ENS 40286
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ENS Event | |
|---|---|
00:48 Nov 1, 2003 | |
| Title | Reactor Trip on Low Steam Generator Water Level |
| Event Description | Automatic Reactor Trip due to low Steam Generator levels. All systems responded normally. Plant is stable at NOT/NOP [normal operating temperature and pressure] in Mode 3. Emergency Feedwater system actuated as designed due to reactor trip.
Lowest Steam Generator level reached was just below the trip setpoint of 25%. Low level caused by trip of one of two Main Feed Pumps. All control rods fully inserted. No primary or secondary relief valves lifted. The electrical system is stable and the EDG's remain in standby. Decay heat is being removed via steam dumps. The licensee has notified the NRC Resident Inspector. |
| Where | |
|---|---|
| Seabrook New Hampshire (NRC Region 1) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
| LER: | 05000443/LER-2003-002 Regarding Reactor Trip Following the Loss of a Main Feed Pump |
| Time - Person (Reporting Time:+-3.55 h-0.148 days <br />-0.0211 weeks <br />-0.00486 months <br />) | |
| Opened: | Tom Waechter 21:15 Oct 31, 2003 |
| NRC Officer: | Mike Ripley |
| Last Updated: | Oct 31, 2003 |
| 40286 - NRC Website
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Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | A/R |
| Before | Power Operation (100 %) |
| After | Hot Standby (0 %) |
Seabrook | |
WEEKMONTHYEARENS 574312024-11-19T18:50:00019 November 2024 18:50:00
[Table view]10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 574322024-11-19T18:50:00019 November 2024 18:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 566452023-07-30T19:26:00030 July 2023 19:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to LOW Main Turbine ELECTRO-HYDRAULIC Control (EHC) Oil Level ENS 565652023-05-06T19:52:0006 May 2023 19:52:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Actuations of Reactor Protection System ENS 565642023-04-12T15:07:00012 April 2023 15:07:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of "B" Emergency Diesel Generator Emergency Power Sequencer ENS 547402020-06-06T13:20:0006 June 2020 13:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip When Group One, Bank 'B' Control Rods Inserted Into the Core ENS 547312020-05-29T18:03:00029 May 2020 18:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Rod Bank Unexpectedly Inserting ENS 527182017-04-29T22:44:00029 April 2017 22:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Steam Generator Hi-Hi Level Signal and Feedwater Isolation ENS 517652016-03-02T18:12:0002 March 2016 18:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Emergency Feedwater ENS 517622016-03-02T07:53:0002 March 2016 07:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Causing a Reactor Trip ENS 499792014-04-01T04:26:0001 April 2014 04:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Electrical Issue ENS 483102012-09-15T00:25:00015 September 2012 00:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 473272011-10-06T16:26:0006 October 2011 16:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 454032009-10-02T02:39:0002 October 2009 02:39:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Experienced a Valid Rps Actuation During Plant Cooldown on Low Steam Generator Levels ENS 439212008-01-20T04:02:00020 January 2008 04:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 416552005-05-01T15:09:0001 May 2005 15:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Main Turbine High Vibration ENS 415932005-04-13T08:50:00013 April 2005 08:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation During Core Reload Reactor Trip Breakers Opened ENS 414282005-02-22T08:08:00022 February 2005 08:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator and Emergency Feedwater Auto Start on Vital Bus Failure to Transfer ENS 402862003-11-01T00:48:0001 November 2003 00:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip on Low Steam Generator Water Level 2024-11-19T18:50:00 | |
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