 05000263/20244032024-12-0606 December 2024 – Security Baseline Inspection Report 05000263/2024403 ML24324A0082024-12-0404 December 2024 Letter to Minnesota State Historic Preservation Office Section 106 Consultation Regarding the Monticello Nuclear Generating Plant Subsequent License Renewal Application IR 05000263/20243012024-11-27027 November 2024 NRC Initial License Examination Report 05000263/2024301 L-MT-24-042, Update to the Technical Specifications Bases2024-11-22022 November 2024 Update to the Technical Specifications Bases ML24323A2142024-11-21021 November 2024 – Relief Request RR-017, Inservice Inspection (ISI) Impracticality During the Fifth Ten-Year Interval ML24318C5002024-11-19019 November 2024 Letter to Robert Blanchard Tribal Chairman Bad River Band of Lake Superior Chippewa Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5322024-11-18018 November 2024 Letter to Robert Vanzile Jr Chairman Sokaogon Chippewa Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5282024-11-18018 November 2024 Letter to Jamie Azure Chairman Turtle Mountain Band of Chippewa Indians Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5242024-11-18018 November 2024 Letter to Cole Miller Chairman Shakopee Mdewakaton Sioux Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24312A1732024-11-18018 November 2024 Ltr. to Shawn Hafen, Site Vice President, Monticello Nuclear Generating Plant, Re., NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5032024-11-18018 November 2024 Letter to Anthony Reider President Flandreau Santee Sioux Tribe NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5232024-11-18018 November 2024 Letter to Alonzo Denney Chairman Santee Sioux Nation Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5022024-11-18018 November 2024 Letter to Reggie Wassana Governor Cheyenne and Arapaho Tribes NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5162024-11-18018 November 2024 Letter to James Williams Jr Chairman Lac Vieux Desert Band of Lake Superior Chippewa Indians Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5222024-11-18018 November 2024 Letter to Darrell Seki Chairman Red Lake Nation Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5102024-11-18018 November 2024 Letter to Louis Taylor Chairman Lac Courte Oreilles Band of Lake Superior Chippewa Indians Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5212024-11-18018 November 2024 Letter to Nicole Boyd Chairwoman Red Cliff Band of Lake Superior Chippewa Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5012024-11-18018 November 2024 Letter to Catherine Chavers Tribal Chairwoman Bois Forte Band Chippewa Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5202024-11-18018 November 2024 Letter to Grant Johnson President Prairie Island Indian Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5192024-11-18018 November 2024 Letter to Michael Laroque President Minnesota Chippewa Tribe Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5182024-11-18018 November 2024 Letter to Gena Kakkak Chairwoman Menominee Indian Tribe of Wisconsin Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5042024-11-18018 November 2024 Letter to Jeffrey Stiffarm President Fort Belknap Indian Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5112024-11-18018 November 2024 Letter to John Johnson President Lac Du Flambeau Band of Lake Superior Chippewa Indians Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24312A3512024-11-18018 November 2024 Letter to Amy Spong, Deputy State Historic Preservation Officer, Re., NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5172024-11-18018 November 2024 Letter to Robert Larsen President Lower Sioux Indian Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5072024-11-18018 November 2024 Letter Timothy Rhodd Chairman Iowa Tribe of Kansas and Nebraska Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5252024-11-18018 November 2024 Letter to J Garrett Renville Tribal Chairman Sisseton Wahpeton Oyate of the Lake Traversee Re NOA Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5262024-11-18018 November 2024 Letter to Lonna Johnson