ENS 48310
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ENS Event | |
|---|---|
00:25 Sep 15, 2012 | |
| Title | Automatic Reactor Trip Due to Low Steam Generator Water Level |
| Event Description | [At] 2025 [EDT] reactor tripped on 'C' Steam Generator Low Low Level due to feed water regulating valve failing closed due to a 7300 process cabinet card failure. Control Room entered E-0, Reactor Trip or Safety Injection, then transitioned to ES-0.1, Reactor Trip Response.
Emergency Feedwater actuated due to the Low Low Steam Generator Level. All other plant equipment functioned as expected. Plant is being stabilized in mode 3. Emergency News Manager will update the states and local media. NRC Resident Inspector was notified at 2045 [EDT]. The trip was uncomplicated and all rods fully inserted. Decay heat is being removed to the condenser via the turbine bypass valves. Electrical buses are powered by offsite power. |
| Where | |
|---|---|
| Seabrook New Hampshire (NRC Region 1) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
| Time - Person (Reporting Time:+-2.33 h-0.0971 days <br />-0.0139 weeks <br />-0.00319 months <br />) | |
| Opened: | Shawn Miller 22:05 Sep 14, 2012 |
| NRC Officer: | Dong Park |
| Last Updated: | Sep 14, 2012 |
| 48310 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | A/R |
| Before | Power Operation (85 %) |
| After | Hot Standby (0 %) |
WEEKMONTHYEARENS 574322024-11-19T18:50:00019 November 2024 18:50:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 566452023-07-30T19:26:00030 July 2023 19:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to LOW Main Turbine ELECTRO-HYDRAULIC Control (EHC) Oil Level ENS 547402020-06-06T13:20:0006 June 2020 13:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip When Group One, Bank 'B' Control Rods Inserted Into the Core ENS 547312020-05-29T18:03:00029 May 2020 18:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Rod Bank Unexpectedly Inserting ENS 527182017-04-29T22:44:00029 April 2017 22:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Steam Generator Hi-Hi Level Signal and Feedwater Isolation ENS 517622016-03-02T07:53:0002 March 2016 07:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Causing a Reactor Trip ENS 499792014-04-01T04:26:0001 April 2014 04:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Electrical Issue ENS 483102012-09-15T00:25:00015 September 2012 00:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 473272011-10-06T16:26:0006 October 2011 16:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 439212008-01-20T04:02:00020 January 2008 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 416552005-05-01T15:09:0001 May 2005 15:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Turbine High Vibration ENS 402862003-11-01T00:48:0001 November 2003 00:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip on Low Steam Generator Water Level 2024-11-19T18:50:00 | |
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