Semantic search

Jump to navigation Jump to search
 Entered dateEvent description
ENS 5689618 December 2023 07:40:00The following information was provided by the licensee email: At 0223 EST, on 12/18/2023, while Unit 2 was at 100 percent power in mode 1, the high pressure coolant injection (HPCI) outboard steam isolation valve closed resulting in the HPCI system being declared inoperable. The cause of the outboard steam isolation valve closing is under investigation. HPCI does not have a redundant system, therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The safety function was restored at 0512, on 12/18/23, and HPCI has been declared operable. Reactor core isolation cooling (RCIC) and low pressure emergency core cooling systems (ECCS) were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5689416 December 2023 08:22:00The following information was provided by the licensee via email: On December 16, 2023, at 0350 CST, Grand Gulf Nuclear Station was operating in mode 1 at 81 percent power when an automatic scram occurred due to a turbine trip signal. Before the scram the unit was performing a rod sequence exchange, and no critical work was underway. The cause of the turbine trip signal is not known at this time and is being investigated. All control rods fully inserted, there were no complications, and all plant systems responded as designed. Reactor water level is being maintained by main feedwater and condensate. Reactor pressure is being maintained with main turbine bypass valves. No radiological releases have occurred due to this event. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of the reactor protection system when the reactor is critical and specified system actuation due to expected reactor water level 3 isolation signals on a reactor scram. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Group 2 and Group 3 isolations occurred on the Level 3 isolation signal.
ENS 5689316 December 2023 04:04:00

At 2045 EST on December 15, 2023, it was determined that the reactor coolant system barrier had a through wall flaw with leakage. The leakage is minor in nature and unquantifiable. The leakage is coming from the welded connection of a vent valve for safety injection tank 2A2 outlet valve rendering both trains of high-pressure safety injection inoperable. The unit is being cooled down to cold shutdown to comply with technical specifications. This event is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The unit was heating up after a maintenance outage. The leak was discovered during mode 3 walkdown.

  • * *UPDATE AT 1254 EST ON 02/12/24 FROM B. MURRELL TO T. HERRITY***

The purpose of this notification update is to retract a portion of a previous report, made on 12/16/2023 at 0404 EST (EN 56893). Notification of the event to the NRC was initially made as a result of declaring both trains of unit 2 high pressure safety injection system inoperable due to reactor coolant barrier through wall leak on the vent line for the 2A2 safety injection tank. Subsequent to the initial report, Florida Power and Light has concluded that the through wall leak rate was insignificant, and therefore the safety injection system's safety-related function was maintained. Therefore, this portion of the event is not considered a safety system functional failure and is not reportable to the NRC pursuant 10 CFR 50.72(3)(v)(D). This update does not affect the original 10 CFR 50.72(b)(3)(ii)(A) report for the degraded condition related to the reactor coolant barrier through wall leak. The NRC Resident Inspector has been notified. Notified R2DO (Miller).

ENS 5685012 November 2023 22:02:00The following information was provided by the licensee via email: On November 12, 2023, at 0300 EST, a Watts Bar contractor was transported offsite for medical treatment due to a work-related injury. Upon arrival at an offsite medical facility, medical personnel determined the injury required the individual to be admitted into the hospital and will be kept overnight. The individual was inside of the Radiological Controlled Area, however was free released with no contamination. The injury and hospitalization were reported to the Occupational Safety and Health Administration (OSHA) under 29 CFR 1904.39(a)(2). The contracting agency informed OSHA at 1319 EST. Watt Bar Operations personnel were officially notified by the contracting agency of the report made to OSHA at 1945 EST. This is a four-hour notification, non-emergency for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified.
ENS 5684610 November 2023 03:14:00The following information was provided by the licensee via email: At 0118 EST, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually scrammed due to degrading main condenser vacuum. The scram was not complex, with all systems responding normally post-scram. The main turbine bypass valves opened automatically to maintain reactor pressure. Operations responded and stabilized the plant. Reactor water level is being maintained via feedwater pumps. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not impacted. Due to Reactor Protection System actuation while critical, this event is being reported as a four-hour and eight-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). Unit 1 reactor is currently stable in mode 3. An investigation is in progress into the cause of the degrading condenser vacuum. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5682531 October 2023 14:20:00

The following information was provided by the licensee via phone call and email: On October 31, 2023, at 0800 CDT, River Bend Station discovered that the results of a blind performance sample provided to an Health and Human Services (HHS)-certified testing facility were inaccurate (false negative). This report is being made in accordance with 10 CFR 26.719(c)(3). The HHS-certified testing facility has been informed of the error. The licensee notified the NRC resident inspector.

  • * * RETRACTION AT 0946 EDT ON NOVEMBER 2, 2023 FROM MICAH NAVARRO TO SAMUEL COLVARD * * *

On November 1, 2023, River Bend Station personnel were informed by the HHS-certified testing facility that the cut-off levels used for analysis of the performance testing sample in question were the correct (higher) cut-off levels currently being used by the licensee. This resulted in a correct negative test. The performance testing sample sent to the HHS-certified testing facility was purchased for use based on the new lower cut-off levels in accordance with the new fit for duty (FFD) rule being implemented by the licensee on November 6, 2023. Because the higher confirmatory cut-off levels were used at the HHS-certified testing facility, the results provided were correct. The NRC Resident Inspector has been notified." Notified R1DO (Eve) and FFD Group (email)

ENS 5682431 October 2023 10:45:00The following information was provided by the Texas Department of State Health Services via email: On October 30, 2023, the licensee reported that on October 27, 2023, they had an industrial radiography source disconnect when the drive cable broke at the connector while the crew was working at a temporary job site. The exposure device was an INC IR-100 (containing a 92.1 curie Iridium-192 source). The source was retrieved and secured in the exposure device by trained personnel. Self reading pocket dosimeters for the radiographers and retriever involved indicate there were no overexposures as a result of this event. Dosimetry badges are being sent for processing. The licensee is re-inspecting and re-servicing all of its crank and cable assemblies. An investigation into this event is ongoing. More information will be provided as it is obtained in accordance with SA-300. Texas Incident Number: 10063 Texas NMED Number: TX230049
ENS 567257 September 2023 12:40:00The following summary information was provided by the PA Bureau of Radiation Protection (PA DEP) via email On September 6, 2023 a Troxler gauge, model 3411, serial number 6829 was hit by a vehicle while on a job site. This gauge contained a 9 millicurie Cesium-137 source and a 44 millicurie Americium 241:Be source. The area was secured, and the PA DEP responded to the site. The owner/radiation safety officer (RSO) retrieved the sources with long handled pliers and secured them in the transportation box for the gauge. The area and gauge were surveyed and smears were taken for contamination. The case was also surveyed and the owner/RSO has contacted a consultant/vendor to leak test the sources and arrange for disposal. Pennsylvania Event Number: PA230024
ENS 5668520 August 2023 18:30:00The following information was provided by the licensee via email: On 8/20/2023 at 1600 EDT, during plant walkdowns in the drywell while in mode 3 to identify a cause of increasing unidentified leakage rate, reactor coolant system pressure boundary leakage (approximately 2 gpm) was identified on the reactor recirculation sample line between the reactor recirculation sample line inboard isolation valve (B3100F019) and where the sample line taps off the B reactor recirculation jet pump riser. This requires entry into technical specification 3.4.4 condition C, identification of pressure boundary leakage with a required action to be in mode 3 in 12 hours and mode 4 in 36 hours. At 1630 EDT, a technical specification required shutdown to mode 4, cold shutdown, was initiated. A press release by DTE is anticipated. This event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i), a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(xi), and an eight-hour, non-emergency notification 10 CFR 50.72(b)(3)(ii)(A) for the degraded condition of the pressure boundary. Investigation into the cause of the reactor coolant system pressure boundary leakage is still ongoing. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified.
ENS 564535 April 2023 10:25:00The following information was provided by the licensee via email: At 0651 EDT on April 5, 2023, with Unit 1 in mode 1 at 85 percent power, the reactor was manually tripped due to loss of main feedwater pump 'C'. The trip was not complex, with all systems responding normally post-trip. Main feedwater pump 'B' had previously been removed from service in preparation for a planned shutdown as a part of refueling outage RF27. Operations responded and stabilized the plant. Decay heat is being removed by the emergency feedwater system. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) resulting from valid actuation of the reactor protection and emergency feedwater systems. There was no impact on the health and safety of the public or plant personnel. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee continues to investigate the loss of main feedwater pump 'C'. The licensee notified the NRC Resident Inspector.
ENS 564545 April 2023 11:51:00