Street Chairperson Spirit Lake Nation Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5092024-11-18018 November 2024 Letter to Doreen Blaker President Keweenaw Bay Indian Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5302024-11-18018 November 2024 Letter to Michael Fairbanks Chairman White Earth Nation Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5052024-11-18018 November 2024 Letter to Bruce Savage Tribal Chairperson Found Du Lac Band of Lake Superior Chippewa Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5062024-11-18018 November 2024 Letter to Robert Deschampe Tribal Chair Grand Portage Band of Lake Superior Chippewa Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24318C5152024-11-18018 November 2024 Letter to Faron Jackson Sr Chairman Leech Lake Band of Ojibwe Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR ML24312A3462024-11-18018 November 2024 Letter to Jaime Loichinger Director Office of Federal Agency Programs, Achp NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24318C5292024-11-18018 November 2024 Letter to Kevin Jensvold Tribal Chairman Upper Sioux Community Re NOA of the Final EIS for the Monticello Nuclear Generating Plant, Unit 1 SLR ML24312A3202024-11-18018 November 2024 Letter to Durell Cooper Tribal Chairman Apache Tribe of Oklahoma Re NOA of the Final EIS for the Monticello Nuclear Generating Plant Unit 1 SLR 2025-03-03
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000263/LER-2024-002, Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure2024-08-27027 August 2024 Low Pressure Coolant Injection Inoperable Due to Motor Valve Failure 05000263/LER-2024-001, Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component2024-04-25025 April 2024 Reactor Scram, Containment Isolation, and Cooldown Rate Outside of Limits Following Technician Adjustment of Wrong Component 05000263/LER-2023-003, Condition Prohibited by Technical Specifications Due to Inoperable Main Steam Line Low Pressure Isolation Switch2023-12-0404 December 2023 Condition Prohibited by Technical Specifications Due to Inoperable Main Steam Line Low Pressure Isolation Switch 05000263/LER-2023-002, Reactor Scram and Containment Isolation Due to Valve Responses During Main Turbine Control Valve Testing2023-11-13013 November 2023 Reactor Scram and Containment Isolation Due to Valve Responses During Main Turbine Control Valve Testing 05000263/LER-2023-001, Main Steam Isolation Valve Leakage Exceeds Technical Specification Requirements Due to Stem Scoring2023-05-17017 May 2023 Main Steam Isolation Valve Leakage Exceeds Technical Specification Requirements Due to Stem Scoring 05000263/LER-2022-001, Loss of Control Room Envelope Operability2022-07-0707 July 2022 Loss of Control Room Envelope Operability 05000263/LER-2019-002, Two Manual Primary Containment Isolation Valves Found Open Resulting in a Condition Prohibited by Technical Specification2019-08-0909 August 2019 Two Manual Primary Containment Isolation Valves Found Open Resulting in a Condition Prohibited by Technical Specification 05000263/LER-2019-001, RHR Decay Heat Removal Pump Start Permissive Logic Hardening Error2019-06-13013 June 2019 RHR Decay Heat Removal Pump Start Permissive Logic Hardening Error 05000263/LER-1917-006, Regarding Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests Due to Use of a Test Fixture2018-01-12012 January 2018 Regarding Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests Due to Use of a Test Fixture 05000263/LER-1917-005, Regarding Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel2017-09-20020 September 2017 Regarding Diesel Generator Emergency Service Water System Automatic Transfer to Alternate Shutdown Panel 05000263/LER-1917-004, Regarding High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test2017-08-16016 August 2017 Regarding High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test 05000263/LER-1917-003, Regarding Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits2017-06-14014 June 2017 Regarding Main Steam Isolation Valve Leakage Exceeds Technical Specification Limits 