05000250/FIN-2015007-01
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Finding | |
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Title | Failure to Establish a Reasonable Maintenance Effectiveness Demonstration for the Unit 3 Containment Atmospheric Temperature System Used in EOPs |
Description | The NRC identified a Green non-cited violation (NCV) of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, for the licensees failure to adequately monitor the performance or condition of the Unit 3 containment atmospheric temperature system against licensee established goals or demonstrate that the performance of the containment atmospheric temperature system was being effectively controlled through preventive maintenance, such that the system remained capable of performing its intended function. Specifically, there were multiple individual component failures on both units since March 2011 and the Unit 3 containment atmospheric temperature system was non-functional from November 5, 2014, to January 17, 2015. In response to the NRC identified issue, the licensee initiated action report (AR) 02023116, and classified the temperature elements into 10 CFR 50.65(a)(1) status on February 23, 2015, under AR 02004990. The inspectors determined that the performance deficiency was more than minor because it affected the Equipment Performance attribute of the Mitigating Systems cornerstone objective. The licensee did not ensure the availability, reliability, and capability of the Unit 3 containment atmospheric temperature system that was used for emergency operating procedures. The inspectors determined the finding to be of very low safety significance (Green) because it was not a deficiency affecting the design or qualification of a mitigating structure, system, or component (SSC), it did not represent the loss of a system and/or function, it did not represent an actual loss of function of at least a single train or two separate safety systems out-of-service for greater than its Technical Specifications (TS) allowed outage time, and it did not represent an actual loss of a non-TS equipment designated as high safety-significant in accordance with the licensees maintenance rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors determined the finding was indicative of present licensee performance and was associated with the cross-cutting aspect of Evaluation, in the area of Problem Identification and Resolution. Specifically, the licensee failed to thoroughly evaluate issues that were identified in the last three years associated with containment atmospheric temperature system failures to ensure that resolutions addressed causes and extent of conditions commensurate with their safety significance. |
Site: | Turkey Point ![]() |
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Report | IR 05000250/2015007 Section 1R17 |
Date counted | Mar 31, 2015 (2015Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.17 |
Inspectors (proximate) | E Stamm J Bartley N Coovert T Fanelli |
Violation of: | 10 CFR 50.65(a)(1) Technical Specification - Procedures 10 CFR 50.65 Technical Specification |
CCA | P.2, Evaluation |
INPO aspect | PI.2 |
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Finding - Turkey Point - IR 05000250/2015007 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Turkey Point) @ 2015Q1
Self-Identified List (Turkey Point)
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