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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5667310 August 2023 04:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor TripThe following information was provided by the licensee via email: At 0039 (EDT) on 8/10/23, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped during a reactor protection system (RPS) bus shift. All systems responding normally post-trip. There was no equipment inoperable at the time of the trip. Operations responded and stabilized the plant. Reactor water level being maintained via feedwater. Decay heat is being removed by cycling safety relief valves. An actuation of high-pressure core spray, division 3 diesel generator, and reactor core isolation cooling occurred during the scram and main steam line isolation closure. The reason for the auto-start was reaching Level 2 (130 inches in the reactor pressure vessel) during the transient. The systems automatically started as designed and injected to the reactor vessel when the Level 2 signal was received. The RPS actuation is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The emergency core cooling system (ECCS) injection is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). The ECCS actuation is being reported as a eight-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.Feedwater
Reactor Protection System
Reactor Core Isolation Cooling
Reactor Pressure Vessel
Core Spray
Emergency Core Cooling System
Main Steam Line
Safety Relief Valve
ENS 551726 April 2021 01:49:0010 CFR 50.72(b)(3)(iv)(A), System ActuationManual Reactor Protection System (RPS) Actuation at Zero Percent Power

At 2149 EDT on April 5, 2021, with the power plant in Mode 2 at zero percent power, an actuation of the RPS system occurred following the decision to abort plant start-up. The reason for the RPS actuation was to align the plant to Mode 3, from Mode 2, following manually inserting all control rods using the Rod Control System. The RPS system initiated as designed when the mode switch was taken from 'Start-up' to 'Shutdown' to align the plant to Mode 3 from Mode 2. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the RPS system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 5/12/21 AT 1345 EDT FROM JOHN NAKEL TO KERBY SCALES * * *

This is a retraction of an event notification made on 4/6/2021 at 0432 EST (EN#55172). This event was initially reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the RPS System. This event was later determined to be pre-planned, in accordance with Technical Specifications, and not the result of a significant event, therefore not meeting the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). On the evening of April 4, 2021, while commencing reactor start up, it was determined that control rod withdrawal to add positive reactivity for the start-up would not overcome the negative reactivity of plant heat up. The control room team determined that the proper course of action would be to insert all control rods . The control room briefed and notified the Outage Control Center about its decision, then proceeded to insert all control rods. The control room manually inserted all control rods using the control rod hydraulic system. Following insertion of all control rods, the mode switch was taken to the shutdown position to meet the prerequisites of the procedure for maintaining hot shutdown. This action establishes Mode 3 in accordance with Technical Specifications and aligns the plant to perform the necessary work prior to a plant restart. By placing the mode switch in the shutdown position, a scram signal is generated for 10 seconds. NUREG-1022 offers guidance that states 'Actuations that need not be reported are those initiated for reasons other than to mitigate the consequences of an event.' The actions the operating crew took that night are accurately described by this statement in NUREG-1022 'shifting alignment of makeup pumps or closing a containment isolation valve for normal operational purposes would not be reportable.' In this situation, the Mode switch was taken to shutdown to align the plant to mode 3 for normal operational purposes, and not to mitigate a significant event. When the mode switch was taken to shut-down, RPS initiated as designed, there was no mis-operation or unnecessary actuation. This actuation was determined to be pre-planned, in accordance with Tech Specs, and not the result of a significant event, therefore not meeting the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident has been notified. Notified R3DO (McGraw).

Reactor Protection System
Control Rod
ENS 5172911 February 2016 20:04:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Start of Emergency Diesel Generator and Loss of Shutdown CoolingAt 1504 EST on February 11, 2016, with the plant shutdown in a forced outage, the Division 1, 4.16 Kv Safety Bus (EH11) lost power. Division 1 Shutdown Cooling was in service at the time and the Division 1 Shutdown Cooling pump A tripped. The Division 1 Emergency Diesel Generator (EDG) started and loaded EH11 as designed. However, the Emergency Service Water (ESW) A pump, which supplies cooling water to the EDG did not start. Due to the absence of cooling water to the EDG, operators took manual action to secure the Division 1 EDG. Division 2 Shutdown Cooling was operable during this transient and was subsequently started. The Division 1 Shutdown Cooling common suction isolation valve (1E12F0008) had previously been de-energized in the open position to support planned maintenance. The Division 2 Shutdown Cooling isolation valve was not affected by the loss of bus EH11. Shutdown Cooling was re-established at 1544 EST using the Division 2 Shutdown Cooling pump. Reactor coolant temperature rose from approximately 89 degrees Fahrenheit to 115 degrees Fahrenheit during the event. The cause of the loss of EH11 and subsequent failure of ESW A pump to start are currently under investigation. This event is being reported under 10 CFR 50.72(b)(3)(iv)(A) as a specific system actuation due to the auto start of the Division 1 EDG on a valid signal. The plant remains shutdown with Division 2 Shutdown Cooling in operation. The plant is in a normal electrical line up with the exception of bus EH11 being de-energized. The licensee notified the NRC Resident Inspector.Service water
Emergency Diesel Generator
Shutdown Cooling
ENS 506017 November 2014 13:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram Due to Loss of FeedwaterThe Perry Nuclear Power Plant experienced an automatic reactor scram due to a loss of feedwater, which resulted in receiving valid reactor vessel water Level 3 and Level 2 initiation signals. The High Pressure Core Spray system and the Reactor Core Isolation Cooling system started and injected. Reactor water level and pressure have been stabilized in the required bands. The motor feed pump automatically started and is being used to control reactor vessel water level. The High Pressure Core Spray and Reactor Core Isolation Cooling systems have been returned to the standby mode. As a result of receiving a reactor vessel water Level 2 signal a Balance of Plant containment isolation signal was received. All systems isolated as required and the plant is restoring isolated systems in accordance with plant procedures. During the scram, all rods fully inserted into the core. Decay heat is being removed via turbine bypass valves to the main condenser. The electrical grid is stable and is supplying plant loads. An emergency diesel generator (Division 3 High Pressure Core Spray) started, as designed, as a result of the reactor vessel water Level 2 signal. No safety relief valves lifted as a result of the transient. The plant is stable with cooldown and depressurization to Mode 4 in progress. The cause of the loss of feedwater is under investigation. The NRC Resident Inspector has been notified. The State of Ohio and local officials will be notified.Feedwater
Emergency Diesel Generator
Reactor Core Isolation Cooling
High Pressure Core Spray
Safety Relief Valve
Main Condenser
ENS 5055120 October 2014 06:18:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram on Loss of Feedwater