05000263/LER-1917-002, Regarding Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements2017-06-13013 June 2017 Regarding Main Steam Isolation Valve Closure Time Outside of Technical Specification Requirements 05000263/LER-1917-001, Regarding Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated2017-06-13013 June 2017 Regarding Reactor Scram and Group II Isolation Due to 11 Reactor Feed Pump (RFP) Removal from Service with 12 RFP Isolated 05000263/LER-1916-003-01, Regarding HPCI Declared Inoperable Due to Excessive Water Level in Turbine2017-05-25025 May 2017 Regarding HPCI Declared Inoperable Due to Excessive Water Level in Turbine 05000263/LER-2016-002, Regarding Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability2016-09-30030 September 2016 Regarding Inadequate Appendix R Fire Barrier Impacts Safe Shutdown Capability 05000263/LER-2016-001, Regarding High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak2016-05-18018 May 2016 Regarding High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak 05000263/LER-2015-006, Regarding Reactor Scram Due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line2016-01-21021 January 2016 Regarding Reactor Scram Due to Group 1 Isolation from Foreign Material in the Main Steam Flow Instrument Line 05000263/LER-2015-007, Regarding Loss of Residual Heat Removal Capability2016-01-21021 January 2016 Regarding Loss of Residual Heat Removal Capability 05000263/LER-2015-005, Regarding Use of the Reactor Water Cleanup System to Lower Level Without Declaring an OPDRV with Secondary Containment Inoperable - Extent of Condition Review2015-10-0202 October 2015 Regarding Use of the Reactor Water Cleanup System to Lower Level Without Declaring an OPDRV with Secondary Containment Inoperable - Extent of Condition Review 05000263/LER-2015-004, Regarding Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements2015-08-21021 August 2015 Regarding Past Inoperability of Turbine Stop Valve Scram Function Exceeded Technical Specification Requirements 05000263/LER-2015-003, Regarding Use of the Reactor Water Cleanup System to Lower Level Without Declaring an Operation with a Potential to Drain the Reactor Vessel (OPDRV) with Secondary Containment Inoperable2015-07-13013 July 2015 Regarding Use of the Reactor Water Cleanup System to Lower Level Without Declaring an Operation with a Potential to Drain the Reactor Vessel (OPDRV) with Secondary Containment Inoperable 05000263/LER-2014-010-02, Regarding Physical Security Plan Inaccuracy Revealed Past Security Vulnerability2015-07-0101 July 2015 Regarding Physical Security Plan Inaccuracy Revealed Past Security Vulnerability 05000263/LER-2015-002, From Monticello Nuclear Generating Plant Regarding Loss of Shutdown Cooling Due to Improperly Landed Jumper Wire2015-06-29029 June 2015 From Monticello Nuclear Generating Plant Regarding Loss of Shutdown Cooling Due to Improperly Landed Jumper Wire 05000263/LER-2015-001, Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment Operable2015-06-16016 June 2015 Regarding Operations with a Potential to Drain the Reactor Vessel (OPDRV) Without Secondary Containment Operable 05000263/LER-2014-011, Regarding Two Emergency Diesels Inoperable Due to Human Error2015-02-26026 February 2015 Regarding Two Emergency Diesels Inoperable Due to Human Error 05000263/LER-2013-007-02, Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures2015-01-27027 January 2015 Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures 05000263/LER-2014-008, Regarding Opening Identified in Fire Barrier2014-07-14014 July 2014 Regarding Opening Identified in Fire Barrier 05000263/LER-2014-007, Regarding Non-compliance with Technical Specification 3.4.9 - Reactor Coolant System Pressure and Temperature Limits2014-06-12012 June 2014 Regarding Non-compliance with Technical Specification 3.4.9 - Reactor Coolant System Pressure and Temperature Limits 05000263/LER-2014-006, Regarding Secondary Containment Doors Opened Simultaneously2014-05-23023 May 2014 Regarding Secondary Containment Doors Opened Simultaneously 05000263/LER-2014-005, Regarding Appendix R Fire Door Failed to