The following is a summary of information provided by the Kentucky Department of Radiation Control via email: On April 4, 2023, an authorized gauge user identified a shutter stuck open on a gauge mounted 15 feet up in the air on a coal feeder at the D.B. Wilson power plant. The shutter opened and closed; however, when the shutter was placed into a closed position some radiation exposure was still present outside the shutter. The gauge is model number 7062BP, serial number 17777, with 100 mCi Cs-137. The Radiation Safety Officer (RSO) alerted employees of the stuck shutter. The gauge will remain in place until a certified contractor can remove it. The contractor is expected to arrive on April 5, 2023.

  • * * UPDATE ON 4/6/2023 AT 1254 EDT FROM CURT PENDERGRASS TO IAN HOWARD * * *

The following information was provided by the Kentucky Department of Radiation Control via email: According to the RSO, RAM Services, Inc. was able to free up the shutter yesterday, but there were issues with elevated exposure rates so the decision was made to dispose of the device and package it for shipping. Notified R1DO (Gray) and NMSS Events Notification.

ENS 5578210 March 2022 17:22:00The following information was provided by the Florida Bureau of Radiation Control (FL BRC) via email: Today, 3/10/2022, at 1000 EST, Lutathera treatment was started in a controlled infusion room within the nuclear medicine department of Moffitt Cancer Center with an initial vial assay of 206 mCi, approximately two minutes later the NMT ((nuclear medicine technologist)) noticed a leak in the infusion line and stopped the infusion. Assistance was provided by a fellow technologist and the vial of Lutathera (Lu-177) was re-assayed at 130 mCi. The floor lead technologist notified the prescribing physician and the physician decided to terminate the treatment and to re-treat at a later date. Wipe tests performed by the technologists on the patient including the arm where the IV was showed no evidence of removable contamination. The department supervisor was notified and called the radiation safety officer (RSO) at 1030 EST. The IV was removed from the patient and the tubing was assayed at 36 mCi. The infusion room was surveyed and appropriately decontaminated. Residual waste from decontamination, as well as the vial, lead vial container, and IV/tubing were logged, labeled, and placed into secure storage. An investigation into the cause of the incident will be completed, and corrective actions will be implemented to prevent reoccurrence. The prescribing physician spoke with the patient and explained what happened and that there would not be any clinical impact on the patient and no medical risks. The referring physician was notified. A written report will be provided to the FL BRC, the referring physician, and the individual within 15 days of this event in accordance to 64E-5.345 4(b). A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 557809 March 2022 23:20:00

The following information was provided by the licensee: At 2013 EST on March 9, 2022, the HPCI System was declared inoperable following evaluation of routine HPCI surveillance testing data indicating that the required response time for reaching rated conditions was not met. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The Reactor Core Isolation Cooling (RCIC) System and Automatic Depressurization System (ADS) are operable. There was no impact on the health and safety of the public or plant personnel. Investigation is in-progress to determine the cause. Unit 1 is not affected by this event. Unit 1 is in a refueling outage. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 05/04/22 AT 1135 EDT FROM CHARLIE BROOKSHIRE TO DAN LIVERMORE * * *

The following information was provided by the licensee via email: At 20:13 EST on March 9, 2022, the HPCI System was declared inoperable following evaluation of routine HPCI surveillance testing data indicating that the required response time for reaching rated flow and pressure was not met. Subsequent to this, it was determined that the required response time was overly conservative for assuring the safety function of the system could be fulfilled. The required response time was revised. The operability determination for this event has been updated indicating that system operability was never lost for this event. There was not a condition that could have prevented the system from fulfilling the safety function. The NRC Resident Inspector has been notified. Notified R2DO (Miller).

