ENS 52406
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ENS Event | |
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03:24 Dec 4, 2016 | |
Title | Automatic Reactor Trip Caused by Main Turbine Trip |
Event Description | On 12/3/16 at 2224 EST, Calvert Cliffs Unit-2 experienced an automatic reactor trip from full power due to a leak in the Unit-2 Main Turbine Electro-Hydraulic Control (EHC) system. The EHC leak caused the Unit-2 Main Turbine governor valves to close, resulting in a turbine trip and automatic reactor trip. The site Outage Control Center is manned, and investigation into the cause of the leak is underway. Unit-2 remains stable in Mode 3 with normal heat removal.
Unit-1 remains at full power and was not affected by the trip. The plant is in a normal shutdown electrical lineup. All Control rods fully inserted and no primary or secondary safety relief valves lifted during the trip. The licensee has notified the NRC Resident Inspector. The licensee will be notifying Calvert County. |
Where | |
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Calvert Cliffs Maryland (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1.6 h-0.0667 days <br />-0.00952 weeks <br />-0.00219 months <br />) | |
Opened: | Ervin Lyson 01:48 Dec 4, 2016 |
NRC Officer: | Jeff Rotton |
Last Updated: | Dec 4, 2016 |
52406 - NRC Website | |
Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 569912024-02-24T20:46:00024 February 2024 20:46:00
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