Latch2014-05-19019 May 2014 Regarding Appendix R Fire Door Failed to Latch 05000263/LER-2014-004, Time to Energize Loads Greater than Surveillance Requirement2014-04-11011 April 2014 Time to Energize Loads Greater than Surveillance Requirement 05000263/LER-2014-002, Regarding Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing2014-04-0808 April 2014 Regarding Torus to Drywell Vacuum Breaker Did Not Indicate Closed During Testing 05000263/LER-2014-003, Regarding Torus to Drywell Vacuum Breaker Dual Indication During Testing2014-04-0808 April 2014 Regarding Torus to Drywell Vacuum Breaker Dual Indication During Testing 05000263/LER-2013-007-01, Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures2014-03-28028 March 2014 Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures 05000263/LER-2014-001, Regarding Primary System Leakage Found in Recirculation Pump Upper Seal Heat Exchanger2014-03-14014 March 2014 Regarding Primary System Leakage Found in Recirculation Pump Upper Seal Heat Exchanger 05000263/LER-2013-008-01, Regarding Both Secondary Containment Access Doors Briefly Opened Simultaneously2014-03-12012 March 2014 Regarding Both Secondary Containment Access Doors Briefly Opened Simultaneously 05000263/LER-2013-003-02, Regarding Inadequate External Flooding Procedure2014-01-28028 January 2014 Regarding Inadequate External Flooding Procedure 05000263/LER-2013-006-01, Regarding Unanalyzed Condition for Emergency Diesel Generator Fuel Oil Pumps Train Separation2013-12-19019 December 2013 Regarding Unanalyzed Condition for Emergency Diesel Generator Fuel Oil Pumps Train Separation 05000263/LER-2013-000-08, Both Secondary Containment Access Doors Briefly Opened Simultaneously2013-11-0808 November 2013 Both Secondary Containment Access Doors Briefly Opened Simultaneously 05000263/LER-2013-007, Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures2013-10-28028 October 2013 Regarding Unanalyzed Condition Due to Inadequate Flooding Procedures 05000263/LER-2013-006, Regarding Unanalyzed Condition for Emergency Diesel Generator Fuel Oil Pumps Train Separation2013-10-18018 October 2013 Regarding Unanalyzed Condition for Emergency Diesel Generator Fuel Oil Pumps Train Separation 05000263/LER-2013-003-01, Regarding Inadequate External Flooding Procedure2013-09-26026 September 2013 Regarding Inadequate External Flooding Procedure 05000263/LER-2013-004, Loss of Normal Off-Site Power as a Result of Switch Gear Fault2013-08-12012 August 2013 Loss of Normal Off-Site Power as a Result of Switch Gear Fault 05000263/LER-2013-003, Regarding Inadequate External Flooding Procedure2013-07-30030 July 2013 Regarding Inadequate External Flooding Procedure 05000263/LER-2013-002, Regarding Essential Bus Transfer During 2R Transformer Testing2013-07-23023 July 2013 Regarding Essential Bus Transfer During 2R Transformer Testing 05000263/LER-2013-001, E SRV Low-Low Set Tailpipe Dp Root Valve Found Closed2013-06-0707 June 2013 E SRV Low-Low Set Tailpipe Dp Root Valve Found Closed 05000263/LER-2012-003-01, Regarding Automatic Reactor Scram During Maintenance on 4160V 12-Bus Ammeter2013-01-18018 January 2013 Regarding Automatic Reactor Scram During Maintenance on 4160V 12-Bus Ammeter 05000263/LER-2012-005, Regarding Partial Group II Isolation During Removal of Original Steam Dryer2013-01-11011 January 2013 Regarding Partial Group II Isolation During Removal of Original Steam Dryer 05000263/LER-2012-004, Regarding High Pressure Coolant Injection Inoperable When Inverter Is Out of Service2012-11-30030 November 2012 Regarding High Pressure Coolant Injection Inoperable When Inverter Is Out of Service 2024-08-27
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e Xcel Energya November 7,2008 L-MT-08-068 10 CFR Part 50.73 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 Monticello Nuclear Generating Plant Docket No. 50-263 Renewed License No. DPR-22 LER 2008-005, "Reactor Scram due to Loss of Normal Offsite Power" A Licensee Event Report (LER) for this occurrence is attached.
This letter contains no new commitments and no revisions to existing commitments.
