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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5489711 September 2020 23:30:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded ConditionAt 1930 EDT, on September 11, 2020, Palisades Nuclear Plant was conducting ultrasonic data analysis from reactor vessel closure head in-service inspections. During this analysis, signals that display characteristics consistent with primary water stress corrosion cracking were identified in head penetration 34. No leak path signal was identified during ultrasonic testing. The plant was in cold shutdown at 0% power and in Mode 6 for a refueling outage at the time of discovery. Repair actions will be completed prior to plant startup from the outage. This condition has no impact to the health and safety of the public. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A) for degradation of a principal safety barrier. This is the only indication that is currently present, however, if additional indications are found, they will also be repaired prior to the plant startup. The licensee notified the NRC Senior Resident Inspector.
ENS 5374921 November 2018 05:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded Condition Identified During Surface Inspection of Reactor Head Nozzle PenetrationOn November 21, 2018, during an extent of condition review, after completion of ultrasonic testing, further interrogation of reactor vessel closure head (RVCH) penetration 36 was performed using eddy current testing. The testing detected three repairable indications. No indication of boric acid leakage was identified at this location during the bare metal visual inspection. Extent of condition review is complete on all RVCH penetrations. The plant was in cold shutdown at 0 percent power and in Mode 6 for a refueling outage at the time of discovery. Repair actions will be completed prior to plant startup from the outage. This condition has no impact to the health and safety of the public. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A) for degradation of a principal safety barrier. The licensee notified the NRC Senior Resident Inspector.
ENS 5373411 November 2018 04:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded Condition Due to Indication During Ultrasonic Inspection of Reactor Head Nozzle Penetration

On November 11, 2018, during ultrasonic data analysis from reactor vessel closure head in-service inspections, signals that display characteristics consistent with primary water stress corrosion cracking in head penetration 33 were identified. No indications of boric acid leakage and no surface indications were detected at this location during bare metal visual inspection.

The plant was in cold shutdown at 0% power and in Mode 6 for a refueling outage at the time of discovery. Repair actions will be completed prior to plant startup from the outage. This condition has no impact to the health and safety of the public. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A) for degradation of a principal safety barrier. The licensee notified the NRC Senior Resident Inspector.

ENS 5373310 November 2018 05:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedBoric Acid Identified on Reactor Vessel Head PenetrationOn November 10, 2018, during a planned bare metal visual inspection of the reactor head, boric acid was discovered at a CRDM (Control Rod Drive Mechanism) nozzle to reactor head penetration. Investigation of the source of the boric acid is ongoing. The plant was in cold shutdown at 0% power and Mode 6 for a refueling outage at the time of discovery. Repair actions will be completed prior to plant startup from the outage. All other reactor vessel head penetrations have had a bare metal visual inspection completed with no other indications identified. This condition has no impact to the health and safety of the public. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A) for degradation of a principal safety barrier. The licensee notified the NRC Senior Resident Inspector.
ENS 527222 May 2017 13:28:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedFailed Ultrasonic Testing of Weld

On May 2, 2017, during planned inspections, an ultrasonic examination performed on weld PCS-4-PRS-1P1-1, revealed an axial indication in the pressurizer nozzle to safe end area of the weld. This indication does not meet applicable acceptance criteria under ASME, Section XI. The plant was in cold shutdown at 0% power for a planned refueling outage at the time of discovery. The condition will be resolved prior to plant startup. This condition has no impact to the health and safety of the public. The licensee notified the NRC Senior Resident Inspector. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A), since an indication was found that did not meet acceptance criteria referenced in ASME Code, Section XI.

  • * * RETRACTION ON 5/9/17 AT 1303 EDT FROM BARBARA DOTSON TO BETHANY CECERE * * *

Additional evaluations of the recorded indication concluded that the indication was attributed to an erroneous ultrasonic response. This was the result of a combined effect of compromised surface contact at the area of the recorded indication and associated examination scan speed. The contact issue is attributed to the specific tooling configuration required for this exam. The combination of these factors resulted in the introduction of an erroneous reflector in the area of interest that had characteristics of a relevant indication. The vendor repeated the entire examination for axial flaws and there were no service induced indications recorded. A review of the newly acquired data by site, vendor and EPRI personnel confirmed that no service induced flaws are present. The licensee has notified the NRC Resident Inspector. Notified the R3DO (Hills).

