On March 18, 2010, at approximately 11:14 hours, while shutdown for refueling, boron accumulation was noted on the reactor coolant pump No, 1 seal bypass three quarter inch line 76 upstream of valve 256B.T Based on the amount of boron, a conclusion was reached on April 5, 2010 that this condition could have existed during plant operation and therefore the plant could have been operating contrary to Technical Specification (TS) TS 3.4.13.T The cause of the through wall indication was a five-sixteenths inch rounded weld defect introduced at the time of system construction which propagated through wall as a result of the system loading conditions during plant operations.
There was no extent of condition since boric acid inspections of other locations did not identify any other instances of similar through wall defects.TCorrective action was taken to repair the indication.T There was no significant effect on public health and safety. |
LER-2010-004, Plant Operation Outside Technical Specifications Due to a Leak in the Reactor Coolant Pressure BoundaryIndian Point 2 |
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10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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2472010004R00 - NRC Website |
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� The Energy Industry Identification System Codes are identified within the brackets {}.
DESCRIPTION OF EVENT
On March 18, 2010, at approximately 11:14 hours, while shutdown for refueling, boron accumulation was noted (there was no sign of wetness but rather white, dry boron which indicated that the leak rate was small) in the reactor coolant pressure boundary (RCPB) {AB} on three quarter inch pipe 76 upstream of valve 256B {V}. This check valve is on the 22 Reactor Coolant Pump (RCP) {P} seal {SEAL} bypass line. On April 5, 2010 at approximately 8:42 am the event was independently reviewed and determined to be reportable. Based on the amount of boron, a conclusion was reached that this condition could have existed during plant operation and therefore the plant could have been operating contrary to Technical Specification (TS) TS 3.4.13. This event was recorded in the Indian Point Energy Center corrective action program (CAP) as CR-IP2-2010-01631.
During boric acid walk downs performed during 2R19, boron was identified adjacent to valve 256B. After cleaning was performed, a surface examination was performed on the socket weld attaching the upstream three quarter inch pipe to valve 256B. This surface examination identified a five-sixteenths inch diameter rounded indication which appeared to be the source of the leakage. This indication was repaired and the post repair examination confirmed that the indication had been removed and the repaired area was acceptable.
Since the indication was removed by grinding, a failure analysis was not performed to identify the exact cause of the indication. However, both internal and external operating experience with similar defects strongly suggests that the cause of the through wall indication was a minor weld defect introduced at the time of system construction which propagated through wall as a result of the system loading conditions during plant operations. Literature documents that forging, casting, welding and other material fabrication defects can propagate through the wall of the component and result in leakage after long periods of service. The predominant driver for this propagation is the service induced loads caused by local stress concentrations as well as local pressure and thermal loads caused by local geometry discontinuities.
The original weld defect would not have been repaired at the time of construction if the indication was within the flaw allowable standards and, since the indication was not removed, it can be concluded that it was accepted during the original inspection (there is no documented evidence of the original inspection results). The defect would not have been discovered by inservice inspection since NDE on three quarter inch welds is not required.
The balance of the boric acid walk downs performed on systems which carry borated water during plant operations, identified no other leaks as a result of a through wall flaw in a pipe or in a component.
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05000247/LER-2010-001 | Automatic Reactor Trip as a Result of a Turbine-Generator Trip Due to a Loss of Generator Field Excitation Caused by a Failed Exciter Rectifier | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2010-002 | Manual Reactor Trip Due to a Cooling Water Leak in the Main Generator Exciter Air Cooler | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000247/LER-2010-003 | 450 Broadway, GSB P.O. Box 249 Buchanan, N.Y. 10511-0249Entergy Tel (914) 734-6700 J. E. Pollock Site Vice President NL-10-036 May 10, 2010 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop 0-P1-17 Washington, D.C. 20555-0001 SUBJECT:L Licensee Event Report # 2010-003-00, "Inoperable Emergency Diesel Generators During Refueling Shutdown Due to Inadvertent Isolation of Service Water Cooling Caused by Failure to Properly Verify the In- Service Cooling Header" Indian Point Unit No. 2 Docket No. 50-247 DPR-26 Dear Sir or Madam: Pursuant to 10 CFR 50.73(a)(1), Entergy Nuclear Operations Inc. (ENO) hereby provides Licensee Event Report (LER) 2010-003-00. The attached LER identifies an event which is reportable as a safety system functional failure under 10 CFR 50.73(a)(2)(v). This condition was recorded in the Entergy Corrective Action Program as Condition Report CR-IP2-2010-01367. There are no new commitments identified in this letter. Should you have any questions regarding this submittal, please contact Mr. Robert Walpole, Manager, Licensing at (914) 734-6710. JEP/cbr cc:L Mr. Samuel J Collins, Regional Administrator, NRC Region I NRC Resident Inspector's Office, Indian Point 3 Mr. Paul Eddy, New York State Public Service Commission LEREvents@inpo.org NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 8/31/2010 (9-2007) Estimated burden per response to comply with this mandatory collection request:D50 hours.DReported lessonsDlearned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internetLICENSEE EVENT REPORT (LER) e-mail to infocollects©nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME: INDIAN POINT 2 2. DOCKET NUMBER 1 3. PAGE 05000-247 1 OF 3
4. TITLE: Inoperable Emergency Diesel Generators During Refueling Shutdown Due to Inadvertent Isolation of Service Water Cooling Caused by Failure to Properly Verify the In-Service Cooling Header | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000247/LER-2010-004 | Plant Operation Outside Technical Specifications Due to a Leak in the Reactor Coolant Pressure Boundary | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2010-005 | Technical Specification Prohibited Condition Due to an Inoperable Control Room Ventilation System Caused by a Closed Normally Open Damper | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2010-006 | Safety System Functional Failure Due to Inoperable Reactor Coolant Loop 21 and 22 Wide Range Hot Leg Temperature Indicators Credited for Remote Shutdown per Technical Specification 3.3.4 | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000247/LER-2010-007 | Automatic Reactor Trip Due to a Turbine Trip as a Result of a High Steam Generator Level Trip After Transition to Single Feedwater Purilp Operation | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000247/LER-2010-009 | Automatic Reactor Trip Due to a Turbine-Generator Trip Caused by a Fault of the 21 Main Transformer Phase B High Voltage Bushing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation |
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