ENS 5578110 March 2022 17:10:00The following information was provided by the Illinois Emergency Management Agency (the Agency) via email: The radiation safety officer (RSO) for Elmhurst Hospital contacted the Agency on 3/10/22 to advise of a Y-90 microsphere administration in which the patient received only 54 percent of the prescribed dose. The administration occurred on the morning of 3/9/22. The physician felt the delivered dose was clinically effective and no further treatment is planned. No adverse patient impacts are expected. The referring physician and patient were notified as required. Agency staff have requested copies of the written directive and associated documentation as details regarding the prescribed activity were not immediately available. Of note, the RSO advised that the authorized user felt resistance during administration and discontinued the procedure. Microspheres were reportedly observed `clumped' within the first two inches of the delivery catheter. A second, smaller vial was obtained and the written directive modified. No contamination or other issues were identified. The Agency will dispatch inspectors, likely at the beginning of next week, to review the procedure and determine root cause. Compliance with Agency regulations regarding modification to a written directive will be reviewed. This matter will be reported under NMED number IL220008. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 557748 March 2022 19:50:00The following information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Qaltek Associates of Idaho Falls, Idaho contracted with AGEC of St. George, Utah to repair a Troxler 3440 Moisture Density gauge. The Troxler gauge was reported by AGEC to be reading low. On August 29, 2021, Qaltek used their own company van to pick up the gauge at the AGEC location in Utah. At this time, Qaltek does not have any information regarding surveys performed on the gauge when placed in the van. Troubleshooting of the gauge has been ongoing since receipt with time spent waiting for repair parts. On March 8, 2022, Qaltek discovered the 40 millicurie Americium-241/Be source was missing. The Cesium 137 source was still in the gauge. Surveys of the facility and of the van did not show any abnormal radiation levels. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 557799 March 2022 16:26:00The following information was provided by the New Mexico Radiation Control Bureau via telephone: Two Berthold Model LB7440 density gauges installed in a mine were discovered to have shutters stuck in the open position during routine maintenance. The gauges (s/n: 1155 and s/n: DZ253A) contain a 30 millicurie and a 150 millicurie Cs-137 source, respectively, and remain mounted in place in the mine. The licensee is adding warning signage and is controlling any work in the area near the gauges. Radiation Technologies, a contracted service company, is scheduled to repair the gauges on March 21, 2022.
ENS 559741 July 2022 17:43:00The following is a synopsis of information received via facsimile: A Model 38878-8 solenoid valve failed a routine coil resistance test at Catawba Nuclear Station while installed on a feed water isolation valve actuator. The solenoid valve was returned to Flowserve where the low resistance was confirmed. The solenoid coil was then sent to the Original Equipment Manufacturer (OEM) for further evaluation. The OEM (Ohmega) completed their analysis and found the reason for failure to be associated with the magnet wire, but the exact point of failure could not be located due to the construction of the coil. Additionally, Flowserve compiled shipment data for the subject coil and found there to be at least 273 instances where the part was shipped to customers. Of those 273+, this case is the only known instance of a failure associated with the coil. Sites that Flowserve shipped the Model 38878-8 Solenoid Valve to: Comanche Peak, Catawba, Braidwood, Byron, Beaver Valley, Seabrook Due to the rigorous functional testing and the historical reliability of the coil in the field, Flowserve does not believe this incident is indicative of an issue with the manufacturing or testing of the coil and concludes that this issue does not affect other coils currently in service. Ohmega suggests a possible manufacturing improvement of winding the coil with a varnish to provide extra insulation of the magnet wire. Flowserve suggests that plant operators using these solenoid coils measure the resistance of the coil periodically, especially after the coil has been energized for testing or service.
ENS 555563 November 2021 10:46:00The following information was received from Illinois Emergency Management Agency (Agency) via E-mail: The (Illinois Emergency Management) Agency was contacted at approximately 16:00 (CDT) on 11/2/21 by Isomedix Operations, Inc. (d/b/a Steris Applied Sterizliation Technologies, RML IL-01123-02) to advise of a fire in one of their irradiation cells that occurred at approximately 05:00 (CDT) this morning in Libertyville, IL. Sources, irradiator lift mechanisms, and associated safety/security systems were reportedly unaffected. Local fire personnel did respond, but maintenance crew were able to extinguish the fire prior to their arrival. This matter is reportable under 32 Ill. Adm. Code 346.830(a)(2). The radiation safety officer for Isomedix Operations, contacted the Agency at 16:00 (CDT) today and informed of a fire in a radiation room at their pool irradiator facility. Reportedly, maintenance crews were performing overhead welding in the source room when hot slag fell on a product tote. The tote was located near the portal entry of irradiator 192. The fire alarm was pulled and the maintenance crew was able to put out the fire using a handheld extinguisher. Local fire arrived, performed an investigation and departed without further concern. The irradiator was removed from service as Isomedix staff spent the duration of the day assessing safety systems. Water purity checks and exposure rates indicate no impacts to sources. Cables, cable shrouds and associated lifting mechanisms were assessed and were not impacted. Having found no additional radiological or safety mechanisms impacted, the facility returned to routine operations at 16:00 (CDT) today. IEMA staff are pursuing additional information from the licensee and performing a reactionary inspection on 11/3/21. Additional information will be communicated as it becomes available. Illinois Report Number : IL210036
ENS 5499715 November 2020 06:11:00At 0144 EST on November 15, 2020, with Unit 1 in Mode 1 at 100 percent power and Unit 2 in Mode 5 at 0 percent power, an actuation of the Emergency Diesel Generator (EDG) system occurred while transferring the 2A-A 6.9 kV Shutdown Board (SDBD) from the maintenance feed to its normal power supply. The reason for the 2A-A 6.9 kV SDBD failing to transfer to the normal power supply is under investigation. The EDGs automatically started as designed when the valid actuation signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EDGs. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5477613 July 2020 17:10:00On July 13, 2020 at 0831 (EDT), Southern Nuclear Operating Company (SNC) determined an SNC supervisory personnel failed their fitness for duty test. The employee has been removed from the site and their access has been terminated. The NRC Resident Inspector has been notified.
ENS 545737 March 2020 13:38:00On March 7th, Kumar and Associates, Inc. (Denver) License No. CO 778-01 reported a stolen truck at gunpoint from the technician. The truck had on board a Troxler 3440 series nuclear density gauge with a standard load of not more than 333 MBq (9 mCi) of cesium-137 and 1.63 GBq (44 mCi) of americium-241: beryllium; or 2.44 MBq (66 microCi) of californium-252. The event took place in Lakewood, Colorado. The Lakewood police have been notified and they are aware that the truck has a density gauge on board. The police department is currently searching for the truck. This event is still ongoing. Colorado Report ID Number: CO200016 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 547679 July 2020 16:17:00The following is a summary of information received from Piezotech, LLC: Piezotech possessed and used source material, in the form of depleted uranium, without applying for and receiving a specific license in accordance with 10 CFR 40.31. The depleted uranium was used to manufacture piezoelectric ceramics which contained an "Unimportant Quantity" of depleted uranium as defined in 10 CFR 40.13(c)(2)(ii). Piezotech transferred the piezoelectric ceramics to several customers without first applying for and receiving a license for initial transfer of items containing source material in accordance with 10 CFR 40.52 and did not file initial transfer reports as required by 10 CFR 40.53. Piezotech suspects that a formulation to manufacture piezoceramics, named K180, was developed in the 1970s or 1980s. K180 uses depleted uranium as one of the doping materials in the manufacture of piezoceramics. The formulation uses an amount of depleted uranium that is less than 1 percent by weight. In January of 2020, an engineer raised a concern to Piezotech's General Manager and to its Compliance Director that the company may need an NRC license to use depleted uranium in making the K180 piezoceramic. A review of NRC regulations showed that this was the case and at that time all activity regarding K180 was halted. All material used in K180 manufacturing and all existing inventory and intermediate stage materials were segregated from manufacturing and the container of depleted uranium was secured in a locked cabinet where it currently remains. In February 2020, Piezotech commissioned a radiation survey of the facility and sampling occurred in all areas where K180 and its component materials were stored or processed. This survey indicated that all processing areas were at background radiation levels and all areas where the depleted uranium and K180 ceramics had been stored were below the annual exposure levels for untrained personnel. Piezotech has decided to discontinue manufacturing the K180 material. The depleted uranium will remain sealed in the original container and shipping crate, having all the original markings and labels and secured in a locked flameproof cabinet. Piezotech is making arrangements with an appropriately licensed facility for the proper disposal of the remaining depleted uranium and intermediate stage and finished K180 product. If in the future Piezotech decides to resume manufacturing the K180 material or any material using NRC regulated substances, Piezotech will apply for the required licenses and will not initiate any regulated manufacturing or sales activities until all applicable licenses have bee issued. For further information, contact: John Churchill Piezotech Compliance Director Phone: (301) 216-3002 FAX: (301) 330-8873
ENS 543662 November 2019 23:03:00At 1515 on November 2, 2019, the Refueling Water Storage Tank (RWST) was declared inoperable due to a Low Head Safety Injection relief valve discharging to the Safeguards Sump during routine surveillance testing. The leakage from the Low Head Safety Injection system in conjunction with a postulated Design Basis Accident (DBA) Loss of Coolant Accident (LOCA) with transfer to Safety Injection Recirculation may result in dose exceeding the Dose Analysis of the Exclusion Area Boundary (EAB) and the Control Room, which is common to both Unit 1 and Unit 2. This condition may not be bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. The Low Head Safety Injection relief valve has been isolated to prevent further leakage, and makeup to the RWST completed. At 1602 on November 2, 2019 the RWST was declared Operable. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(B), (C), (D) as an Unanalyzed Condition and a condition that could have prevented the Fulfillment of a Safety Function." The licensee notified the NRC resident inspector.
ENS 543683 November 2019 00:00:00

The following was received from the Mississippi Division of Radiological Health via phone: A radiographer was exposed to a 100 Curie Ir-192 source for 8 minutes while changing film during a radiography shot. The radiographer was not wearing dosimetry and did not have a hand held radiation meter. While changing film, the radiographer realized the source had not been retracted and left the area. This was not an equipment malfunction, and the source was retracted when it was realized that the radiographer had been exposed. The radiographer reported the event to the Mistras Radiation Safety Officer (RSO). Estimated dose is 20 Rem to the hands and 19.6 to 19.7 Rem whole body. The radiographer was sent to a local hospital for bloodwork.