ENS 497965 February 2014 18:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded Condition Discovered on Pressurizer Nozzle Weld During TestingOn February 5, 2014, during planned inspections, an ultrasonic examination performed on weld PCS-6-PRS-1C1-1 (RV-1041) revealed two axial indications in the root area of the weld. The weld containing the indications is the nozzle to safe end dissimilar metal weld on the flange for pressurizer safety valve RV-1041. These two indications do not meet applicable acceptance criteria under ASME, Section XI, IWB-3600, 'Analytical Evaluation of Flaws,' or ASME Section Xl, Table IWB-3410, 'Acceptance Standards,' and will require a repair or replacement activity in order return the weld to an acceptable condition. The plant was in cold shutdown at 0% power for a planned refueling outage at the time of discovery. Replacement or repair actions will be completed prior to plant startup from the outage. This condition has no impact to the health and safety of the public. The licensee notified the NRC Senior Resident Inspector. This report is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A), since indications were found that did not meet acceptance criteria referenced in ASME Code, Section XI.
ENS 4977329 January 2014 14:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedIndications Identified on Control Rod Drive Mechanism HousingsOn January 29, 2014, during planned inspections of control rod drive mechanism (CRDM) upper housings, it was determined that the inspection results for some housings did not meet the applicable acceptance criteria. That is, evaluations of the housing indications are being performed under ASME Code, Section XI, IWB-3600, 'Analytical Evaluation of Flaws,' and indications were identified that exceed acceptance criteria specified in the Code. None of the indications were through-wall and there was no evidence of leakage. The housing indications, varying in depth and length characteristics, were identified in 17 of the 45 CRDM housings inspected. All 45 CRDM housings were inspected, which constituted 100% extent of condition inspection. The plant was in cold shutdown at 0% power for a planned refueling outage at the time of discovery. Replacement or repair actions are in progress and will be completed prior to plant startup from the outage. This condition has no impact to the health and safety of the public. This report is being made in accordance with 10CFR 50.72(b)(3)(ii)(A), since indications were found that did not meet acceptance criteria referenced in ASME Code, Section XI. The licensee notified the NRC Senior Resident Inspector.Control Rod
ENS 4818212 August 2012 08:18:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDegraded Condition Reported Based on the Discovery of Pressure Boundary LeakageFollowing a planned shutdown to investigate the source of elevated Primary Coolant System (PCS) Unidentified Leakage, the Mode 3 PCS walk-down identified a steam leak on CRD-24, Control Rod Drive Mechanism (CRD), pressure housing. The leak is ~ 1 foot above the CRD to Reactor Head flange. The leak was observed from the Refueling floor deck and appears to be coming from an area of the CRD with no bolted connections. Leakage from this area is unexpected and the mechanism of failure is not understood at this time. Closer examination of the leak is expected to occur in parallel with plant cool-down. The plant entered T.S. 3.4.14 (PCS Operational Leakage) Condition B. at 0418 EDT hours this morning and this requires the plant to be placed in Mode 5 within 36 hours. The leakage is considered Pressure Boundary Leakage. Operations is in progress of performing the plant cool-down from Mode 3 to Mode 5. The licensee discovered this condition following a shutdown the morning of 8/12/12 to investigate unidentified primary coolant leakage of about 0.3 gpm that had been recently trending upwards. Plant conditions are currently 400 degrees F with primary system pressure at about 1000 psi. The licensee has notified the NRC Resident InspectControl Rod
ENS 4112816 October 2004 21:30:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedReactor Vessel Head Nozzle Cracking

On 10/16/04, with the Plant in Mode 6, Nuclear Management Company identified through wall cracks in the inconel buttering adjacent to the J-weld on reactor head penetrations 29 and 30. Ultrasonic examinations of the reactor vessel head were being performed in accordance with the First Revised Order, EA-03-009. The ultrasonic examinations identified leak path detection indications. Therefore, in accordance with the Order, a bare metal visual inspection of the exterior of the reactor head was performed. No evidence of leakage was discovered. A dye-penetrant examination was then performed. The dye-penetrant exam showed minor surface indications that required further examination. Following minor excavation of the weld surface, the through wall cracks were identified. This condition was determined to be reportable at 1730 EST for penetration 30, and at 1915 EST for penetration 29. This notification is being made in accordance with 10 CFR 50.72(b)(3)(ii)(A). Reactor head penetrations 29 and 30 will be repaired prior to placing the reactor vessel head back in service. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 11/19/14 AT 1434 EST FROM TERRY DAVIS TO DONG PARK * * *

On October 17, 2004, Nuclear Management Company notified the NRC, via non-emergency event report 41128 that leak path detection indications had been identified in two reactor pressure vessel head control rod drive mechanism nozzle penetrations at Palisades. At that time, the probable cause of the identified indications was believed to be primary water stress corrosion cracking (PWSCC). As a result, event report 41128 was made in accordance with 10 CFR 50.72(b)(3)(ii)(A) as a condition that resulted in a principle safety barrier being seriously degraded. Based on a recently completed engineering evaluation that compared the indications found in 2004 to the indications identified in subsequent examinations, it was determined the indications originally discovered in 2004 were embedded welding indications, caused by the original welding process. Since the indications identified in 2004 were not caused by PWSCC, serious degradation of a principle safety barrier did not exist. Consequently, the reporting criterion of 10 CFR 50.72(b)(3)(ii)(A) is not applicable. Therefore, event report 41128 is being retracted. In addition, Palisades Licensee Event Report (LER), 2004-002, 'Leak Path Indications Identified in Reactor Pressure Vessel Head Nozzle Penetrations,' is being cancelled. The licensee has notified the NRC Resident Inspector. Notified R3DO (Peterson).

Reactor Pressure Vessel
Control Rod