The Perry Power Plant experienced a reactor scram during a shift of non-essential vital power supply to the alternate source. Feedwater was lost resulting in receiving a valid level 3 and level 2 signal. High Pressure Core Spray and Reactor Core Isolation Cooling started and injected. Reactor level and pressure have been stabilized to required bands. The motor feed pump has been started and is controlling level. High Pressure Core Spray and Reactor Core Isolation Cooling have been returned to standby. During the scram, all rods fully inserted into the core. Decay heat is being removed via the steam dumps to the condenser. The electrical grid is stable and supplying plant loads. An emergency diesel generator started, as designed, as a result of the level 2 signal but did not load. No safety valves lifted as a result of the transient. The cause of the loss of feedwater is under investigation. The licensee will be notifying the State of Ohio and Perry Township and has notified the NRC Resident Inspector.

  • * * UPDATE FROM DOUG SHORTER TO HOWIE CROUCH AT 0933 EDT ON 10/20/14 * * *

The plant is currently in Mode 3, stable with cooldown and depressurization to Mode 4 in progress. Level control is being provided by the motor feedwater pump. Troubleshooting of the cause of the scram and loss of feed water is on-going. The initial notification identified 10CFR50.72(b)(3)(iv)(A), 'Specified System Actuation', as a reporting criteria. The specific system that actuated was not provided. As a result of receiving a reactor vessel water level 2 signal a containment/BOP isolation signal was received. All systems isolated as required and the plant is restoring isolated systems in accordance with procedure. The licensee will be notifying the State of Ohio and Perry Township and has notified the NRC Resident Inspector. Notified R3DO (Pelke).

Feedwater
Emergency Diesel Generator
Reactor Core Isolation Cooling
High Pressure Core Spray
ENS 4868822 January 2013 08:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Protection System ActuationOn January 22, 2013, at approximately 0332 hours (EDT), an automatic Reactor Protection System (RPS) actuation occurred at the Perry Nuclear Power Plant, Unit 1. At the time of the event, the plant was in Mode 1 at 100% power. All control rods are inserted into the reactor core and the plant is currently stable in Mode 3 (Hot Shutdown) with reactor pressure and level being maintained in the normal shutdown range. The RPS actuation was initiated by a low reactor water level (Level 3 - 178") signal. In response to the RPS actuation and subsequent reactor Level 2 (130") signal, the High Pressure Core Spray (HPCS) system and Reactor Core Isolation Cooling (RCIC) system both actuated and injected to maintain reactor coolant level. The reactor level is currently being maintained in its normal band by the feedwater system and decay heat is being removed by (turbine bypass valves to) the condenser (both HPCS and RCIC have been returned to standby). The plant is in a normal electrical line-up with all three Emergency Diesel Generators operable and available, if needed. The Containment Isolation Valves (responded to the Level 2 and 3) isolation signals as designed. The cause of the RPS actuation is under investigation. The NRC Resident Inspector has been notified.Feedwater
Reactor Protection System
Emergency Diesel Generator
Reactor Core Isolation Cooling
High Pressure Core Spray
Control Rod
05000440/LER-2013-001
ENS 4380828 November 2007 12:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Reactor Scram and Eccs InjectionA reactor scram occurred at full power due to either a main turbine trip or loss of feedwater (cause is still under investigation). All rods fully inserted. RCIC started as expected but tripped shortly thereafter on a preliminary indication of low suction pressure. The Digital Feedwater System backup motor driven feedwater pump did not function as required and reactor water level decreased to level 2 ( 130 inches). High Pressure Core Spray (HPCS) started automatically at level 2 and restored water level. Currently reactor water level is at 188 inches and reactor pressure is at 927 PSI. Decay heat is being removed via the turbine bypass valves. No other significant equipment was out of service at the time of the scram. The scram had no impact on offsite or onsite power availability. The licensee attempted to restore RCIC a second time and experienced another trip. In addition, the licensee attempted to restore the digital feedwater and was unsuccessful. Feedwater continues to be supplied as needed via the HPCS while the licensee attempts to restore RCIC and Digital Feedwater System. The licensee notified the NRC Resident Inspector.Feedwater
High Pressure Core Spray
05000440/LER-2007-004