  • * * UPDATE FROM ROBERT SIMS TO HOWIE CROUCH VIA EMAIL AT 1706 EST ON 11/8/19 * * *

(A state of Mississippi Health Physicist investigator) interviewed the RSO on 11/7/2019 and investigated the incident. After reviewing and questioning the incident details, (the investigator) found the following evidence that may determine this may not have been an overexposure. The assistant radiographer retracted the source, but did not perform the bump test to fully retract the source into the locked position. This caused the assistant radiographer to believe the source was still in the collimator. When returning to change the film, he saw the red button on the camera instead of green which would indicate the source was in the locked position. The assistant was not using dosimetry, rate alarm or survey instrumentation. He appears to have panicked, came down the ladder, and couldn't get the crank to move in. The lead radiographer then grabbed the crank and cranked out and back in immediately to fully retract the source into the camera. (The investigator) reviewed compliant leak tests of camera and wipes along with maintenance and service reports before and after the incident and the RSO could not replicate any problems that would prevent them from retracting the source. There was no malfunction with the camera or the cranks. It appears that the source was in the end of the camera but not in the fully shielded position, which could allow some radiation out of the tube that the source enters. However, we do not know how much because the assistant was not wearing any dosimetry. The other assistant's dosimetry (assistant radiographer 2) only picked up 1 milliRem of dose but he was approximately 25 ft. away with steel shielding from the tank they were working on in between him and the source. (The investigator is) waiting on the emergency reading of the doses recorded on the OSL badges used by the crew and follow up doctor's visit. (The investigator) interviewed (the assistant radiographer on) 11/8/2019 at 1549 CST. (The assistant radiographer) reports that he had more blood drawn today and will provide results next week. He said he feels great and has had no sickness such as nausea, pain or redness and swelling in the hands. Will update again next week after receiving lab results.

  • * * UPDATE FROM ROBERT SIMS TO THOMAS KENDZIA VIA EMAIL AT 1409 EST ON 11/19/19 * * *

(A state of Mississippi Health Physicist investigator) interviewed the assistant radiographer (who was not wearing dosimetry) on 11/12/2019. (The assistant radiographer) reported that lab was drawn on 11/3/2019 and 11/8/2019. Both labs results returned within normal limits and (the assistant radiographer) has no physical symptoms of radiation sickness. (The assistant radiographer) remains at regular work duties recommended in his physician reports that he provided to (the investigator). (The RSO) was interviewed on 11/11/2019 and provided the Landauer dosimetry report for the three RT crew members. The crew received new dosimeters on 11/1/2019 and they were sent for an emergency read the day after the incident. (The) lead radiographer received 109 milliRem, (assistant radiographer 2 who was wearing dosimetry) received 269 milliRem and (the assistant radiographer) received 150 milliRem although he was not wearing his dosimeter during this incident. (The assistant radiographer) is also on UT and other duties until the end of the year until his new annual dose limit year starts January 1, 2020. This is upon the recommendation of (the investigator) because although it has been determined that (the assistant radiographer) did not receive an over exposure equaling or exceeding the 15 to 25 RAD to cause radiation sickness, it does not rule out if he did or did not exceed his 5 rem TEDE. The licensee's personnel believe that the source was in the end of the camera, but not in the fully locked position because the red button was showing on the QSA 880 camera when (the assistant radiographer) returned from changing the digital film plate. Due to his elevation up on the tank and the tank shielding we cannot use any of the other crew members dosimetry to make any determinations. However based on the medical reports and physical evidence it appears that (the assistant radiographer) has no physical symptoms from radiation sickness. (The assistant radiographer) will have his last lab test on 11/22/2019, if it is normal, (the assistant radiographer) states that the physician intends to release him completely from all medical care related to this incident. Notified the R4DO (O'Keefe) and NMSS Events Notification via email.

  • * * UPDATE AT 1333 ON 12/5/2019 FROM ROBERT SIMS TO JEFF HERRERA * * *

As the investigation continued (a state of Mississippi Health Investigator) reviewed additional information received throughout the day on 11/18/2019, but sufficient time did not exist to thoroughly review the latest findings to include them on the 11/19/2019 update. The current additional findings are as follows: (the state of Mississippi Health Physicist Investigator) Re interviewed all personnel again, and requested all lab results and Physician findings from (the assistant radiographer). (The assistant radiographer) willingly provided all CBC and cytogenetic lab test results that were taken on 11/3/2019, 11/8/2019, and 11/22/2019. (The assistant radiographer) stated that the physician reported the lab results to be within normal limits and the physician released (the assistant radiographer) from medical care on 11/22/2019 that had resulted from this incident. (The state of Mississippi Health Physicist Investigator) also found during the second interview of personnel that the films that were with (the assistant radiographer) and located on the pipe during the 8 minutes that it took (the assistant radiographer) to change out the film were processed later and were acceptable images. (The state of Mississippi Health Physicist Investigator) attached the images in the file as evidence to support that (the assistant radiographer) was not overexposed. If the films had been exposed with an open source out for 8 minutes they would be blacked out from overexposure. The original exposure time to produce the radiograph with the film combination, distance and thickness of steel for this job was 1 minute. Even with digital radiography, an image receptor plate can be overexposed beyond acceptable exposure limits, and cannot be window leveled to make it an acceptable image, but this was not the case. The radiographer and RSO reported that an attempt to crank out and retract the source was made by each assistant and the radiographer when trying to retract the source after (the assistant radiographer) returned down the ladder. This would explain why the images produced were acceptable radiographs. There had been enough exposure to properly expose the film but not overexpose it. This appears to support the possibility that the source was not out the entire 8 minutes while (the assistant radiographer) was changing the film and moving the source tube on the jig. At this point (the assistant radiographer) was also down the ladder 25 feet away with the other radiographers who were wearing the required dosimetry behind the shielding of the tank. Three (3) violations were issued and corrective actions have been submitted to the Mississippi Division of Radiological Health All records are included in the 2019 Incident file at the Mississippi State Department of Health Division of Radiological Health. (The state of Mississippi Health Physicist Investigator) considers this investigation and incident closed. If you require any further information, documentation or have questions, please contact (The state of Mississippi Health Physicist Investigator). Mississippi Incident No.: MS-190005, NMED #190535 Notified the R4DO (Taylor) and NMSS (via email).