President, Monticello Nuclear Generating Plant States Power - Minnesota Enclosure cc:
Administrator, Region Ill, USNRC Project Manager, Monticello, USNRC Resident Inspector, Monticello, USNRC 2807 West County Road 75 Monticello, Minnesota 55362-9637 Telephone: 763-295-5151 Fax: 763-295-1454
LICENSEE EVENT REPORT (LER) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(2)(v) 20.2203(a)(2)(vi) 20.2203(a)(3)(i) 50.46(a)(3)(ii) 50.73(a)(2)(i)(A) 50.73(a)(2)(i)(B) 50.73(a)(2)(i)(C) 50,73(a)(2)(ii)(A)
LICENSEE CONTACT FOR THlS LER (12) 50.73(a)(2)(v)(C) 50.73(a)(2)(v)(D) 50.73(a)(2)(vii) 50,73(a)(2)(viii)(A) 50.73(a)(2)(viii)(B)
NAME Ron Baumer in NRC Form 366A TELEPHONE NUMBER (Include Area Code) 763-295-1 357 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THlS REPORT (13)
REPORTABLE TO EPIX YEAR ABSTRACT On September I I, 2008 at 2248 hours0.026 days <br />0.624 hours <br />0.00372 weeks <br />8.55364e-4 months <br />, the site experienced a lockout of the primary auxiliary transformer with the reserve transformer isolated for planned maintenance. This resulted in a Loss of Normal Off-site Power (LONOP) and an associated SCRAM. The cause of the event was the A and B phase conductors supplying power to the primary auxiliary transformer faulted to ground. Corrective actions taken or planned are: the faulted cable was repaired, repaired other degraded cable splices identified by the extent of condition, and improvements in the cable condition monitoring program.
COMPONENT F:::"RER TO EPIX Y
CAUSE
C
'OMPoNENT CBL SYSTEM FK SUPPLEMENTAL REPORT EXPECTED (14)
KKRER XOOO
CAUSE
EXPECTED SUBMISSION DATE (1 5)
YES (If yes, complete EXPECTED SUBMISSION DATE).
SYSTEM MONTH X
DAY NO (9-2007)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
DOCKET (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVISION Monticello Nuclear Generating Plant 05000263 YEAR NUMBER NUMBER 2of5 2008 - 005 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (1 7 )
I
Event Description
At the Monticello NGP, three transformers are provided to supply the plant with offsite power from the substation. All three sources can independently provide adequate power for the plant's safety-related loads. These transformers and their interconnections to the substation are as follows: The primary station auxiliary transformer (2R) is fed from a 345 KV Bus and underground cabling. The 2R transformer is of adequate size to provide the plant's full auxiliary load requirements. The reserve transformer (1 R) is fed from a 115 KV substation via an overhead line. The 1 R transformer is of adequate size to provide the plant's full auxiliary load requirements. The reserve auxiliary transformer (IAR) may be fed from two separate 13.8 KV sources. The IAR transformer is sized to provide only the plant's essential 4160 Vac buses and connected loads.
On September I I, 2008, the plant was operating at 100% power with transformer [XFMR] I R
isolated and tagged out for planned maintenance. Off-site power was supplied via transformer 2R with IAR and on-site emergency diesel generators (EDGs) [DG] as backup power sources.
At approximately 2248 hours0.026 days <br />0.624 hours <br />0.00372 weeks <br />8.55364e-4 months <br />, a 34.5 kV breaker [BKR] opened, de-energizing the 2R transformer and causing a Loss of Normal Off-site Power (LONOP). A reactor SCRAM was experienced and all rods inserted normally. Both # I 1 and #I2 EDG auto-started but were not needed for loading. Buses 15 and 16 were automatically powered from IAR transformer.
Control Room operators took action per applicable procedures to control Reactor vessel level and pressure.
I During the scram and recovery, the following occurred:
The High Pressure Coolant Injection (HPCI) [BJ] turbine [TRB] failed to trip at the +48 inch Reactor Vessel level signal. Operators manually isolated the steam line for the turbine. HPCl was declared inoperable and an Event Notification (ENS) was made to the NRC on 09/12/2008 at 0655. lnvestigation determined the failure of the HPCl to trip was due to three effects: the trip solenoid valve [LSV] had been misassembled, no periodic maintenance on the valve, and a battery voltage well above the minimum required, but slightly below the normally observed voltage. The first two conditions were responsible for the degraded performance of the valve. The battery voltage, while acceptable, did cause the degradation from the misassembled valve and the lack of periodic maintenance to become apparent. The diaphragm was replaced, the valve wa:
reassembled correctly, and HPCl was declared operable.
