05000263/LER-2001-007

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LER-2001-007,
Docket Number
Event date: 02-24-2001
Report date: 04-23-2001
Reporting criterion: 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2632001007R00 - NRC Website

Description On February 24, 2001 while operating at 100% power, the Monticello Nuclear Generating Plant (MNGP) staff discovered that the High Pressure Coolant Injection (HPCI)1 system and both divisions of the Low Pressure Coolant Injection (LPCI)2 mode of the Residual Heat Removal (RHR)2 system were inoperable due to the failure to test the testable check valves' as required by the Technical Specification and ASME Code Section Xl. The Reactor Core Isolation Cooling (RCIC)4 system and Core Spray (CS)5 system testable check valves were believed to have been tested as required by the Technical Specification and ASME Code Section Xl. Later, after the plant was shutdown, it was determined that the CS system testable check valve had not been tested using the full accident flow rate and therefore did not meet the Technical Specification and ASME Code Section XI requirements. The RCIC system testable check valve, although disassembled and inspected during the January, 2000 refueling outage, may not have been partial stroke tested after reassemble and thus did not meet the Technical Specification and ASME Code Section XI requirements.

MNGP's Technical Specification have a surveillance requirement in 4.15.B that states:

"Inservice Testing of Quality Group A, B, and C pumps and valves shall be performed in accordance with the requirements for ASME Code Class 1, 2 and 3 pumps and valves, respectively, contained in Section XI of the ASME Boiler and Pressure Vessel Code and applicable Addenda as required by 10 CFR 50, Section 50.55a(g) except where relief has been granted by the Commission pursuant to 10 CFR 50, Section 50.55(a)(g)(6)(i), or where alternate testing is justified in accordance with Generic Letter 89-04.

Since the LPIC mode of the RHR system and the HPCI system were declared inoperable, the Limiting Condition for Operation (LCO) for Technical Specification 3.5.A was entered and the plant was required to be in a condition for which the inoperable equipment is not required to be operable (in this case less than 212 degrees). The plant reached shutdown conditions on February 25, 2001 within the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO.

During the review to determine the extent of condition for this event, additional items were discovered to not comply with the Technical Specification and ASME Code Section XI inservice testing requirements. These additional items are discussed below.

While shutdown on March 2, 2001 the HPCI system suction check valve (HPCI-32) from the condensate storage tank (CST)6 was discovered to not comply with the testing requirements specified in the Technical Specifications and ASME Code Section Xl. This valve had not been tested in the closed direction. This valve has a safety related function to close to assure the suppression pool water does not reverse flow, when Primary Containment is pressurized, and bypass Secondary Containment. This could occur for a short period of time when the HPCI system suction motor operated valves are opened automatically during transfer from the CST to the suppression pool on high level in the suppression pool or low level in the CST.

While shutdown on March 2, 2001 the RCIC system suction check valve (RCIC-41) from the condensate storage tank (CST) was discovered to not comply with the testing requirements specified in the Technical Specifications and ASME Code Section Xl. This valve had not been tested in the closed direction. This valve has a safety related function to close to assure the suppression pool water does not reverse flow, when Primary Containment is pressurized, and bypass Secondary Containment. This could occur for a short period of time when the RCIC system suction motor operated valves are opened automatically during transfer from the CST to the suppression pool on low level in the CST.

1 EIIS Code = BJ � 2 EIIS Code = BO � 3 EllS Code = V � 4 EIIS Code = BN � 5 EIIS Code = BM 6 EIIS Code = TK

NRC

� FORM � 366A � (1-2001) While shutdown on March 3, 2001 the Core Spray pump' discharge check valves (CS 9-1 and CS 9-2) were discovered to not comply with the testing requirements specified in the Technical Specifications and ASME Code Section Xl. These valves had not been tested in the closed direction and were incorrectly tested in the open direction. These check valves were determined to have a closed safety function to keep the Core Spray system discharge lines filled with water, prior to pump start, to minimize the possibility of dynamic loading due to pipe voiding. These check valves also have a safety related function in the open direction to pass full accident flow rates for injection into the reactor vessel. The open test was not being performed at the full accident flow rate.

While shutdown on March 12, 2001 the HPCI gland seal condenser' condensate pump discharge check valve (HPCI-20) were discovered to not comply with the testing requirements specified in the Technical Specifications and ASME Code Section Xl. These valves had not been tested in the closed direction. The safety related closed function is the pressure boundary between the non-safety related condensate pump discharge and the safety related cooling water return line to the suction of the HPCI Booster Pump.

While shutdown on March 12, 2001 the RCIC condensate pump discharge check valve (RCIC-14) were discovered to not comply with the testing requirements specified in the Technical Specifications and ASME Code Section Xl. These valves had not been tested in the closed direction. The safety related closed function is the pressure boundary between the non- safety related condensate pump discharge and the safety related return line to the pump suction.

While shutdown on March 12, 2001 it was discovered that the method used for testing the Feedwater (FW)3 check valves (FW-94-1, 97-1, 94-2, and 97-2) did not positively demonstrate they complied with the requirements of the Technical Specification and ASME Code Section Xl. These check valves have an open safety function to pass the HPCI and RCIC system flows into the reactor vessel. The method used for testing the open function did not assure there was not a flow mismatch in the parallel injection lines. A flow mismatch could mask a malfunction of a FW check valve.

Event Analysis

Analysis of Reportability This event is being reported as required by 10CFR50.73(a)(2)(i)(A) as a completion of a plant shutdown required by the Technical Specifications. The completion of the surveillance requirement 4.15.B for the testable check valves could not be completed while at full power.

This event is being reported as required by 10CFR50.73(a)(2)(i)(B) as a condition prohibited by Technical Specification 4.15.B and 3.5.A for the inoperable testable check valves for the LPCI mode of RHR and HPCI systems. These components were not tested in accordance with the ASME Code Section XI Inservice Testing requirements.

Safety Significance

There was no safety significance associated with these events since all components were subsequently demonstrated to be in compliance with the Technical Specification and ASME Code Section XI requirements.

1 EIIS Code = P 2 EIIS Code = COND 3 EIIS Code = SJ

Cause

Maintaining and implementing the 1ST program to current regulatory requirements and industry high standards was not given the proper priority. Therefore, implementing procedures and program documents did not effectively include 1ST requirements from regulatory source documents.

Responsible personnel were unaware of the requirements related to ASME Code Section XI for the component identified in this LER.

Corrective Actions

Implementing procedures and program documents have been revised.

An action to review and appropriately revise the training and qualification programs for the responsible engineers has been entered into the corrective action process.

An independent assessment to determine the extent of condition has been completed. A root cause investigation team has been formed. Findings and actions are being entered into the corrective action program.

The HPCI, LPCI mode of RHR, Core Spray and RCIC systems testable check valves were successfully tested.

The HPCI system pump suction check valve (HPCI-32) closed function was successfully tested.

The RCIC system pump suction check valve (RCIC-41) closed function was successfully tested.

The CS system pump discharge check valves open and closed function was successfully tested.

The HPCI gland seal condenser condensate pump discharge check valve (HPCI-20) closed function was successfully tested.

The RCIC condensate pump discharge check valve (RCIC-14) closed function was successfully tested.

The FW system check valves open function were determined to be acceptable.

Failed Component Identification None Similar Events Filtration Treatment Service Water Pump Requirements.

The corrective actions for these LERs did not prevent this event because they did not correct the lack of organizational knowledge, processes and procedures for implementing the AMSE Code Section XI requirements.