  • * * RETRACTION ON 12/6/19 AT 1452 FROM ROBERT SIMS TO CATY NOLAN * * *

A review of the incident details represented a 'substantial potential for an exposure in excess of 10 CFR 20.' However, there was not enough evidence to definitively prove there was an overexposure due to the details listed throughout this investigation. These included the assistant who was allegedly overexposed. This individual never experienced any signs of radiation sickness or erythema or redness to the hands throughout the investigation period to its close date on 12/3/2019. None of the other crew members' dosimeter readings exceeded occupational dose limits. On 12/2/2019, Mistras also requested anonymity for the individuals involved in this incident. All documentation concerning this incident investigation is stored in Mississippi State Department of Radiological Health 2019 Incident File, under incident Report No. MS-190005. NMED #190535 Notified the R4DO (Taylor) and NMSS (via email).

ENS 5409126 May 2019 09:25:00This is a 4-hour Non-Emergency 10 CFR 50.72(b)(2)(iv)(B) notification due to a Plant Protection System (PPS) actuation. Arkansas Nuclear One, Unit 2, automatically tripped from 100 percent power at 0512 CDT. The reactor automatically tripped due to 2P-32B Reactor Coolant Pump tripping as a result of grounding. No additional equipment issues were noted. All control rods fully inserted. Emergency Feedwater (EFW) actuated and was utilized to maintain Steam Generator (SG) levels. The EFW actuation meets the 8-hour Non-Emergency Immediate Notification Criteria of 10 CFR 50.72(b)(3)(iv)(A). No Primary safety valves lifted. Main Steam Safety Valves (MSSVs) did lift initially after the trip. The NRC Resident Inspector has been notified. Decay heat is being removed via the steam dump valves to the main condenser. Unit 2 is in a normal shutdown electrical lineup. Unit 1 was not affected by the transient on Unit 2. The licensee notified the State of Arkansas.
ENS 5408925 May 2019 00:30:00A licensed employee was determined to be under the influence of alcohol during a random (fitness-for-duty) test. The employee's access to the plant has been canceled. The licensee notified the NRC Resident Inspector.
ENS 5375225 November 2018 02:47:00

EN Revision Text: LOSS OF CONTROL ROOM ENVELOPE DUE TO DOOR FAILURE On 11/24/18 at 2015 EST, a loss of Control Room Envelope (CRE) was declared due to failure of the control room boundary door, 204-36-008. (Abnormal Operating Procedure 8588A Mitigating Actions for Control Boundary Breach was implemented). The door was repaired at 2030 EST, restoring CRE to operable (status). A mechanical failure of the control room door latch prevented the door from closing. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 01/18/19 AT 1457 EST FROM GARY CLOSIUS TO JEFFREY WHITED * * *

The purpose of this call is to retract a report made on November 25, 2018, NRC Event Number EN53752. NRC Event Report number EN53752 describes a condition at Millstone Power Station Unit 2 (MPS2) in which a control room envelope boundary door was discovered to not be able to fully close due to the latching mechanism being stuck in the extended position. The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) via an 8-hour prompt report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. Upon further review, MPS2 determined that there was no loss of safety function. An engineering evaluation determined that even with the control room boundary door unable to be fully closed due to the latching mechanism being stuck in the extended position, control room air in-leakage would not have been sufficient to prevent the control room emergency ventilation system from performing its safety function. Therefore, this condition is not reportable and NRC Event Number EN53752 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified the R1DO (Carfang).

ENS 5375022 November 2018 03:56:00

EN Revision Text: HPCI UNEXPECTEDLY TRANSFERRED TO ALTERNATE SUCTION SOURCE DURING TESTING At 2125 (CST) on 11/21/2018, it was discovered that U1 High Pressure Coolant Injection System (HPCI) was inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, HPCI automatically transferred from its normal suction source to the alternate suction source. The control room operator then manually tripped the HPCI turbine. HPCI was already inoperable in accordance with Technical Specifications (TS) Limiting Condition for Operability (LCO) 3.5.1, ECCS Operating, Condition C during performance of the surveillance. However, this condition was not expected nor induced by the testing. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. CR 1469109 documents this condition in the Corrective Action Program.

  • * * RETRACTION ON 12/28/18 AT 1300 EST FROM MARK MOEBES TO JEFFREY WHITED * * *

ENS Event Number 53750, made on November 22, 2018, is being retracted. NRC notification 53750 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72(b)(3)(v)(D) were met when the licensee discovered an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, the High Pressure Coolant Injection (HPCI) System automatically transferred from its normal suction source to the alternate suction source. As a result, Unit 1 HPCI was declared inoperable. On December 20, 2018, a Past Operability Evaluation was completed which determined that the HPCI System remained operable. The evaluation determined that the HPCI System could have performed its specified safety function of vessel injection throughout the time that the suction path was aligned to the torus. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the Corrective Action Program in Condition Report 1469109. The licensee has notified the NRC Resident Inspector. Notified R2DO (Desai).

ENS 533938 May 2018 10:38:00On May 8, 2018 at 0139 Central Daylight Time, Farley Nuclear Plant Unit 1 declared containment inoperable due to total containment leak rate greater than technical specifications. The 1B containment cooler had seat leakage of approximately 30 gallons per minute from a service water drain valve. Though the containment cooler service water supply is not tested per the Appendix J program, a loss of the containment barrier is possible under accident conditions. The service water flow path to the 1B containment cooler has been isolated to exit the condition. The licensee will notify the NRC resident inspector.
ENS 533887 May 2018 16:31:00On May 7, 2018, during an engineering review of mission time requirements for Technical Specification related equipment, a deficiency was discovered regarding the Emergency Operating Procedure (EOP) guidance for natural circulation cooldown with a stagnant loop. This condition could be the result of a postulated Main Steam Line Break with a loss of offsite power. During a natural circulation cooldown with a faulted steam generator, flow in the stagnant reactor coolant system (RCS) loop associated with the isolated faulted steam generator (SG) could stagnate and result in elevated temperatures in that loop. This becomes an issue when RCS depressurization to residual heat removal system (RHR) entry conditions is attempted. The liquid in the stagnant loop will flash to steam and prevent RCS depressurization. In this condition, the time required to complete the cooldown would be sufficiently long that the nitrogen accumulators associated with Callaway's atmospheric steam dumps and turbine driven auxiliary feedwater pump flow control valves would be exhausted. The atmospheric steam dumps and turbine driven auxiliary feedwater pump would not be capable of performing their specified safety functions of cooling the plant to entry conditions for RHR operation. This issue has been analyzed by Westinghouse in WCAP-16632-P. This WCAP determined that to prevent loop stagnation, the RCS cooldown rate in these conditions should be limited to a rate dependent on the temperature differential present in the active loops. The WCAP analysis was used to support a revision to the generic Emergency Response Guideline (ERG) for ES-0.2 "Natural Circulation Cooldown." Figure 1 in ES-0.2 provides a curve of the maximum allowable cooldown rate as a function of active loop temperature differential which is directly proportional to the level of core decay heat. At the time of discovery of this condition, Callaway's EOP structure did not ensure that the ES-0.2 guidance would be implemented for a natural circulation cooldown with a stagnant loop. Callaway has issued interim guidance to the on-shift personnel regarding this concern and is in the process of revising the applicable EOPs. This condition is reportable per 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shutdown the reactor and maintain it in a safe shutdown condition, (B) Remove residual heat, or (D) mitigate the consequences of an accident." The licensee notified the NRC Resident Inspector of this condition.
ENS 5323027 February 2018 01:15:00At 2247 Eastern (Standard) Time the Unit 1 Control Room was notified of a personnel injury in the Unit 1 lower containment. Unit 1 is currently in Mode 1 at 100 (percent) (Reactor) Power and the individual was working in lower containment. The individual's injury appears to be Heat Exhaustion. Site emergency medical technicians responded to the scene and the individual was transported to a local medical facility via ambulance. At the time of transport, the individual was considered to be potentially contaminated because complete surveys could not be performed while the individual was immobilized for transfer. The individual and clothing were surveyed at the hospital by a resident Radiation Protection Technician and no contamination was found. This report is being made pursuant to 10 CFR 50.72(b)(3)(xii), 'Any event requiring the transport of a radioactively contaminated person to an offsite medical facility for treatment.' The NRC Resident Inspector has been notified.
ENS 5322925 February 2018 11:24:00A non-licensed employee was found in violation of the sites Fitness for Duty Policy. The employee's access authorization to the plant has been terminated. The NRC Resident Inspector has been notified.
ENS 5309025 November 2017 06:02:00