The Automatic Depressurization System (ADS) [VB] timer [TMR] showed erratic indication following the event. The ADS auto-initiation was inhibited per procedure. The ADS system was declared inoperable, but manual safety relief valve operation was available. This was reported to the NRC in the event notification made on 09/12/2008 a 0655. lnvestigation determined the erratic display was due to an issue with the NRC FORM
?&A (9-2007)
IRC FORM 366A 3-2007)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
FACILITY NAME (I)
DOCKET (2)
LER NUMBER (6)
PAGE (3)
SEQUENTIAL REVISION donticello Nuclear Generating Plant 05000263 YEAR NUMBER NUMBER 3of5 2008 - 005 00
'EXT (If more space is required, use additional copies of NRC Form 366A) (1 7 )
indication device and not the actual ADS timer utilized in the Emergency Core Cooling System [BM] logic. The ADS system was declared operable.
A second Group 2 isolation signal was received when reactor water level lowered below
+9 inches while pumping drywell sumps. All Group 2 valves except the drywell sump isolation valves were closed due to a previously reported Group 2 signal. The drywell sump valves had been opened to allow manual pump down of the sumps. The sump valves closed as expected. An ENS notification was made to the NRC on 09/12/2008 at 1656.
During the event, operators were challenged with isolating water in-sources to the reactor vessel to maintain level. At no time did the reactor water level reach the main steam lines, however, opportunities for improved performance were identified. A review of the reactor vessel level challenges by the Monticello PRA group determined this was of low safety significance.
Ivent Analysis The above events were reported under 10 CFR 50.72(b)(2)(iv)(B), "Reactor Protection System 4ctuation - Critical, 50.72(b)(3)(iv)(A), "Engineered Safety Feature Actuation," and 50.72(b)(3)(v)(B), "Event or Condition that could have prevented Fulfillment of a Safety
=unction." Therefore, these events are reportable under 50.73(a)(2)(iv), "System Actuation (for
?PS and ESF)," and 50.73(a)(2)(v) (B) "an event or condition that could have prevented
'ulfillment of a Safety Function (for HPCI)." The loss of HPCI is considered a safety system Functional failure.
Safety Significance
The station Probabilistic Risk Analysis group reviewed the event and provided the following
safety significance
Accounting for the Division I RHRSW [BI] system being out of service, and crediting the potential for re-establishing power from the 1 R transformer within six hours from the transient, Conditional Core Damage Probability (CCDP) is estimated to be 3.86 E-07, and Conditional Large Early Release Probability (CLERP) is estimated to be 9.76 E-08. 1 R transformer recovery within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> is credited with 90% assumed success. Several conditions were evaluated with regard to their potential for complicating recovery from this event, and thus contributing to the assessed risk. Upon reaching the ECCS automatic initiation setpoint, the ADS timer was noticed to be displaying erratically, and ADS logic was inhibited to prevent an inadvertent reactor vessel depressurization. This is assumed to have an insignificant affect on risk since the timer is intended to be inhibited per the EOP's for all emergency events, and the erratic display was strictly an indication device and not the actual ADS timer utilized in the
- - - NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
Monticello Nuclear Generating Plant TEXT (If more space is required, use additional copies of NRC Form 366A) (1 7 )
ECCS logic. The HPCl [BJ] and RCIC [BN] systems initiated automatically and injected to the reactor normally, but HPCl did not automatically trip at the high water level setpoint. Although the operators were successful at preventing water from filling the steam lines to the point of affecting HPCl andlor RCIC, failing to do so could result in potential negative impact on systems (HPCI, RCIC, and SRV's) that tap off of the steam lines. In the case where HPCl and RCIC are threatened with steam line flooding, much more favorable conditions exist. To be in this condition implies that initial water injection was successful. This results in conditions where vessel water inventory is sub cooled and relatively high, and decay heat levels are relatively low, allowing ample time to recover potentially failed equipment prior to dependence on their availability. Specifically, there is more than adequate time to drain HPCl and RCIC steam lines prior to water level dropping to the top of active fuel. Additionally, Monticello specific thermo-hydraulic calculations show that in cases where reactor water level is initially maintained for a short period (less than one minute) following a non-LOCA transient, nominal CRDH flow to the reactor vessel is adequate to maintain water inventory such that core damage will be precluded.