At 0238 (CST) a manual reactor scram was inserted by placing the Reactor Mode Switch in Shutdown. At 0149 (CST), with reactor power just above the point of adding heat, IRM (Intermediate Range Monitor) channels A, C, and D received a spurious upscale trip signal which immediately cleared. Upon investigation, operability of RPS (Reactor Protection System) scram function for Intermediate Range Detectors was placed in question. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON NOVEMBER 26, 2017, AT 1850 FROM GRAND GULF TO MICHAEL BLOODGOOD * * *

At 0238 (CST) a manual reactor scram was inserted by placing the Reactor Mode Switch in Shutdown. At 0149 (CST), with reactor power just above the point of adding heat, Intermediate Range Monitor neutron flux detector (IRM) channels A, C, and D received a spurious Upscale Trip signal which immediately cleared. Upon investigation, IRM channels A, C, and D were declared Inoperable. IRM G was already Inoperable for another reason. RPS scram function from IRM channels B, E, F, and H was always Operable and available. That event is being reported under 10CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical. This Revised Statement to Event Notification # 53090 is being made to make it clear that only four IRM channels (A, C, D, G) were Inoperable and that the IRM RPS SCRAM function was still available from the four remaining Operable IRM channels (B, E, F, and H). The licensee notified the NRC Resident Inspector. Notified R4DO (O'Keefe)

  • * * RETRACTION ON 01/16/2018 AT 1629 EST FROM JASON COMFORT TO DAVID AIRD * * *

On 11/25/17, at 0149 (CST), with reactor power just above the point of adding heat, Intermediate Range Monitor neutron flux detector (IRM) channels A, C, and D received a spurious Upscale Trip signal which immediately cleared. Upon investigation, IRM channels A, C, and D were declared Inoperable. IRM G was already Inoperable for another reason. At 0238 (CST) a manual reactor scram was inserted by placing the Reactor Mode Switch in Shutdown. RPS scram function from IRM channels B, E, F, and H was always Operable and available. That event was initially being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical. After the trip alarms were received, the Operators spent approximately twenty minutes investigating possible causes and implications, and consulted with Reactor Engineering and the Shift Technical Advisor. The investigation showed that the plant was stable and the upscale IRM alarms were spurious. A review of plant technical specifications by the operators determined that a plant shutdown was not required. After further discussions, Operations concluded that a shutdown to allow further investigation of the issue was the prudent course of action. Prior to shutting down, Operations spent approximately twenty minutes reviewing procedures, notifying personnel to exit containment, and conducting a brief. The shutdown was then conducted by inserting a manual reactor scram by placing the reactor mode switch in SHUTDOWN. This was initially reported under 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the RPS. Based on the sequence of events, and Operator actions in conducting the shutdown, the event is considered 'part of a pre-planned sequence during testing or reactor operation' as specified in 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.73(a)(2)(iv)(A). In accordance with NUREG-1022, Section 3.2.6, the event is not reportable as an actuation of RPS. The licensee notified the NRC Resident Inspector. Notified R4DO (Taylor).

ENS 5308923 November 2017 02:54:00

On November 22, 2017, at 2043 (CST), Unit I MCC (Motor Control Center) 18/19-5 overvoltage relay target was found actuated and would not reset. MCC 18/19-5 was powered from the normal feed, Bus 19. Bus 19 voltages were verified to be normal. The overvoltage relay actuation would result in MCC 18/19-5 being de-energized in the event of a DBA LOCA (Design Basis Accident Loss of Coolant Accident) in which the 1/2 Emergency Diesel Generator fails to energize Bus 18, therefore rendering both divisions of the Low Pressure Cooling Injection (LPCI) mode of Residual Heat Removal (RHR) system inoperable. Technical Specification 3.5.1 Condition E was entered, requiring restoration of LPCI in 72 hours. The overvoltage target was subsequently able to be reset at 2114 (CST), restoring the LPCI function of RHR. Technical Specification 3.5.1 Condition E was exited at that time. This event is reportable under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM RONALD SNOOK TO STEVEN VITTO ON 01/11/18 AT 1913 EST * * *

The purpose of this notification today (01/11/18) is to retract the ENS Report made on November 23, 2017 at 0248 hours EST (ENS Report #53089). Upon further review, it was determined that the Unit 1 MCC 18/19-5 overvoltage relay target that was found actuated and would initially not reset was caused only by intermittent degraded DC control power. During this event, MCC 18/19-5 remained powered from the normal feed Bus 19, and Bus 19 voltages were verified to be normal. It was further determined from plant drawings that under this condition the degraded DC control power to the Unit 1 MCC 18/19-5 overvoltage relay has no impact to the Technical Specification 3.5.1 required capability to auto transfer power from the normal Bus 19 to the alternate Bus 18 should Bus 19 lose power such as during a DBA LOCA. This overvoltage relay was installed in the early 1990's only to support enhanced reliability of the power supply to the LPCI injection valves, and its actuation due to degraded DC control power would not impact the ability to auto transfer to alternate Bus 18. Therefore, both divisions of the Low Pressure Cooling Injection (LPCI) mode of Residual Heat Removal (RHR) system would have remained fully operable under the as-found relay condition, and Technical Specification 3.5.1 Condition E was not required to be entered. On December 6, 2017, it was determined that a loose fuse clip terminal had caused the DC control power to the overvoltage relay to become degraded which in turn caused the relay target and its reset to become erratic. This fuse clip terminal was repaired on December 6, 2017. Based on the subsequent reviews of this event, the LPCI system was not required to be declared inoperable in accordance with Technical Specifications 3.5.1 during the period of the MCC 18/19-5 overvoltage relay actuation (i.e., 31 minutes on 11/22/17), and hence was not required to be reported under 10CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. Therefore, based on this information, ENS Report #53089 is being retracted. The NRC Resident Inspector has been notified. R3DO(Jeffers) has been notified.

ENS 5301514 October 2017 16:37:00At approximately 19:48 Mountain Standard Time on October 13, 2017, Palo Verde Nuclear Generating Station (PVNGS) staff confirmed a non-licensed supervisor tested positive for drugs during a random 'Fitness for Duty' test. The person's access authorization was terminated in accordance with station procedures. The NRC resident inspector has been notified by the licensee.
ENS 5300811 October 2017 11:16:00The following report was received from the Texas Department of State Health Service via email: On October 10, 2017, the Agency had an alarm system breach at 1135 CDT. Security called our program stating the alarm to the source room was alarming. I went down to the room to check it out. I checked the door and it was locked, turned off the alarm system by entering the code, and called the security company and provided information to stop law enforcement from responding to the location. The postal service technician was next door and I asked her who opened the door, she said the contractors asked her to open the door and she stated she went to building operations office and got the key and opened the door for the contractors. And she said when the alarm went off, the door was closed and security guard was informed. That is when our program received the call to go down there. An investigator from our program stayed with the contractors and set the alarm when they were finished. A complete investigation will be completed. Investigation ongoing. Update will be provided in accordance with SA300. Texas Incident#: I-9516
ENS 5297719 September 2017 13:16:00

The following information was received via fax: On September 19, 2017, the (Alabama Department of Public Health) received a phone call from Schlumberger, stating that they had failed to notify the Agency (Alabama Department of Public Health) upon entering the State, to perform a job on September 13, 2017, and that two sources (Cf-252 - 18.3 mCi and Cs-137 - 1.78 Ci) are stuck down hole. Schlumberger stated that the first fishing attempt had failed to recover the sources, and the second attempt is now underway. Gathering information is continuing. Alabama Incident: #17-26

  • * * UPDATE FROM MYRON RILEY TO VINCE KLCO AT 1148 EDT ON 9/26/2017 Via Fax * * *

On September 24, 2017, after several days of fishing for the logging tools, all recovery attempts had been unsuccessful and the sources were cemented in place down hole. The licensee will follow up with a written report and a picture of the plaque to be placed on the well head. Notified R1DO (Bower) and NMSS Events Notification via email. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf Note: This device is assigned an IAEA Category 3 value based on the actual radioactivity of the source, not on the device type. (Reference IAEA RG-G-1.9)

ENS 5297819 September 2017 16:54:00

The following information was received from the State of Florida via email: (The State of Florida Bureau of Radiation Control) received a call from (the licensee) RSO to report a stolen Troxler gauge. An employee from GFA International had the gauge stolen from the back of his truck while at a convenience store. Awaiting the police report for more information. The stolen gauge is a Troxler Moisture Density Model 3430, S/N 29415, containing two sources; 8 mCi Cs-137 and 40 mCi Am241/Be.

  • * * UPDATE ON 9/20/17 AT 1215 EDT FROM TIM DUNN TO DONG PARK * * *

The following information was received from the State of Florida via email: (The State of Florida Bureau of Radiation Control) received a call from (the licensee RSO) to report that the gauge has been found. A contractor onsite found the gauge on 9/19 and secured it until (the licensee RSO) could be located and took possession of the gauge on 9/20. The case has a small crack, but all radiation readings are normal. Incident Number: FL17-256 Notified R1DO (Kennedy) and NMSS Events Notification via email. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5297518 September 2017 20:08:00The following is a report emailed from the California Department of Public Health, Radiologic Health Branch (RHB): On 09/18/17, RHB received a call from an employee at an unlicensed facility (Clorox Company) in Fairfield, CA, regarding recovery of a lost/stolen moisture density gauge. The gauge is a Troxler Model 3450, S/N 1083 gauge containing approximately 9 mCi of Cs-137 and 44 mCi of Am-241. On Sunday afternoon (09/17/17) one of the Clorox employees noticed a locked container left on the side of the street in front of their facility. On Monday (9/18/17) morning, the locked container was noticed to have been moved farther from the road and closer to their facility. Clorox called Troxler and Fairfield Police, but neither could pick up the container. The Clorox employee then contacted RHB, and received instruction on how to safely store the container until RHB arrives at the facility. RHB picked up the gauge the same day and brought it back to the storage facility at the Richmond Regional office. A survey performed by RHB at the Clorox facility using a Thermo Scientific Rad Eye B20, S/N 30744, calibrated 03/09/17, indicated 0.4 mR/hr at one meter, which is a typical reading for a moisture density gauge in its transportation container. The type A transportation container appeared to be in good condition and was locked with two padlocks. RHB had the padlocks cut, and located a copy of a license indicating the gauge belongs to RMA Group in Rancho Cordova, CA (License # 7565-34). RHB has not received any notification from the licensee regarding a lost or stolen gauge. RHB will be contacting the licensee to follow up on this incident. California 5010 Number: 091817 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5286520 July 2017 13:30:00In order to address the concerns outlined in RIS 2015-06 'TORNADO MISSILE PROTECTION,' an evaluation of tornado missile vulnerabilities and their potential impact on Technical Specification (TS) plant equipment was conducted. This evaluation concluded that the following Structures, Systems, and Components (SSCs) are potentially vulnerable to tornado generated missiles: The Davis-Besse Nuclear Power Station (DBNPS) Unit 1 Emergency Diesel Generator (EDG) Fuel Oil Storage Tanks (FOST) (DB-Tl53-l, DB-T-153-2) support the EDG operation for 7 days. The vents on the FOST are necessary to support the transfer of fuel from the FOST to the EDG day tank. These vents are not protected and are vulnerable to a potential tornado-generated missile impact. This postulated strike could impact fuel transfer to the EDG day tank and, therefore does not support operability of both EDGs for Technical Specification 3.8.1. Tornado generated missiles striking the FOST vent piping could potentially affect pump performance and challenge the structural integrity of the tank. This would render both the FOST and corresponding EDG inoperable. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(A). The potential vulnerabilities for the FOST vents (as discussed above) are being addressed in accordance with NRC EGM-15-002 Revision 1 and DSS-ISG-2016-01 NRC enforcement discretion and interim guidance documents. Immediate compensatory measures were taken to mitigate the potential consequences of an onsite tornado generated missile impact on the FOST vents. The licensee notified the NRC Resident Inspector.
ENS 5286620 July 2017 15:40:00At 1730 on 19 July 2017, HM-15 aircraft 13 had the Main Rotor Fairing, commonly referred to as the 'beanie', depart in flight. The 'beanie' cover is constructed of fiberglass, is circular in shape and 5 feet in diameter, weighing approximately 20 pounds. In addition to the beanie, we discovered that one of the In-flight Blade Inspection System (IBIS) Indicators also departed the aircraft. Loss of this IBIS Indicator is of concern because it contains strontium-90 which is radioactive material. Loss of this IBIS Indicator was not discovered until the aircraft shutdown on its line at Naval Station Norfolk. Location lost: Approximately 100 miles west of Norfolk, VA over the Roanoke River near Lake Gaston. The location is just north of the Virginia / North Carolina border over the Roanoke River approximately 3 miles east of the Kerr Lake Power Plant. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5262420 March 2017 04:40:00On March 20, 2017 at 0227, Nine Mile Point Unit1 was manually scrammed due to pressure oscillations. The Unit was offline and reactor shutdown was in-progress at the time of the scram. The scram was inserted at approximately 4% reactor power when pressure oscillations occurred exceeding the procedurally required limit for pressure oscillations. The cause of the scram was due to Operators manually inserting the scram. The cause of the pressure oscillations is being investigated. The licensee notified the NRC Resident Inspector. Notified the R1DO (Gray).
ENS 5262822 March 2017 08:10:00

A PET scan was administered to a patient even though a CT scan was ordered by the prescribing physician. Initially the prescribing physician ordered a PET scan, but changed the order to a CT scan. An administrative error resulted in the order change not being implemented to reflect the change to a CT scan. The patient was provided all release forms for the PET scan and was aware that a PET scan was being administered. The patient received 1R of exposure. There was no harm to the patient.