In conclusion, overall impact of the events on plant safety was small due to minimal increases in the conditional core damage probability (less than 1.0 E-06), and the conditional large early release probability (less than 1.0 E-07).
Cause
The root cause of the event was the A and B phase conductors supplying power to the 2R transformer faulted to ground, resulting in the 34.5 kV Breaker opening as designed to protect equipment from fault current damage. The opening of the 34.5 kV breaker with transformer 1 R out of service resulted in a loss of normal off site power (LONOP) and a reactor scram.
Due to the destruction of the failed insulation (splice and cable), it is impossible to determine the exact failure mechanism and sequence of the two faults.
Corrective Action
The following corrective actions have been completed or are planned:
Faulted cable and splice were replaced. Transformer 2R was returned to service.
Testing identified additional degraded splices, all splices were replaced.
Identified all underground cable access points and periodically inspect these points for water.
The station will allocate and prioritize resources to carry out actions established in the Cable Condition Monitoring Program.
A Preventive Maintenance request was created to include the HPCl solenoid valve in the preventative maintenance schedule.
DOCKET (2) 05000263 PAGE (3) 4 of 5 LER NUMBER (6)
YEAR 2008 - 005 -
00 SEQUENTIAL NUMBER REVISION NUMBER NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (9-2007)
LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
Monticello Nuclear Generating Plant TEXT (If more space is required, use additional copies of NRC Form 366A) (1 7)
Operational challenges associated with reactor vessel level have been assessed by the station and the results entered into the corrective action program.
Failed Component Identification Cablec XLPE cables rated at 35 kV, 750 kcmil, 100% insulation, aluminum conductor, manufactured in 1985.
Previous Similar Events
- 1. 611 711 987: Conductor on a transformer separated from its bushing, causing a voltage disturbance which tripped both Circulating Water pumps. The reactor then scrammed when vacuum decreased.
- 2. 11/25/1997: An underground 480V cable electrical fault led to the loss of the Recombiners and subsequent low vacuum condition. The affected underground cables were replaced.
DOCKET (2) 05000263 PAGE (3) 5 o f 5 LER NUMBER (6' REVISION NUMBER YEAR 2008 - 005 -
00 SEQUENTIAL NUMBER
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05000263/LER-2008-001, Re Non-Conservative High Energy Line Break Analysis Discovered During Extended Power Uprate Review | Re Non-Conservative High Energy Line Break Analysis Discovered During Extended Power Uprate Review | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000263/LER-2008-002, Regarding Inoperability of Channel B Spent Fuel Pool Radiation Monitor Due to Incorrect Calibration | Regarding Inoperability of Channel B Spent Fuel Pool Radiation Monitor Due to Incorrect Calibration | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2008-003, For Monticello Regarding Control Room Emergency Filtration Trains Inoperability in Recirculation Mode | For Monticello Regarding Control Room Emergency Filtration Trains Inoperability in Recirculation Mode | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) | 05000263/LER-2008-004, Required Manual Isolation Time for High Energy Line Break Calculation Not in Procedure | Required Manual Isolation Time for High Energy Line Break Calculation Not in Procedure | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(viii)(A) | 05000263/LER-2008-005, Regarding Reactor Scram Due to Loss of Normal Offsite Power | Regarding Reactor Scram Due to Loss of Normal Offsite Power | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(viii)(B) | 05000263/LER-2008-006, Regarding Loss of Normal Offsite Power Due to Equipment Contact with 115KV Lines | Regarding Loss of Normal Offsite Power Due to Equipment Contact with 115KV Lines | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(viii)(A) | 05000263/LER-2008-007, Loss of Shutdown Cooling Due to ESF Actuation | Loss of Shutdown Cooling Due to ESF Actuation | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(viii)(A) | 05000263/LER-2008-008, For Monticello, Regarding Technical Specification Required Shutdown Margin Not Met During All Conditions for Refueling Outage 23 | For Monticello, Regarding Technical Specification Required Shutdown Margin Not Met During All Conditions for Refueling Outage 23 | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System |
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