  • * * RETRACTION AT 1429 EDT ON 3/22/17 FROM BRYAN HARRIS TO DONG PARK * * *

The licensee has determined that this event did not meet reporting requirements. The licensee notified Region 3 (Craffey). Notified R3DO (Orlikowski) and NMSS Events Resource via email. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

ENS 520738 July 2016 08:48:00Oil reported in the vicinity of the station's circulating water system effluent after the start of 3rd circulating water pump. The source of the oil is believed to be from oil entrained in the discharge canal from oil leak previously reported in EN#52045. One circulating water pump was removed from service to mitigate the source. The United States Coast Guard Response Center, and the New York State Department of Environmental Conservation have been notified. James A. Fitzpatrick Control Room was notified of the issue at 0645, off site agencies were first notified at 0743. The licensee notified the NRC Resident Inspector. Notified DOE, EPA, USDA, HHS, and FEMA.
ENS 5193216 May 2016 02:02:00

At 0300 EDT on May 16, 2016, Seabrook Station's seismic monitoring instrumentation will be removed from service for a planned upgrade to the Seismic Monitoring Control Panel and its accelerometers. Modifications are expected to be complete on May 27, 2016. Proceduralized compensatory measures are in place and have been communicated to applicable emergency response decision makers. This preplanned action is being reported in accordance with 10 CFR 50.72(b)(xiii). The NRC Resident Inspector has been notified.

  • * * UPDATE ON 5/26/16 AT 2049 EDT FROM MIKE TAYLOR TO HOWIE CROUCH * * *

At 2045 EDT on 5/26/16, the seismic monitoring system was returned to service. The licensee notified the NRC Resident Inspector. Notified R1DO (Lilliendahl).

ENS 5150629 October 2015 10:38:00At 0348 CDT, while Point Beach Unit 2 was performing outage activities, it experienced a Main Power Transformer lockout and associated loss of busses (2A-01, 2A-02, 2B-01 and 2B-02). The loss of the two non-vital 4160 V buses resulted in actuation of the Unit 2 undervoltage logic which resulted in actuation of the Auxiliary Feedwater System. The Auxiliary Feedwater System functioned normally upon actuation. This condition was determined to be reportable per 10CFR50.72(b)(3)(iv)(A)(6), PWR auxiliary or emergency feedwater system actuation. This event did not affect the operating Unit 1. The NRC Senior Resident Inspector has been notified.
ENS 5134526 August 2015 09:45:00At 05:48 (EDT) BVPS (Beaver Valley Power Station) received notification that siren #6, Potter Township Municipal Building, was sounding intermittently. The fire department activation cable to the siren was severed by a motor vehicle. The ENS activation function remains functional. This event is reportable as a 4-hour Non-Emergency Notification 10 CFR 50.72(b)(2)(xi) as 'a News Release or Notification of Other Government Agency.' The Resident Inspector has been notified.
ENS 511378 June 2015 00:45:00

At 2359 EDT on June 7, 2015, the Grand Gulf Nuclear Station declared a Notice of Unusual Event in accordance with Emergency Action Level HU4 for a fire in the protected area lasting greater than 15 minutes. The fire started in the wiring of a terminal box for Electro Hydraulic Pump C, the running pump located in the turbine building. The running pump was then deenergized by operators and the standby pump started. The site fire brigade responded and extinguished the fire. The emergency was terminated at 0030 on June 8, 2015. The licensee notified state and local agencies and will inform the NRC Resident Inspector. Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, and FEMA NWC and Nuclear SSA via email.

  • * * RETRACTION AT 1645 ON 7/9/2015 FROM KEITH HUFF TO MARK ABRAMOVITZ * * *

The notification of an Unusual Event is being retracted because the event did not meet the definition of 'fire' in NEI 99-01 Revision 5, 'Methodology of the Development of Emergency Action Levels'. The document was endorsed by the NRC on February 22, 2008 (see ADAMS ascension # ML080450149) and is part of the Grand Gulf Nuclear Station's current licensing basis. Per the guidance, a 'fire' is defined as: 'Combustion characterized by heat and light. Sources of smoke such as slipping drive belts or overheated electrical equipment do not constitute as 'fires'. Observation of flame is preferred but is NOT required if large quantities of smoke and heat are observed.' According to eyewitness reports from personnel, flames were not observed at any time and evidence of large quantities of heat and smoke were not observed. Additionally, the definition of 'fire' specifically excludes overheated electrical equipment. This information leads to the conclusion that the event did not meet the definition of a 'fire' per NEI 99-01 Revision 5. Therefore, the event is not an immediately reportable Unusual Event under 10 CFR 50.72(a)(1)(i). The licensee notified the NRC Resident Inspector and will notify the state and local governments. Notified the R4DO (Haire) and NRR EO (Morris via e-mail).

ENS 511357 June 2015 05:46:00

An individual approached the protected area and grabbed the fence. Local law enforcement assistance has been requested. The Security Team leader does not consider this to be hostile. An emergency declaration was made based on HU4.1, for a security condition that does not involve a hostile action. The licensee notified state and local agencies and informed the NRC Resident Inspector. Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, and FEMA NWC and NuclearSSA via email.

  • * * UPDATE STEVE WILSON TO DAN LIVERMORE AT 0649 ON 06/07/2015 * * *

The individual was taken into custody without incident. Notified R2DO (Rose), NRR EO (Morris), and IRD (GOTT). Notified DHS SWO, FEMA OPS Center, DHS NICC Watch Officer, and Nuclear SSA via email.

  • * * UPDATE AT 1616 EDT ON 6/8/2015 FROM MICHAEL MOORE TO MARK ABRAMOVITZ * * *

Update to correct description of where the individual was apprehended.

An individual approached the outside of the administrative fence near the circulating water intake structure. Local law enforcement assistance was requested. The Security Team Leader does not consider this to be hostile.

This declaration was made based on HU 4.1, a security condition that does not involve Hostile Action.

The NRC Resident Inspector has been notified. Notified the R2DO (Rose).

ENS 5099921 April 2015 12:06:00Clinton Power Station (CPS) has completed a review of the station seismic monitor performance. The CPS seismic monitor laptop is currently operable; however, this review identified 3 times in the last 3 years that the seismic monitoring laptop was declared non-functional such that the capability to perform an EAL assessment in accordance with the Radiological Emergency Plan Annex would be adversely impacted. A loss of the seismic laptop computer prevents active seismic data from processing through the central recording unit and will not alarm in the main control room. The seismic monitor laptop became non-functional and unresponsive on the following dates: 1) January 4, 2013 2) July 19, 2013 3) November 2, 2014 The loss of assessment capability is reportable to the NRC within 8 hours of discovery in accordance with 10 CFR 50.72 (b)(3)(xiii) This report is required per 10 CFR 50.72(1)(1)(ii) as an event that occurred within 3 years of the date of discovery. The NRC Resident Inspector has been notified. Notified the R3DO (Valos).